ML16161A818

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Insp Repts 50-269/87-13,50-270/87-13 & 50-287/87-13 on 870310-0511.No Violations or Deviations Noted.Major Areas Inspected:Cleaning & Testing of Reactor Bldg & DHR Coolers, Shutdown Work in Progress,Operations & Surveillance
ML16161A818
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 05/27/1987
From: Bryant J, Peebles T, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16161A820 List:
References
50-269-87-13, 50-270-87-13, 50-287-87-13, NUDOCS 8706020237
Download: ML16161A818 (12)


See also: IR 05000269/1987013

Text

SREG(

UNITED STATES

0

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos: 50-269/87-13, 50-270/87-13, and 50-287/87-13

Licensee:

Duke Power Company

422 South Church Street

Charlotte, N.C. 28242

Facility Name:

Oconee Nuclear Station

Docket Nos.:

50-269, 50-270, and 50-287

License Nos.:

DPR-38, OPR-47, and DPR-55

Inspection Conducted: March 10 -

May 11, 1987

I n s p e c t o r s :

.

r

An

e

L

Br-

Date Signed

.

Approved by:

A,/

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T.rPeebr/

Sectiog

leif

Date Signed

Dvision o Reactor rojects

SUMMARY

Scope:

This routine, unannounced inspection involved on-site resident

inspection in the areas of operations, surveillance, lineups, followup of events,

cleaning and testing of reactor building cooling units and decay heat removal

coolers, and shutdown work in progress. Additional areas examined during the

report period are described in Report No. 50-269,270,287/87-16.

Results: No violations or deviations were identified in the areas covered in

this report.

8706020237 870522

PDR

ADOCK 05000269

G

PDR

REPORT DETAILS

1.

Licensee Employees Contacted

  • M.S. Tuckman, Station Manager

T.B. Owen, Maintenance Superintendent

R.L. Sweigart, Operations Superintendent

J.M. Davis, Technical Services Superintendent

  • C.L. Harlin, Compliance Engineer
  • F.E. Owens, Assistant Engineer, Compliance

L.V. Wilkie, Superintendent of Integrated Scheduling

Other licensee employees

contacted

included technicians,

operators,

mechanics, security force members, and staff engineers.

Resident Inspectors:

  • J.C. Bryant

L.D. Wert

.

  • Attended exit interview.

2.

Exit Interview

The inspection scope and findings were summarized on May 12,

1987, with

those persons indicated in paragraph 1 above.

The licensee did not identify as proprietary any of the materials provided

to or reviewed by the inspectors during this inspection.

3.

Licensee Action on Previous Enforcement Matters

(Closed) Violation 50-269,270,287/86-33-02:

Inadequate Testing of ECCW

System.

This item was discussed in Report No. 87-10.

Corrective action

and response have been completed.

4.

Unresolved Items

No unresolved items were identified during this inspection.

5.

Plant Operations

The inspectors reviewed plant operations throughout the reporting period

to verify conformance with regulatory requirements, technical specifica

tions (TS),

and administrative controls.

Control

room logs,

shift

turnover records,

and equipment removal

and restoration records were

reviewed routinely.

Interviews were conducted with plant operations,

maintenance, chemistry, health physics and performance personnel.

2

Activities within the control rooms were monitored on an almost daily basis.

Inspections were conducted on day and on night shifts, during week days and on

weekends. Some inspections were made during shift change in order to evaluate

shift turnover performance.

Actions observed were conducted as required by

Operations Management Procedure 2-1.

The complement of licensed personnel

on each shift inspected met or exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were cognizant of plant conditions.

Plant tours were taken throughout the reporting period on a routine basis.

The areas toured included the following:

Turbine Building

Auxiliary Building

Units 1,2, and 3 Electrical Equipment Rooms

Units 1,2, and 3 Cable Spreading Rooms

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Unit 3 Containment Building

During

the plant tours,

ongoing activities, housekeeping,

security,

equipment status, and radiation control practices were observed.

Unit 1 ran at 88% power throughout the report period, limited by the

temporary main stepup transformer installed in early March.

Unit 2 began the report period at 96% power, as limited by steam generator

level, and continued at that level until March 26 when it tripped on RCS

high pressure as a result of a feedwater transient.

Reactor trips are

discussed in paragraph 8 of this report.

The unit was returned to 96%

power on March 28 and continued at that power until April 7, when power

was reduced due to degraded heat transfer in reactor building cooling

units (RBCU's)

and decay heat removal

(DHR)

coolers

(See paragraph 12).

The reactor was returned to 88% power (as limited by high steam generator

level) on April 12,

where it

remained until April 20, when it tripped on

high steam generator level. Unit 2 reached 88% power again on April 21,

and continued at that power until the end of the report period.

Unit 3 began the report period in refueling shutdown. The unit was placed

on line at 15-20% power on March 31, for a brief period to test the main

generator which had been rebuilt during the refueling shutdown.

The

reactor was then taken to hot shutdown for testing of RBCU's

and DHR

coolers (Paragraph 12) and then to cold shutdown to repair a leak on the

RVLIS system. Subsequent to repairs, as Unit 3 was being heated for RBCU

testing and startup, procedures were violated concerning the HPI system

and RBCU's. Theses events are discussed in detail in Report No.

50-269,

270,287/87-16, and will not be discussed in this report. After startup on

April 14, the unit was taken off line on April 15, to replace a bad phase

pot fuse and to balance turbine bearings,

then reached 60% power on

3

April 16 and 100% power on the 17th.

The unit was taken off line on

April 23,

to repair a steam generator tube leak and was again taken

critical on May 2 (Paragraph 13). Unit 3 operated at 100% power for the

remainder of the report period.

No violations or deviations were identified.

6.

Surveillance Testing

The surveillance tests listed below were reviewed by the inspector to

verify procedural and performance adequacy.

The completed tests reviewed were

examined for necessary test pre

requisites,

instructions,

acceptance

criteria,

technical

content,

authorization to begin work, data collection, independent verification

where required, handling of deficiencies noted, and review of completed

work.

The tests witnessed, in whole or in part, were inspected to determine that

approved procedures

were

available,

test equipment was

calibrated,

prerequisites were met, tests were conducted according to procedure, test

results were acceptable and systems restoration was completed.

Surveillances witnessed in whole or in part:.

PT/0/A/0150/08A RB Personnel Lock Leak Rate Test

MP/0/A/1705/27

Fire Protection, Repair of Electrical Penetration

IP/1/A/305/3

Reactor Protection System, Channel D Calibration

and Functional Test.

IP/0/A/360/2

3R1A-54 Turbine Building Sump Radiation Monitor

Calibration

Completed surveillance reviewed:

W/R 05900C Unit 1 TDEFWP Bearing Oil Cooling Pump

No violations or deviations were identified.

7.

Maintenance Activities

Maintenance activities were observed throughout the report period but were

limited to spot checks of maintenane personnel, appropriate procedures and

work performance.

Some of the activities observed were rework of Unit 3

main feedwater valves, rework of Limitorque operators, auxiliary boiler

inspection, repair of a fireproof penetration, rework of RCW "B" Pump.

  • k

No violations or deviations were identified.

4

8.

Unit 2 Trips

On March 26,

1987, at 11:33 p.m.,

Unit 2 tripped from 96% power on high

reactor coolant system (RCS)

pressure.

Cause of the event appeared to

be an intermittent, poor connection in the Integrated Control System (ICS)

BTU limit circuitry. The specific portion of the ICS affected was the

steam generator feedwater control. As a result of the electrical failure,

feedwater (FDW) demand went to near zero on "A" steam generator (SG).

The

ICS responded by reducing flow to "A" SG,

resulting in increased RCS

temperature and pressure and the reactor trip.

Circuitry repairs were

made and the reactor started up and placed on line at 12:00 noon on

March 28.

On April 20,

1987,

at 5:33 a.m., Unit 2 tripped from 86% power when FDW

demand on the A loop went low.

The ICS responded by decreasing flow to

"A" SG and increasing flow to "B" SG. Since "B" SG level was already at

about 89%,

the level quickly reached 96%,

tripping FDW pumps and the

turbine. The reactor then tripped on the turbine anticipatory trip.

Investigation revealed that a failed multiplier module in the BTU limit

circuitry had caused the problem.

The module was replaced and the unit

taken critical at 5:15 p.m. on April 20.

There have been other trips in the past caused by failures in the BTU

limit circuitry.

The primary purpose of the BTU limit circuitry, as

stated by the licensee, is to maintain steam. quality for protection of the

turbine at low power levels.

Unit 3 was shut down at the time of the

Unit 2 trip, and prior to startup of Unit 3 a modification was installed

which will remove the BTU limit circuitry signal at power levels above

25%. This modification later was installed on Unit 2 with the unit on

line, and it will be installed on Unit 1 while it is on line.

No violations or deviations were identified.

9.

Unusual Events Due to Non-isolable Leaks, Units 2 and 3

An Unusual Event was declared at 3:31 p.m. on March 31, when an unisolable

leak of less than 1 gpm was discovered in the Unit 3 reactor coolant

system (RCS)

at a pipe to coupling weld in the RVLIS system.

At the

time, Unit 3 was at hot shutdown.

The RCS was reduced to cold shutdown

conditions under the assumption that the reactor would have to be defueled

and drained to repair the leak.

The Unusual Event was terminated when

the RCS reached cold shutdown conditions.

At this point the licensee

determined that the leak, which had been reduced to weeping,

could be

repaired "wet" by stick welding the leak closed then making a TIG overlay

on the pipe.

The weld procedures to be used were discussed with the resident inspector

and then, by telephone, with welding engineers in Region II. The pipe was

then successfully repaired and stiffeners added to the pipe to prevent

recurrence.

5

On April 8, 1987, a leak of 0.3 gpm at an almost identical location was

discovered on Unit 2 while the RCS was at 240 degrees F and 185 psig. An

Unusual

Event was declared.

The same repair methods were used as on

Unit 3 and the cause was the same. Therefore, causes of the event will be

discussed as one.

An entry was made into Unit 1 containment with the

reactor at power to search for similar leaks, but none were found.

The

RVLIS

instrumentation lines were attached as follows.

The low

pressure injection (LPI)

pump suction drop lines from the

RPS are

2500 psig lines.

A half couplant was welded to the drop lines and a 3/4"

schedule 160 pipe was socket welded into the half couplant.

At the end

of the 3/4" pipe was an isolation valve where the piping was reduced to

instrument tubing to a supported level transmitter. The leaks were in the

heat affected zone of the socket weld.

The crack on Unit 3 propagated

circumferentially about 180 degrees around the pipe.

The RVLIS modification was made on Unit 1 (which had no failure), during

a refueling outage which began February 13, 1986. The pipe drawings used

for fabrication of the pipe showed full pipe diameters.

It showed the

isolation valve at the end of the 3/4" pipe 12 inches from the centerline

of the 12"

LPI drop line.

The modification for Unit 1 was fabricated in

that manner.

In early 1986,

Duke Design Engineering changed the type drawings to one

line computerized isometrics showing only the centerline on the drawings.

Reportedly,

no training concerning this change was given to personnel

associated with implementation of modifications at Oconee.

Consequently,

the piping for Units 2 and 3 was fabricated with the isolation valve 12",

from the 12" pipe wall rather than from the centerline. Proper installa

tion would have resulted in the valve being 6" from the pipe wall.

The QA

inspectors also misread the drawings.

The prefabricated piping was

welded

into the Unit 2 LPI line on

September 11,

1986,

and Unit 2 was in operation from October 15,

1986,

until the failure was detected on April 8, 1987.

The piping was welded

into the Unit 3 LPI line on January 27,

1987, during refueling outage.

The

weld

was visually inspected by Maintenance,

during heatup,

on

March 28, 1987. Total unit operation under nuclear heat, at a maxim power

level of 20%, was only about one day.

Duke

Power Company investigators determined that failure was due to

weakening of the pipe wall by stress induced by natural frequency vibra

tion. This was caused by the extra length of pipe putting.the pipe

section outside the seismic stress design basis.

It

appears that work and inspection were done correctly except for the

lack of understanding of the new drawing system.

This appears to be

another example of inadequate communication between Design Emgineering and

plant personnel. Currently, there is a violation open on the same subject

6

in the same time frame as described in Report No.

50-269,270,287/86-16.

That violation concerned inadequate communication concerning installation

of Keowee batteries.

The matter of communications concerning drawing

changes will be considered as another example of the referenced violation.

10.

Resident Inspector Safeguards Inspection

In the course of the monthly activities, the Resident Inspectors included

a review of the licensee's physical security program. The performance of

various shifts of the security force was observed in the conduct of daily

activities which included: protected and vital area access controls,

searching of personnel, packages

and vehicles,

badge issuance

and

retrieval, escorting of visitors, patrols and compensatory posts.

In

addition, the

Resident Inspectors observed protected area lighting,

protected and vital area barrier integrity and verified interface between

the security organization and operations and maintenance.

The Resident

Inspectors also witnessed spent fuel shipment and visited central

and

secondary alarm stations.

11.

Information Notice 87-19: Perforation and Cracking of Rod Cluster Control

Assemblies

The referenced notice concerns perforation and cracking of Westinghouse

control rod assemblies. Since Westinghouse assemblies in which problems

were detected are about the same age as those at Oconee, the inspectors

made inquiries and reviewed documentation to determine control

rod

assembly conditions at Oconee.

Control

rod assemblies at Oconee are inspected periodically during

refueling outages and a schedule of routine partial replacement of

assemblies is in place which will replace all rods over a 10 -

12 year

interval.

Due primarily to significant differences in construction,

Babcock and Wilcox assemblies do not appear to be subject to the fretting

and wear of the Westinghouse assemblies.

The major factors in this case

are the long "C" and "Split" guide tubes of the B&W assemblies which guide

the rod fingers when withdrawn. The Westinghouse assemblies do not use

such long rod guides. The problems of wear and fretting of rods due to

flow-induced vibration have not been observed at Oconee.

12.

Reduced Efficiency of Reactor Building Cooling Units and Decay Heat

Removal Coolers

During the report period,

the licensee determined that heat transfer

capability of reactor building cooling units (RBCUs)

and decay heat

removal

(DHR)

coolers had fallen below design requirements.

For power

operation, Technical Specifications (TS) require two independent trains of

low pressure injection, including the DHR coolers, be completely operable

and that three independent trains of reactor building cooling, including

the RBCU's,

be completely operable.

The above requirements allow some

relief for maintenance.

7

Extensive cleaning and testing was carried out by the licensee and a

Confirmatory Order was issued by

NRC.

A Region

II

inspection team

examined data and history to determine if

the licensee had knowingly

operated outside of requirements. The team findings and a description of

events,

and data, will be provided in Report No.

50-269,270,287/87-17;

therefore,

the resident inspectors'

report will deal primarily with

operational aspects during the report period.

The first indication of reduced heat transfer capacity of DHR coolers was

observed in 1985 when the licensee noted that a Unit 1 cooler seemed to

take longer than usual to cool down the RCS. During 1986 the licensee had

considerable communication with the RBCU vendor in an attempt to evaluate

test data. Some RBCU and DHR cooler cleaning was performed and the method

of evaluation available indicated that performance was satisfactory.

A

section of report no. 50-269,270,287/86-20 discusses an inspection of

bio-fouling and states that no significant degradation had occurred due to

the cleanliness of Lake Keowee water, which is used in the low pressure

service water (LPSW) system (the cooling water supply to the coolers). It

also discusses the licensee's method of determining flow degradation.

In 1986, the licensee continued cleaning and testing of coolers and issued

a contract to a consultant to develop state of the art formulas for

determining heat transfer under plant conditions.

The computer program

was received from the consultant on March 30,

1987..

On March 31,

Duke

Power Company (DPC)

notified NRC that full power operations could not be

supported for Unit 3, which was in refueling shutdown at the time, due to

inadequate decay heat removal capability.

After completion of operability evaluations for Units 1 and 2, on April 1,

DPC notified NRC that full power operation could not be supported for

Units 1 and 2.

The licensee determined that heat removal capabilities

would permit operation of Unit 1 at power levels below 91 %. Unit 1 was

then operating at 88% power as limited by the main stepup transformer in

use.

DPC also determined that Unit 2 operation below 66% power was

acceptable. At the time, Unit 2 was operating at 97%; power was then

reduced to 60%.

On April 6 DPC issued a request to NRC for an amendment to the operating

license permitting continued operations with reduced maximum power trip

set points.

The request specified increasing

LPSW flow through

DHR

coolers from

3000 gpm to 5000 gpm during certain accident conditions

to assure adequate cooling.

NRC responded with a letter on April 7

acknowledging the verbal

temporary waiver of compliance extended on

April 3. The temporary waiver was later extended until 5:00 p.m.

on

April 10.

On April 10,

the

NRC

issued a Confirmatory Order placing

restrictions of operation on all three units until all RBCU's and DHR

coolers had been verified to meet design requirements.

8

As described in Report 87-17, all three units underwent cleaning, and in

the cases of Units 2 and 3, all coolers were tested. Unit 2 was shut down

for cleaning and testing. Unit 3 coolers were cleaned during shutdown,

then the unit was shut down again for additional cleaning and testing.

Unit 1, which had already been tested, had one DHR cooler cleaned but not

tested while the reactor was on line.

The Confirmatory Order of April 10

dealt with those coolers which had not yet passed inspection for full

power operation at the time of the order.

In brief, the order placed the following conditions for operation of the

separate units.

Unit 1:

Until the 1A LPI (0HR) cooler is cleaned, tested, evaluated

and approved for full power operation, the maximum power shall be

91.5% of rated power with the high flux trip point set at that power,

and the remaining non-ES LPI pump shall be operable.

Also Oconee 1

shall not operate at any power level following the cycle 10 refueling

outage unless the Regional Administrator, Region II, has approved the

1A LPI cooler for full power operation.

Unit 2:

Until the 2A LPI cooler is cleaned, tested, evaluated and

approved for full power operation by the Regional Administrator,

Region II,

the maximum power level shall be 81.7% rated power with

the high flux trip point set at that level.

Should lake cooling

water rise above 550 F the unit shall be shut down. The remaining

non-ES LPI pump shall be operable.

Unit 3:

Oconee Unit 3 shall not operate at any power level after

midnight of April 22,

1987,

unless the

Regional

Administrator,

Region II, has approved full power operation.

On April 13,

1987,

and until the end of the report period, the status of

the Oconee units was as follows:

Unit 1:

As verified by NRC inspectors, Unit I is operating under the

above restrictions. (The unit is currently limited to approximately

88% power by the temporary main step-up transformer in use.)

The

Confirmatory Order conditions remain in effect.

Unit 2:

On April

11,

NRC inspectors reviewed test results and

analyses on Unit 2 LPI coolers and reactor building cooling units

and found that they met conditions of the Confirmatory Order.

The

required approval for power ascension to 100% was given by Region II

to the station manager at 11:00 a.m.

on April

11.

(Unit 2 is

currently limited to 88% power due to high steam generator levels.)

Unit 3:

Unit 3 LPI coolers and reactor building cooling units were

cleaned and tested. Test results and analyses were reviewed by NRC

inspectors on April 12, and found to satisfy the requirements of the

9

order.

The required approval for startup was given by Region II to

the station manager at 2:00 p.m. on April 12.

The resident inspectors will continue followup of any developments

concerning the cooling units.

13.

Unit Three Steam Generator Tube Leak

Unit Three was shut down on April 23,

to repair a primary to secondary

leak in the A steam generator. The leak was approximately 0.1 gallons per

minute. A total of eight steam generator tubes were plugged and the unit

was returned to service on May 2, 1987.

No violations or deviations were identified.

14.

Inadequate Overpressure Protection for Auxiliary Steam Header

During followup reviews of the Safety System Functional Inspection (SSFI)

concerns on undersized relief valves, the licensee discovered a potential

failure of the Turbine Driven Emergency Feedwater Pump due to possible

overpressurization of the Auxiliary Steam System.

This was reported to

the NRC operations duty officer on February 27,

1987.

Analysis of safety

valves on steam lines to the Emergency Feedwater Pump Turbine revealed

that if control valves MS-126 (6 in. steam to auxiliary steam) and MS-129

(2 in. main steam to auxiliary steam) fail open, overpressurization of the

auxiliary steam system and the Emergency

Feedwater Pump Turbine could

occur. The potential overpressure situation is due to the undersizing of

the auxiliary steam header safety valves (AS-23) and is the subject of LER 269/87-03 of March 30, 1987.

LER 269/87-03 detailed corrective action steps taken as an interim measure

until permanent corrective actions were completed. These actions included

installation of travel stops on each unit's MS-126 to limit valve stroke,

and administrative control of bypass and control valves.

These adminis

trative controls are to ensure that:

Only one unit is supplying the

auxiliary steam header at a given time (other 2 units MS-126 and MS-129

shut); auxiliary steam header section block valves between units are open

(ensures a total of 3 sets of 2 relief valves are available); and the

manual bypass valves around MS-126 for each unit (MS-131) are shut. These

actions will maintain system pressure within applicable code limits and

allow sufficient auxiliary steam flow for unit startup.

During the incorporation of these interim measures,

an error caused the

auxiliary steam header to be supplied from Unit I before travel stops

were installed on that unit's MS-126.

A scaffold had been installed at

1 MS-126 so that the modification could be performed.

Through an error,

maintenance removed the scaffold without having performed the work,

and

operations was informed, erroneously, that the job was complete.

Unit 1

10

then supplied the auxiliary header from March 23 to April 21, with some of

the administrative controls relaxed due to the misunderstanding.

On

April 21 the situation was corrected by shifting the auxiliary steam

header back to being supplied from Unit 2 which

had travel

stops

installed. Travel stops were then promptly installed on Unit 1 MS-126,

completing all the interim corrective actions.

Administrative control of

the associated steam valves has been closely followed by the resident

inspectors.

Operation with Unit 1 supplying auxiliary steam without travel stops

installed and with some of the administrative controls relaxed was a

violation of a commitment to NRC.

However, the licensee identified the

error during a routine surveillance, took immediate corrective action,

and the situation appears to meet all requirements of 10 CFR Part 2,

Appendix C; therefore the event will not be cited as a deviation.

15.

Inspection of Open Items

The following open items are being closed based on inspection and/or

record review and discussions with licensee personnel as appropriate.

(Closed)

LER

50-269/86-09;

Keowee Battery Racks Outside of Design

Specifications.

The immediate problem was corrected within hours of

discovery. Satisfactory corrective actions have been taken to correct the

underlying cause,

communications

between

Design Engineering

and site

personnel.

(Closed)

UNR 50-269,270,287/86-20-03; Discrepancy in Document/Design

Control.

Same as LER 86-09 above.

(Closed)

LER 50-269/86-11;

Inoperability of Emergency Condenser

Circulating Water System. This problem was discussed in Reports 86-26 and

86-33. Resolution was satisfactory.

(Closed)

LER

50-269/86-14;

TS 4.16 Violation-Source Leak Test Not

Performed. Corrective action has been reviewed and found acceptable.

(Closed)

LER

50-270/86-03;

Core Flood Tank Concentration Below T.S.

Limit.

Problem and corrective action were reviewed and found satis

factory.

(Closed)

IFI 50-270/86-26-01; Revisions to the Keowee Load Shed Surveil

lance Test. Test revisions were reviewed and found satisfactory.

(Closed) IFI 50-270/86-26-02; LPSW Valves to Decay Heat Coolers Did Not

Appear to Respond Correctly.

Repeated tests have not revealed a

discrepancy.

(Closed)

LER 50-287/86-01; Reactor Trip From High Reactor Coolant System

Pressure. Failure of Al Feedwater Transmitter.

Defective module was

identified and replaced.

(Closed) LER 50-287/86-03; Turbine Building Sump Radiation Monitor Found

in Bypass Due to a Defective Procedure.

Corrective action was reviewed

and appears satisfactory.

(Closed) IFI 50-287/85-07-02;

Improve Valve LP-2 Operability.

Valve

operator has been rebuilt and MOVATS tested.

(Closed) Part 21 50-269,270,287/P2184-01; HVAC Equipment Mfg. by Bahnson.

In response to IE Information Notice 84-30 the licensee inspected welds in

the Bahnson supplied air handling unit in the standby shutdown facility

and performed an as-built weld stress calculation. Thirty-eight defective

welds were identified, but were eventually determined to be cosmetic in

nature. No repairs were required.