ENS 47817
ENS Event | |
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09:29 Apr 9, 2012 | |
Title | Valid Emergency Diesel Generator Actuation |
Event Description | On April 9, 2012, at 0529 hours0.00612 days <br />0.147 hours <br />8.746693e-4 weeks <br />2.012845e-4 months <br />, electrical power was lost to the 4160v emergency bus E1. Activities to support testing of emergency bus E1 were in progress when technicians connected a recorder across the terminals of an under-voltage relay on emergency bus E1 and caused the normal supply breakers for emergency bus E1 to open.
The power loss to emergency bus E1 affected both Unit 1 and Unit 2. Emergency diesel generator #1 automatically started and re-energized the E1 emergency bus. Unit 1 was in Mode 5 and electrical systems were aligned to support testing of emergency bus E1. As a result, no other safety system isolations or actuations occurred. Per design, no Unit 2 safety system isolations or actuations occurred. The safety significance of this event is minimal. Safety systems functioned as designed when emergency bus E1 de-energized. There was no interruption of Unit 1 shutdown cooling as a result of this event. Normal power supply was restored to emergency bus E1 and emergency diesel generator #1 was shutdown at 0701 hours0.00811 days <br />0.195 hours <br />0.00116 weeks <br />2.667305e-4 months <br />. Reporting requirements met by this notification: 10CFR50.72(b)(3)(iv)(A) with specified system in 10CFR50.72(b)(3) (iv)(B)(8). The NRC Resident Inspector has been notified. |
Where | |
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Brunswick North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-0.23 h-0.00958 days <br />-0.00137 weeks <br />-3.15054e-4 months <br />) | |
Opened: | Lee Goldstein 09:15 Apr 9, 2012 |
NRC Officer: | Mark Abramovitz |
Last Updated: | Apr 9, 2012 |
47817 - NRC Website | |
Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 569772024-02-19T04:25:00019 February 2024 04:25:00
[Table view]10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Start of Emergency Diesel Generator ENS 564782023-04-20T05:48:00020 April 2023 05:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Turbine Trip ENS 556272021-12-06T16:25:0006 December 2021 16:25:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Safety System Actuation ENS 540162019-04-22T03:07:00022 April 2019 03:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Reactor Trip and Specified System Actuation ENS 539662019-03-30T21:47:00030 March 2019 21:47:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram and Specified System Actuation ENS 539622019-03-28T20:54:00028 March 2019 20:54:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of the Primary Containment Isolation System and the Reactor Protecton System ENS 539552019-03-25T08:02:00025 March 2019 08:02:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Start of Four Emergency Diesel Generators ENS 539112019-03-05T10:35:0005 March 2019 10:35:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of the Primary Containment Isolation System ENS 533192018-04-07T12:36:0007 April 2018 12:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip and Pcis Actuation During Stator Cooling System Testing ENS 529742017-09-17T13:38:00017 September 2017 13:38:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator and Primary Containment Isolation System Actuations ENS 526832017-04-17T04:04:00017 April 2017 04:04:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of Emergency Diesel Generators ENS 517152016-02-07T18:26:0007 February 2016 18:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Scram and Alert Declaration Due to Electrical Fault Resulting in Fire/Explosion ENS 478172012-04-09T09:29:0009 April 2012 09:29:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Emergency Diesel Generator Actuation ENS 476972012-02-24T05:37:00024 February 2012 05:37:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Reactor Protection System Actuation During Neutron Instrument Testing ENS 476902012-02-23T04:19:00023 February 2012 04:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to High Delta-P Across Circulating Water Pump Traveling Screens ENS 459022010-05-05T15:44:0005 May 2010 15:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Reactor Feed Pump Trip ENS 457322010-02-27T06:58:00027 February 2010 06:58:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Core Isolation Cooling (Rcic) System Manually Started to Maintain Reactor Pressure Vessel Level Following a Pre-Planned Reactor Scram ENS 453752009-09-21T18:46:00021 September 2009 18:46:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Protection System and Primary Containment Isolation System Actuation After Placing Hpci System Inservice ENS 451902009-07-08T14:13:0008 July 2009 14:13:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Emergency Diesel Generator Actuation ENS 446852008-11-26T17:00:00026 November 2008 17:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Ehc Malfunction ENS 446472008-11-09T16:08:0009 November 2008 16:08:00 Other Unspec Reqmnt, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Spurious Srv Opening ENS 444532008-08-30T19:03:00030 August 2008 19:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Electro-Hydraulic Control Malfunction Leads to Reactor Scram ENS 430622006-12-25T10:39:00025 December 2006 10:39:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Reactor Scram Due to Trip from Neutron Monitoring System ENS 429862006-11-11T17:43:00011 November 2006 17:43:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scram Due to Conductivity Excursion ENS 429552006-11-01T23:37:0001 November 2006 23:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unit 2 Declared an Unusual Event Due to Loss of Offsite Power to the 4Kv Emergency Buses ENS 418372005-07-13T13:17:00013 July 2005 13:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip/Reactor Trip ENS 415822005-04-09T05:50:0009 April 2005 05:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scrammed from 61% Power Due to Low Reactor Water Level ENS 402972003-11-04T22:32:0004 November 2003 22:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Brunswick Unit 2 Scram Due to Generator/Turbine Trip 2024-02-19T04:25:00 | |