ENS 42572
ENS Event | |
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21:40 Mar 14, 2006 | |
Title | Inadvertant Core Spray Pump Actuation |
Event Description | The notification is being made pursuant to 10CFR50.73(a)(2) (iv) (A) and is reported per 10CFR50.73(a)(1)
An invalid actuation of the 1 C Core Spray Pump start during D13 LOCA/LOOP Testing. a) The specific train(s) and system(s) that were actuated. The 1C Core Spray Pump actuated automatically on an inadvertent Division 3 LOCA signal during LOCA/LOOP testing. No other ECCS train/system actuated. b) Whether each train actuation was complete or partial. The 1C Core Spray Pump actuated in the minimum flow protection mode. c) Whether or not the system started and functioned successfully. The 1 C Core Spray System started and functioned successfully but did not inject into the vessel. On March 14, 2006 at 5:40 PM during performance of the D13 LOCA/LOOP Test, ST-6-092-117-1, the 1 C Core Spray pump was inadvertently started. The pump started (but did not inject) when an I&C Technician attempted to demonstrate operation of the test switch. He inadvertently picked up the energized test switch which was next to 2 spare test switches and manipulated it which resulted in a Division 3 LOCA signal to the 1C Core Spray Pump. The 1C Core Spray Pump never injected and was running with min-flow protection and functioned as expected. The cause of the event was lack of attention to detail and self check. The licensee notified the NRC Resident Inspector. |
Where | |
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Limerick Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1405.92 h58.58 days <br />8.369 weeks <br />1.926 months <br />) | |
Opened: | Roy Harding 10:35 May 12, 2006 |
NRC Officer: | Mark Abramovitz |
Last Updated: | May 12, 2006 |
42572 - NRC Website
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WEEKMONTHYEARENS 564642023-02-16T12:05:00016 February 2023 12:05:00
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