05000324/FIN-2015007-02
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Finding | |
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Title | Insufficient Material Evaluation of Commercially Dedicated Allen Bradley Relays |
Description | An NRC-identified Green NCV of 10 CFR Part 50, Appendix B, Criterion III, Design Control was identified for the licensees inadequate commercial grade dedication technical evaluation that resulted in non-conforming relays being installed in the control circuits for emergency diesel generator output breakers. This led to specification of a relay that was unsuitable for the application being installed in the control circuit for two emergency diesel generator output breakers and failure of one of those breakers to close. The licensee documented this issue in their corrective action program and performed corrective actions to mitigate the effects of the undetected changes on the relay. The inspectors determined that the finding was more than minor in accordance with Manual Chapter 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated September 7, 2012, because, if the process for detecting commercial grade item changes using material evaluations was left uncorrected, additional undetected design or process changes would likely occur. Using Manual Chapter 0609, Appendix A, issued June 19, 2012, The Significance Determination Process (SDP) for Findings At-Power, the inspectors determined the finding required a detailed risk evaluation because the effect on two emergency diesel generators was considered a loss of function. For Unit 1, the regional Senior Reactor Analyst used demand data to adjust the probability that an emergency diesel generator would fail to start and ran a condition assessment on SAPHIRE. Because of limited exposure time, the finding was determined to be Green for Unit 1. For Unit 2, the conditions for exposure occurred during an outage with the reactor cavity filled, and both EDGs would be available. The SRA determined the significance to be bounded by the at power risk analysis performed for Unit 1. Because of the low exposure time, and the high likelihood of operators recovering the failure to start of the EDGs, this issue was Green for Unit 2. The inspectors did not identify a crosscutting aspect associated with this finding because the original relay evaluation was done in 1999 and was not indicative of current licensee performance. |
Site: | Brunswick |
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Report | IR 05000324/2015007 Section 4OA2 |
Date counted | Jun 30, 2015 (2015Q2) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | A Masters C Oelstrom D Retterer M Cain N Staples R Taylor S Freeman T Stephen A Armstrong |
Violation of: | 10 CFR 50 Appendix B Criterion III, Design Control |
INPO aspect | |
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Finding - Brunswick - IR 05000324/2015007 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Brunswick) @ 2015Q2
Self-Identified List (Brunswick)
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