ENS 44952
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ENS Event | |
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22:05 Apr 1, 2009 | |
Title | Unplanned Manual Reactor Trip |
Event Description | At 1805, due to lowering Condenser Vacuum caused by ingress of algae and seaweed, Unit 2 was manually tripped. Power had been reduced to 94% for the securing of one Circulating Water Pump (2A1). It was then identified that 2A2 Circulating Water Debris filter differential pressure was above administrative limits of 200 inches water. While the station was making preparations to reduce Circulating water flow on the 2A2 Circulating Water Pump, the unit began losing condenser vacuum. Plant was manually tripped at 92% power. All CEA's fully inserted on the trip. Auxiliary Feedwater automatically initiated on Low Steam Generator Level. No PZR PORVS opened. RCS Heat removal is now being maintained with Main Feedwater and Steam Bypass control system. All systems functioned normally, and plant is stabilized at normal operating Temperature and Pressure. This non-emergency notification is being made pursuant to 10 CFR 50.72(b)(2)(iv)(B) due to manual RPS actuation and 10 CFR 50.72(b)(3)(iv)(B) due to PWR auxiliary feedwater system actuation.
There was no impact on Unit 1. The licensee informed the Resident Inspector. |
Where | |
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Saint Lucie Florida (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-1.23 h-0.0513 days <br />-0.00732 weeks <br />-0.00168 months <br />) | |
Opened: | Noel Pitoniak 20:51 Apr 1, 2009 |
NRC Officer: | Steve Sandin |
Last Updated: | Apr 1, 2009 |
44952 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (92 %) |
After | Hot Standby (0 %) |
Saint Lucie with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 572492024-07-28T22:37:00028 July 2024 22:37:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 571772024-06-18T07:17:00018 June 2024 07:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip ENS 571612024-06-04T17:52:0004 June 2024 17:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip ENS 560872022-09-03T02:48:0003 September 2022 02:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Feed Pump ENS 556412021-12-10T15:24:00010 December 2021 15:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip ENS 550782021-01-20T23:22:00020 January 2021 23:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Trip of Motor Control Center ENS 542622019-09-07T12:24:0007 September 2019 12:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 540272019-04-25T13:18:00025 April 2019 13:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Turbine Generator Trip ENS 537032018-10-29T04:00:00029 October 2018 04:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Inadequate Feedwater Flow ENS 536652018-10-12T04:00:00012 October 2018 04:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 530362017-10-26T06:12:00026 October 2017 06:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Following a Loss of Load ENS 527572017-05-15T22:00:00015 May 2017 22:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Emergency Diesel Generator Signal Generated Upon Loss of 4160V Power ENS 521912016-08-21T23:37:00021 August 2016 23:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event - Loss of Offsite Power ENS 514232015-09-17T16:22:00017 September 2015 16:22:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of Uv Relays Following Loss of Unit 2 Startup Transformer ENS 513022015-08-10T02:15:00010 August 2015 02:15:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip During Testing ENS 506072014-11-12T20:48:00012 November 2014 20:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Lowering Steam Generator Water Level ENS 495362013-11-14T17:18:00014 November 2013 17:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Low Level in the 2B Steam Generator ENS 495282013-11-12T05:02:00012 November 2013 05:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Unisolable Leak in Digital Electro-Hydraulic System ENS 490822013-05-31T11:12:00031 May 2013 11:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to an Anticipated Loss of Condenser Cooling ENS 488182013-03-12T18:51:00012 March 2013 18:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip on Thermal Margin/Low Pressure ENS 483882012-10-08T01:40:0008 October 2012 01:40:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Essential Bus Deenergized While Defueled ENS 483692012-10-03T12:43:0003 October 2012 12:43:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Failure of Startup Transformer Caused Undervoltage Condition on Essential Bus ENS 479872012-06-02T23:35:0002 June 2012 23:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip Due to a Turbine Control System Failure ENS 479152012-05-11T07:55:00011 May 2012 07:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Feedwater Control Valve Failure ENS 477932012-03-31T04:22:00031 March 2012 04:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Uncontrolled Cooldown ENS 477522012-03-19T03:36:00019 March 2012 03:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Control Element Assembly Anomalous Behavior ENS 476572012-02-10T06:34:00010 February 2012 06:34:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Maintenance Activities Cause an Inadvertent Emergency Diesel Generator Start ENS 473532011-10-19T09:28:00019 October 2011 09:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip on Loss of Condenser Vacuum ENS 471782011-08-22T19:13:00022 August 2011 19:13:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Rising Condenser Backpressure ENS 469282011-06-06T07:29:0006 June 2011 07:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Error During Reactor Protection System Surveillance Leads to Reactor Trip ENS 460182010-06-16T21:10:00016 June 2010 21:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip After Two Control Rods Dropped ENS 458432010-04-15T19:39:00015 April 2010 19:39:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Manual Reactor Trip ENS 453742009-09-21T17:34:00021 September 2009 17:34:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Manual Reactor Trip During Reactor Startup ENS 449522009-04-01T22:05:0001 April 2009 22:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Manual Reactor Trip ENS 442762008-06-07T12:18:0007 June 2008 12:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Following the Trip of a Condensate Pump ENS 442682008-06-04T21:30:0004 June 2008 21:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Following Loss of Main Feedwater Pump ENS 439412008-01-29T10:31:00029 January 2008 10:31:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Manual Reactor Trip to Repair Rcp "2B1" Seal Package ENS 438742007-12-29T06:31:00029 December 2007 06:31:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip When Five Control Rods Unexpectedly Dropped 20 Inches ENS 426472006-06-16T02:23:00016 June 2006 02:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Digital Electro-Hydraulic Leak ENS 422772006-01-20T13:56:00020 January 2006 13:56:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Rps Actuation ENS 419112005-08-11T14:48:00011 August 2005 14:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip on a Condensate Pump Bus Lockout ENS 417152005-05-19T00:59:00019 May 2005 00:59:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Inadvertent De-Energization of 4160 V Safety Related A.C. Bus with Edg Auto Start ENS 412972004-12-27T22:20:00027 December 2004 22:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Following Problem with Steam Generator Water Level Control ENS 412932004-12-25T11:52:00025 December 2004 11:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Manually Tripped to Remove Failing Condensate Pump from Service ENS 410722004-09-26T03:56:00026 September 2004 03:56:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to a Loss of Offsite Power ENS 410182004-09-04T05:56:0004 September 2004 05:56:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Steam Generator Level Oscillations ENS 404032003-12-20T14:49:00020 December 2003 14:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rps Actuation Due to Loss of Turbine Generator Excitation ENS 403752003-12-04T21:32:0004 December 2003 21:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation St. Lucie Unit 2 Manual Reactor Trip Due to Loss of Condensate Pump 2024-07-28T22:37:00 | |
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