05000446/LER-2003-001, Actuation of Reactor Protection System

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Actuation of Reactor Protection System
ML032580453
Person / Time
Site: Comanche Peak Luminant icon.png
Issue date: 09/05/2003
From: Walker R
TXU Energy
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
10010, CPSES-200301531, TXX-03122 LER 03-001-00
Download: ML032580453 (6)


LER-2003-001, Actuation of Reactor Protection System
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation
4462003001R00 - NRC Website

text

0-Ahrxu aw, TXU Energy Comanche Peak Steam Electric Station P.O. Box 1002 (E01)

Glen Rose, TX 76043 Tel: 254 897 8920 Fac 254 897 6652 lance.terry@txu.com C. Lance Terry Senior Vice President &

Principal Nuclear Officer Ref: 10CFR50.73(a)(2)(iv)(A)

CPSES-200301531 Log# TXX-03122 File # 10010 September 5, 2003 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555

SUBJECT:

COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)

DOCKET NO. 50-446 ACTUATION OF REACTOR PROTECTION SYSTEM LICENSEE EVENT REPORT 446/03-001-00 Gentlemen:

Enclosed is Licensee Event Report (LER) 03-001-0 for Comanche Peak Steam Electric Station Unit 2, " Reactor Trip Due To Loss of Reactor Coolant Pump."

This communication contains no new licensing basis commitments regarding CPSES Units 1 and 2.

QrTXu TXX-03122 Page 2 of 2 Sincerely, TXU Generation Company LP By:

TXU Generation Management Company LLC, Its General Partner C. L. Terry Senior Vice President and Principal Nuclear Officer By: 6?2e Z.5 Rogtr D. Walker Regulatory Affairs Manager GLM/gm Enclosures c -

T. P. Gwynn, Region IV W. D. Johnson, Region IV M. C. Thadani, NRR Resident Inspectors, CPSES

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COMANCHE PEAK STEAM ELECTRIC STATION UNIT 2 05000446 1 OF4 Tide (4)

ACTUATION OF REACTOR PROTECTION SYSTEM Evaw Due

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. DESCRIPTION OF REPORTABLE EVENT A.

REPORTABLE EVENT CLASSIFICATION

Any event or condition that resulted in manual or automatic actuation of the Reactor Protection System (RPS) including reactor trip or reactor scram.

B.

PLANT OPERATING CONDITIONS PRIOR TO THE EVENT On July 9, 2003, Comanche Peak Steam Electric Station (CPSES) Unit 2 was in Mode 1, Power Operation, operating at 100 percent power.

C.

STATUS OF STRUCTURES, SYSTEMS, OR COMPONENTS THAT WERE INOPERABLE AT THE START OF THE EVENT AND THAT CONTRIBUTED TO THE EVENT There were no inoperable structures, systems, or components that contributed to the event.

D.

NARRATIVE SUMMARY OF THE EVENT, INCLUDING DATES AND APPROXIMATE TIMES On July 9, 2003, Comanche Peak Steam Electric Station (CPSES) Unit 2 was in Mode 1, Power Operation, operating at 100% power. At 0109 hours0.00126 days <br />0.0303 hours <br />1.802249e-4 weeks <br />4.14745e-5 months <br />, the 2-04 Reactor Coolant Pump (RCP) motor breaker [EIIS: (AB)(P)(MO)(BKR)] unexpectedly opened which resulted in loss of the 2-04 RCP. Operators (utility, licensed) in the Unit 2 Control Room received a "Rx > 48 percent 1 of 4 loop flow low trip" alarm which resulted in an automatic reactor trip. All control rods fully inserted, all Auxiliary Feedwater pumps [EHS: (BA)(P)] automatically started as expected, and the unit was stabilized in Mode 3.

E.

THE METHOD OF DISCOVERY OF EACH COMPONENT OR SYSTEM FAILURE, OR PROCEDURAL OR PERSONNEL ERROR Operators (utility, licensed) in the Unit 2 Control Room received a "Rx > 48 percent I of 4 loop flow low trip" alarm.

NRC: RMM 306

(-2001)

Enclosure to TXX-03122

I, NRCOIORM 366A U.S. NUC.RAR REGULATORY COMMISSION (1-2OI)

LICENSEE EVENT REPORT (LER)

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II.

COMPONENT OR SYSTEM FAILURES A.

FAILURE MODE, MECHANISM, AND EFFECTS OF EACH FAILED COMPONENT TXU Energy's evaluation of this event determined that a "B" phase stator to ground short occurred in the 2-04 RCP motor.

B.

CAUSE OF EACH COMPONENT OR SYSTEM FAILURE The "B" phase stator to ground short occurred in the 2-04 RCP motor due to degradation of the stator ground wall insulation.

C.

SYSTEMS OR SECONDARY FUNCTIONS THAT WERE AFFECTED BY FAILURE OF COMPONENTS WITH MULTIPLE FUNCTIONS Not applicable - No failures of components with multiple functions were identified.

D.

FAILED COMPONENT INFORMATION

Westinghouse S/N 89P969 Model #CS-VSS 7000 HP, 6600 volt, 6 pole, Reactor Coolant Pump Motor 11.

ANALYSIS OF THE EVENT

A.

SAFETY SYSTEM RESPONSES THAT OCCURRED The Reactor Protection System and the Auxiliary Feedwater System actuated as expected during the event Both Motor Driven Auxiliary Feedwater pumps and the Turbine Driven Auxiliary Feedwater pump automatically started as expected based on Lo-Lo level in 2 of 4 Steam Generators. All control rods fully inserted and the plant response to the automatic trip was as expected.

B.

DURATION OF SAFETY SYSTEM TRAIN INOPERABILITY Not applicable -- No safety system was rendered inoperable.

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C.

SAFETY CONSEQUENCES AND IMPLICATIONS

This event is specifically bounded by the accident analysis of the partial loss of forced reactor coolant flow discussed in Section 15.3.1 of the CPSES Final Safety Analysis Report (FSAR). The partial loss of forced reactor coolant flow is classified as an ANS Condition II event, a fault of moderate frequency. In the July 9, 2003 event, the Auxiliary Feedwater System responded as expected and maintained the necessary Steam Generator heat transfer capability. There were no other malfunctions or equipment failures which complicated the plant response or otherwise elevated risk beyond the event analysis data. There were no safety system functional failures associated with this event. Based on this analysis, it was concluded that this event did not adversely affect the safe operation of CPSES Unit 2 or the health and safety of the public.

IV.

CAUSE OF THE EVENT

TXU Energy believes that the cause of the event was the opening of the 2-04 RCP motor breaker due to a "B" phase stator to ground short in the 2-04 RCP motor. The "B" phase stator to ground short occurred in the 2-04 RCP motor due to degradation of the stator ground wall insulation.

V.

CORRECTIVE ACTIONS

Corrective actions include repair of the 2-04 RCP motor stator and, as previously discussed in Licensee Event Report 03-002-00 for CPSES Unit 1, an evaluation of the Predictive Analysis Program specifically for large electric motors will be performed to assess the current program scope, monitoring practices, and overall effectiveness.

VL

PREVIOUS SIMILAR EVENTS

In 1996, CPSES Unit 2 experienced a reactor trip due to the loss of a Reactor Coolant Pump (see LER 446/96-007). However, the Reactor Coolant Pump loss during the 1996 event was due to the loss of the power supply, which was different than the July 9, 2003 event.

1. -
- NR BE 366 tl.-.1