05000260/LER-2005-003, Re Reactor Protection System Actuation from Scram Discharge Volume High Level While Shutdown

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Re Reactor Protection System Actuation from Scram Discharge Volume High Level While Shutdown
ML051610096
Person / Time
Site: Browns Ferry 
(DPR-052)
Issue date: 06/09/2005
From: Skaggs M
Tennessee Valley Authority
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LER 05-003-00
Download: ML051610096 (8)


LER-2005-003, Re Reactor Protection System Actuation from Scram Discharge Volume High Level While Shutdown
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
2602005003R00 - NRC Website

text

June 9, 2005 U.S. Nuclear Regulatory Commission 10 CFR 50.73 ATTN: Document Control Desk Mail Stop OWFN, P1-35 Washington, D. C. 20555-0001

Dear Sir:

TENNESSEE VALLEY AUTHORITY - BROWNS FERRY NUCLEAR PLANT (BFN) -

UNIT 2 - DOCKET 50-260 - FACILITY OPERATING LICENSE DPR LICENSEE EVENT REPORT (LER) 50-260/2005-003-00 The enclosed report provides details of an event which involved a valid initiation of the reactor protection system while shutdown. TVA is reporting this event pursuant to the requirements of 10 CFR 50.73(a)(2)(iv)(A).

There are no commitments contained in this letter.

Sincerely, Original Signed by:

Mike D. Skaggs cc: See page 2

U.S. Nuclear Regulatory Commission Page 2 June 9, 2005 Enclosure cc (Enclosure):

Ms. Eva Brown, Project Manager U.S. Nuclear Regulatory Commission (MS 08G9)

One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852-2739 Mr. Stephen J. Cahill, Branch Chief U.S. Nuclear Regulatory Commission Region II Sam Nunn Atlanta Federal Center 61 Forsyth Street, SW, Suite 23T85 Atlanta, Georgia 30303-8931 NRC Resident Inspector Browns Ferry Nuclear Plant 10833 Shaw Road Athens, Alabama 35611-6970

U.S. Nuclear Regulatory Commission Page 3 June 9, 2005 WDC:DTL:PSH:BAB Enclosure cc (Enclosure):

A. S. Bhatnagar, LP 6A-C J. C. Fornicola, LP 6A-C N. M. Moon, BR 4T-C R. F. Marks, PAB 1C-BFN R. G. Jones, NAB 1A-BFN K. L. Krueger, POB 2C-BFN J. R. Rupert, NAB 1A-BFN K. W. Singer, LP 6A-C M. D. Skaggs, POB 2C-BFN E. J. Vigluicci, ET 11A-K NSRB Support, LP 5M-C LEREvents@inpo.org EDMS WT CA - K S:lic/submit/lers/260-2005-03.doc

NRC FORM 366 (7-2001)

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (6-2004)

LICENSEE EVENT REPORT (LER)

(See reverse for required number of digits/characters for each block)

APPROVED BY OMB NO. 3150-0104 EXPIRES 06/30/2007

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

1. FACILITY NAME Browns Ferry Unit 2
2. DOCKET NUMBER 05000260
3. PAGE 1 OF 5
4. TITLE Reactor Protection System Actuation from Scram Discharge Volume High Level while Shutdown
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL NUMBER REV NO.

MONTH DAY YEAR FACILITY NAME none DOCKET NUMBER N/A 04 13 2005 2005-003-00 06 09 2005 FACILITY NAME none DOCKET NUMBER N/A

11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §:(Check all that apply)
9. OPERATING MODE 4

20.2201(b) 20.2203(a)(3)(i) 50.73(a)(2)(i)(C) 50.73(a)(2)(vii) 20.2201(d) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(A) 20.2203(a)(1) 20.2203(a)(4) 50.73(a)(2)(ii)(B) 50.73(a)(2)(viii)(B) 20.2203(a)(2)(i) 50.36(c)(1)(i)(A) 50.73(a)(2)(iii) 50.73(a)(2)(ix)(A) 20.2203(a)(2)(ii) 50.36(c)(1)(ii)(A)

X 50.73(a)(2)(iv)(A) 50.73(a)(2)(x) 20.2203(a)(2)(iii) 50.36(c)(2) 50.73(a)(2)(v)(A) 73.71(a)(4) 20.2203(a)(2)(iv) 50.46(a)(3)(ii) 50.73(a)(2)(v)(B) 73.71(a)(5) 20.2203(a)(2)(v) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(C)

OTHER

10. POWER LEVEL 0

20.2203(a)(2)(vi) 50.73(a)(2)(i)(B) 50.73(a)(2)(v)(D) specify in Abstract below or in (If more space is required, use additional copies of (If more space is required, use additional copies of (If more space is required, use additional copies of NRC Form 366A) (17) VII. ADDITIONAL INFORMATION A.

Failed Components None B.

Previous LERs on Similar Events None C.

Additional Information

Browns Ferry corrective action document PER 80721 D.

Safety System Functional Failure Consideration:

This event does not involve a safety system functional failure which would be reported in accordance with NEI 99-02. The RPS responded properly to the SDIV high level condition.

E.

Loss of Normal Heat Removal Consideration:

This event occurred with the reactor in Mode 4 (cold shutdown), and the main condenser was not in service, nor was it needed, at the time of this event.

VIII. COMMITMENTS

None