:on 970909,loss of Fire Protection Water to Auxiliary Bldgs & Containment Was Noted.Caused by Human Error Due to Inattention to Detail.Loss Prevention Tours Have Been Revised to Include Once Per Shift Verification| ML18106A187 |
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| Site: |
Salem  |
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| Issue date: |
11/14/1997 |
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| From: |
Enrique Villar Public Service Enterprise Group |
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| To: |
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| Shared Package |
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| ML18106A186 |
List: |
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| References |
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| LER-97-016-01, LER-97-16-1, NUDOCS 9712090139 |
| Download: ML18106A187 (5) |
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Similar Documents at Salem |
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text
NRCFORM366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (4-95)
EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.
Ll9ENS~E EVENT REPORT (LER)
REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (T~ F33J U.S. NUCLEAR (See reverse for required number of REGULATORY COMMISSIOJ!n WASHINGTON, DC 20 !;s:Ooo1i': AND TO THE PAPERWORK REDU ON PROJECT ~3150-0104), 0 FICE OF digits/characters for each block)
MANAGEMENT AND BUDGET, WASHINGTON, C 20503.
FACILITY NAME (1)
DOCKET NUMBER (2)
PAGE(3)
SALEM GENERATING STATION UNIT 2 05000311 1 OF 5 TITl.E (4)
LOSS OF FIRE PROTECTION WATER TO THE SALEM UNIT 1 AND 2 AUXILIARY BUILDINGS AND CONTAINMENTS.
EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
FACILITY NAME DOCKET NUMBER MONTH DAY YEAR SEQUENTIAL MONTH DAY YEAR YEAR I NUMBER I REVISION NUMBER STATION UNIT 1 05000272 09 09 97 97 016 00 11 14 97 FACILITY NAME DOCKET NUMBER 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11)
MODE(9) 20.2201(b) 20.2203(a)(2)(v)
- 50. 73(a)(2)(1)
- 50. 73(a)(2)(vlll)
POWER 20.2203(a)(1) 20.2203(a)(3)(1)
- 50. 73(a)(2)(11)
- 50. 73(a)(2)(x)
LEVEL(10) 20.2203(a)(2)(1) 20.2203(a)(3)(11)
- 50. 73(a)(2)(111) 73.71 20.2203(a)(2)(11) 20.2203(a)(4)
- 50. 73(a)(2)(1v) x OTHER 20.2203(a)(2)(111) 50.36(c)(1)
- 50. 73(a)(2)(v)
Spec~ln Abstract below or In C Form 366A 20.2203(a)(2)(1v) 50.36(c)(2)
- 50. 73(a)(2)(vll)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (Include A,.* Code)
E. H. Villar (Station Licensing Englnner) 6093395456 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS TONPRDS SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH DAY YEAR IYES x1NO SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE).
DATE(15)
ABSTRACT (Umlt to 1400 spaces, I.e., approximately 15 single-spaced typewritten lines) (16)
At 2210 hrs on September 16, 1997, a Unit 1 Nuclear Control Operator (NCO) identified that the fire protection water for Salem Units 1 and 2 Auxiliary Buildings and Containment was isolated.
Fire protection water for these areas is supplied via valves 1FP186 and 1FP187, which were found closed.
While the exact cause of the valves being mispositoned could not be determined, the valves were most probably misaligned during relamping activities on September 9, 1997. The cause of the condition going unidentified is attributed to human error due to inattention to detail by the NCO and the Loss Prevention Operators during subsequent panel reviews.
Fire protection personnel were promptly notified, and the valves were opened at 2237 hrs.
Pursuant to License Conditions 2.C.(10) and 2.I of the Unit 2 Facility Operating License, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> report and a follow-up Special Report were made to the NRC on September 17 and September 30, 1997, respectively.
This Special Report is being Specification Section Report.
97120 90139 971114 ADOCK 05000311 PDR PDR s
6
- 3 I made* in accordance with Technical and supplements the September 30 Special
J (4-95)
FACILITY NAME (1)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
SALEM GENERATING STATION UNIT 2 05000311 YEAR I SE,fill,feT,tL I ~
2 OF 5
97 -
016 00 TEXT (If more space Is required, use additional copies of NRC Fonn 366A) (17)
PLANT IDENTIFICATION:
Salem Generating Station - Unit 2 Public Service Electric and.Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCQRRENCE:
Loss of Fire Protection Water to Salem Units 1 and 2 Auxiliary Buildings and Containments.
Date of Occurrence:
Date of Identification Report Date:
September 9, 1997 September 16, 1997 November 14, 1997 CQNDITIONS PRIOR TO OCCQRRENCE:
Salem Unit 1 - Defueled Salem Unit 2 -
Mode 1 approximately 58% Power DESCRIPTION OF OCCQRRENCE:
The following is a timeline of the events, as recreated from operators logs, interviews, and a brief summary of the event recreation, as well as a level one root cause investigation Time line July 15, 1997 - Valves 1FP186 and 1FP187 were stroked open and closed using surveillance procedure SC.FP-ST.FS-0007.
September 1, 1997-Valves 1FP186 and 1FP187 were locally position verified open by Loss Prevention personnel.
September 2, 1997 -
1FP147 was stroked open and closed during performance of procedure Sl.RA-IS.ZZ-0001, "Types B And C Leak Rate Test."
The controls for 1FP147 are located on panel 1RP5, immediately to the right of the control for 1FP186 and 1FP187. (4-95)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2) 05000311 SALEM GENERATING STATION UNIT 2 TEXT (If more space Is required, use addltlonail copies Of NRC Form 366A) (17)
DESCRIPTION OF OCCURRENCE (cont'd):
LER NUMBER 6)
YEAR I SEQUENTIAL NUMBER REVISION NUMBER 97 -
016 00 PAGE(3) 3 OF 5
September 6, 1997 -
I&C Craft personnel started relamping activities at panel lRPS per Work Order.
September 9, 1997 -
I&C Craft personnel completed relamping lRPS. Work Order notations and personnel interviews indicate that valves 1FP186 and 1FP187 were relamped on the second night the panel was worked on. This work was performed from 2100 hrs on September 8 to 0700 hrs on September 9, 1997.
September 16, 1997 - At 2210 hrs a Unit 1 NCO noted that the indicator for valves 1FP186 and 1FP187 was illuminated, and at 2225, the valves were field verified closed by Loss Prevention personnel.
At 2237, Operations personnel opened the valves, and at 2243, the valves were field verified open by Loss Prevention personnel.
Pursuant to License Conditions 2.C. (10) and 2.I of the Unit 2 Facility Operating License, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> report and a follow-up Special Report were made to the NRC on September 17 and September 30, 1997, respectively.
This Special Report is being made in accordance with Technical Specification Section 6.9.3, and supplements the September 30, Special Report.
CAUSE OF OCCURRENCE:
The exact cause of how the 1FP186 and 1FP187 valves were closed, and could have potentially been closed from September 1, 1997, through September 16, 1997, could not be determined.
These dates represent the times when the 1FP186 and 1FP187 valves were field verified open by Loss Prevention personnel.
However from the timeline of the events, as presented above, the most probable cause for the inadvertent closure of the 1FP186 and 1FP187 valves was relamping activities on lRPS panel on September 9, 1997. (4-95)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2) 05000311 SALEM GENERATING STATION UNIT 2 TEXT (If more space la required, use additional copies of NRC Fonn 366A) (17)
CAUSE OF OCCURRENCE (cont'd):
LER NUMBER 6)
YEAR I SEQUENTIAL NUMBER 97 -
016 00 PAGE(3) 4 OF 5
The cause for this condition going unidentified for the period from September 9, 1997, through September 16, 1997 is attributed to human error due to inattention to detail by the Nuclear Control Operators and the Loss
- - Prevention Operators during subsequent panel reviews.
The reviews did not focus on valve position indication, but were focused on verification of alarm status and lamp functionality.
PRIOR SIMILAR OCCURRENCES:
A search of the LER database using the phrase "fire protection" did not identify any LERs within the past five years related to mispositioned fire protection valves.
Similar searches were performed using the same phrases as described above for the corrective action program database searches, and no applicable documents were identified.
SAFETY CONSEQUENCES AND IMPLICATIONS
Although fire suppression was potentially unavailable during the period from September 1 (when the valves were field verified opened) to September 16 (when the valves were again field verified opened), there were hourly roving fire watch tours of the Unit 1 and 2 Auxiliary Buildings.
These roving fire watch tours were established for other unrelated fire protection issues, but they did provide a level of assurance that a fire would not have gone undetected.
PSE&G has an onsite dedicated Fire Protection Department.
Additionally, the fire protection detection system for the Auxiliary Buildings and Containments was unaffected by the closure of the 1FP186 and 1FP187 valves, which provides the primary means of detection.
CORRECTIVE ACTIONS TAKEN:
The valves were opened at 2237 hrs on September 16, 1997, and locally verified open by Loss Prevention personnel at 2243 hrs.
- LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION.
FACILITY NAME (1)
SALEM GENERATING STATION UNIT 2 U.S. NUCLEAR REGULATORY COMMISSION DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3) 05000311 YEAR I 8F;fil'=AL I== 5 OF 5
97 -
016 00 TEXT (If more apace rs required, use addltlonal copies of NRC Fonn 366A) (17)
CORRECTIVE ACTIONS TAICEN (cont'd):
On September 18, 1997, Loss Prevention personnel completed a lineup verification of Fire Protection valves (C02 and Water) at Salem station, and as a temporary compensatory measure, initiated position verification of the 1FP186 and 1FP187 valves on a twice per shift (every 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />) basis pending completion of the cause investigation.
The monthly verification of Hope Creek valves was performed the week prior so no further action was initiated for Hope Creek.
Loss Prevention tours have been revised to include a once per shift verification of valve position for 1FP186 and 1FP187.
This measure will remain in place until the lRPS panel status report checklist is revised to include verification of 1FP186 and 1FP187 indicator lamp test once per shift.
Operators will receive training on the controls associated with the 1FP186 and 1FP187 valves. This training will be completed by November 30, 1997.
An event notice will be issued to Operations, Work Control, Loss Prevention and Station Planning to share the lessons learned from this event.
This notice will be issued by October 31, 1997.
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| 05000272/LER-1997-001, :on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With |
- on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1997-001-01, :on 970115,inadequate Surveillance for PORV Accumulator Discharge Check Valves Was Noted.Caused by Reviewers Not Identifying That Test Method Did Not Meet Requirements of ASME Code.Revised Procedure |
- on 970115,inadequate Surveillance for PORV Accumulator Discharge Check Valves Was Noted.Caused by Reviewers Not Identifying That Test Method Did Not Meet Requirements of ASME Code.Revised Procedure
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000272/LER-1997-001-02, :on 970117,discovered Inadequate IST Surveillance of B Injection Inlet Valves.Caused by Inadequate Communication Between EOP & Ist.Reviewed Salem EOPs for Similar Problems |
- on 970117,discovered Inadequate IST Surveillance of B Injection Inlet Valves.Caused by Inadequate Communication Between EOP & Ist.Reviewed Salem EOPs for Similar Problems
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1997-002-01, :on 970210,chilled Water Sys Single Failure Vulnerabilities Identified.Caused by Design Deficiency. License Change Request S97-05 Submitted |
- on 970210,chilled Water Sys Single Failure Vulnerabilities Identified.Caused by Design Deficiency. License Change Request S97-05 Submitted
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000311/LER-1997-002-02, :on 970213,discovered non-seismically Qualified Pressure Switches in Auxiliary Bldg Ventilation.Caused by Pressure Switches Being Replaced w/non-qualified Pressure switches.Re-installed Qualified Switches |
- on 970213,discovered non-seismically Qualified Pressure Switches in Auxiliary Bldg Ventilation.Caused by Pressure Switches Being Replaced w/non-qualified Pressure switches.Re-installed Qualified Switches
| 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000272/LER-1997-003-01, :on 970131,new Alignment Assumes Single Failure of 125 Volt Dc Channel Resulted in Two SWS Pumps in Runout Condition Which Caused Insufficient SWS Flow Rates.Modified SW223 Valves for Five Unit 2 Cfcus |
- on 970131,new Alignment Assumes Single Failure of 125 Volt Dc Channel Resulted in Two SWS Pumps in Runout Condition Which Caused Insufficient SWS Flow Rates.Modified SW223 Valves for Five Unit 2 Cfcus
| | | 05000311/LER-1997-003-02, :on 970319,excessive Debris in Unit Two Containment Was Caused by Poor Enforcement & Lack of Mgt Expectations Over Life of Plant,Coupled W/Poor Worker Practices.Debris Removed |
- on 970319,excessive Debris in Unit Two Containment Was Caused by Poor Enforcement & Lack of Mgt Expectations Over Life of Plant,Coupled W/Poor Worker Practices.Debris Removed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000311/LER-1997-003-03, :on 970909,loss of Fire Protection Water to Auxiliary Bldgs & Containments Was Noted.Caused by Human Error Due to Inattention to Detail.Loss Prevention Tours Have Been Revised |
- on 970909,loss of Fire Protection Water to Auxiliary Bldgs & Containments Was Noted.Caused by Human Error Due to Inattention to Detail.Loss Prevention Tours Have Been Revised
| | | 05000311/LER-1997-004-02, :on 970408,failed to Comply W/Ts Action Statement,Dg Start & Inadequate Surveillance Testing Due to Inadequate Tracking of Inoperable Equipment by Shift Personnel.Procedures Were Revised |
- on 970408,failed to Comply W/Ts Action Statement,Dg Start & Inadequate Surveillance Testing Due to Inadequate Tracking of Inoperable Equipment by Shift Personnel.Procedures Were Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000311/LER-1997-004, :on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With |
- on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000272/LER-1997-004-01, :on 970221,inadequate Surveillance Testing of Molded Case Circuit Breakers Were Identified.Caused by Instantaneous Function Not Accurately Specified in Procedure.Tssip Has Been Initiated |
- on 970221,inadequate Surveillance Testing of Molded Case Circuit Breakers Were Identified.Caused by Instantaneous Function Not Accurately Specified in Procedure.Tssip Has Been Initiated
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) | | 05000272/LER-1997-005-02, :on 970625,radioactive Liquid Effluent Samples Were Not Analyzed within Required Surveillance Interval. Caused by Incorrect Interpretation of TS Sr.Training Will Be Provided to Chemistry Supervisors |
- on 970625,radioactive Liquid Effluent Samples Were Not Analyzed within Required Surveillance Interval. Caused by Incorrect Interpretation of TS Sr.Training Will Be Provided to Chemistry Supervisors
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1997-005-01, :on 970430,discovered Violation in Pressurizer Overpressure Protection Sys Ts.Caused by Inadequate Procedural Guidance.Revised Procedures for 115 Volt Vital Instrument Bus & 125 Vdc Bus Operations |
- on 970430,discovered Violation in Pressurizer Overpressure Protection Sys Ts.Caused by Inadequate Procedural Guidance.Revised Procedures for 115 Volt Vital Instrument Bus & 125 Vdc Bus Operations
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000272/LER-1997-006, :on 970312,determined Relays That Are Part of Logic for Opening PORVs Were Not Tested.Caused by Lack of Adequate Control for Maint of TS Surveillance Procedures. Initiated New Procedures & Revised Procedures |
- on 970312,determined Relays That Are Part of Logic for Opening PORVs Were Not Tested.Caused by Lack of Adequate Control for Maint of TS Surveillance Procedures. Initiated New Procedures & Revised Procedures
| 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) | | 05000311/LER-1997-006-02, :on 970404,seismic Adequacy of Svc Water Header Was Invalidated Due to Unclear Work Instructions.Piping Has Been Reinstalled Correctly |
- on 970404,seismic Adequacy of Svc Water Header Was Invalidated Due to Unclear Work Instructions.Piping Has Been Reinstalled Correctly
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000272/LER-1997-007-02, :on 970630,failure to Perform Independent Verification for Radioactive Release Lineup as Required by TS 3.3.3.8,noted.Caused by Personnel Error.Cr Supervisor Was Held Accountable for Actions |
- on 970630,failure to Perform Independent Verification for Radioactive Release Lineup as Required by TS 3.3.3.8,noted.Caused by Personnel Error.Cr Supervisor Was Held Accountable for Actions
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1997-007-01, :on 970623,TS 4.0.5 ISI Requirement to Perform Radiography of Check Valves 2CC195 & 2CC210 Every 92 Days Determined to Have Been Missed.Caused by Personnel Error. Check Valves Subsequently Tested |
- on 970623,TS 4.0.5 ISI Requirement to Perform Radiography of Check Valves 2CC195 & 2CC210 Every 92 Days Determined to Have Been Missed.Caused by Personnel Error. Check Valves Subsequently Tested
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1997-008, :on 970321,inadequate Surveillance Testing of PORV Accumulators & Check Valves Was Attributed to Lack of Adequate Controls for Development & Maintenance of TS Surveillance Procedures.New Procedure Made |
- on 970321,inadequate Surveillance Testing of PORV Accumulators & Check Valves Was Attributed to Lack of Adequate Controls for Development & Maintenance of TS Surveillance Procedures.New Procedure Made
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(iii) | | 05000311/LER-1997-008-02, :on 970715,failure to Enter Action Statement for Having Both Radiation Monitors in Same Control Room Air Intake Duct Was Inoperable.Caused by Misjudgement by CR Supervisor.Personnel Was Held Accountable |
- on 970715,failure to Enter Action Statement for Having Both Radiation Monitors in Same Control Room Air Intake Duct Was Inoperable.Caused by Misjudgement by CR Supervisor.Personnel Was Held Accountable
| | | 05000311/LER-1997-009-02, :on 970711,failure to Stroke Pump Discharge Valves for Potential Pressure Locking Concern Was Noted. Caused by Personnel Error.Revised Procedures to Address Addl Instances of CS Pump Operation |
- on 970711,failure to Stroke Pump Discharge Valves for Potential Pressure Locking Concern Was Noted. Caused by Personnel Error.Revised Procedures to Address Addl Instances of CS Pump Operation
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000272/LER-1997-009, :on 970418,determined That Past Operation of ECCS Was Outside of Plant Design Basis.Caused by Failure to Address All Accident Scenarios Affecting Assumptions Made. Issued New NPSH Calculation Re RHR Pumps |
- on 970418,determined That Past Operation of ECCS Was Outside of Plant Design Basis.Caused by Failure to Address All Accident Scenarios Affecting Assumptions Made. Issued New NPSH Calculation Re RHR Pumps
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1997-010, :on 970819,CR Operators Initiated Plant Shutdown to Comply W/Requirements of Ts.Caused by Design, Mfg Const/Installation Deficiencies.Calibr Procedure Revised |
- on 970819,CR Operators Initiated Plant Shutdown to Comply W/Requirements of Ts.Caused by Design, Mfg Const/Installation Deficiencies.Calibr Procedure Revised
| 10 CFR 50.73(a)(2)(viii) | | 05000272/LER-1997-010-01, :on 970819,position Indication Sys Were Shutdown as Required by Ts.Caused by Deficiencies in Design, Mfg Const/Installation.Successfully Recalibrated Rod Position Indication Sys |
- on 970819,position Indication Sys Were Shutdown as Required by Ts.Caused by Deficiencies in Design, Mfg Const/Installation.Successfully Recalibrated Rod Position Indication Sys
| | | 05000272/LER-1997-011-02, :on 971119,failure to Test Isolation of Sgb & SS on Automatic Start of Afps Was Noted.Caused by Inadequate Incorporation of DBA Mitigation Features Into Plant Tp.Pse&G Committed to Complete GL 96-01 Evaluations by 971231 |
- on 971119,failure to Test Isolation of Sgb & SS on Automatic Start of Afps Was Noted.Caused by Inadequate Incorporation of DBA Mitigation Features Into Plant Tp.Pse&G Committed to Complete GL 96-01 Evaluations by 971231
| 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000272/LER-1997-011, Forwards LER 97-011-00,re Failure to Test Isolation of SG Blowdown & Sampling Sys on Automatic Start of Afp,Per 10CFR50.73(a)(2)(ii)(A) | Forwards LER 97-011-00,re Failure to Test Isolation of SG Blowdown & Sampling Sys on Automatic Start of Afp,Per 10CFR50.73(a)(2)(ii)(A) | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000311/LER-1997-011-01, :on 970902,improper Scheduling of Staggered Surveillance Testing Was Noted.Caused by Personnel Error. Personnel Involved Have Been Held Accountable IAW Disciplinary Policies & Addl Training Provided |
- on 970902,improper Scheduling of Staggered Surveillance Testing Was Noted.Caused by Personnel Error. Personnel Involved Have Been Held Accountable IAW Disciplinary Policies & Addl Training Provided
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1997-012-01, :on 970709,identified Failure to Perform Surveillance Channel Checks of Loop Average Temp Channels. Caused by Misinterpretation of Info in Operating Logs. Revised Control Room Operating Logs |
- on 970709,identified Failure to Perform Surveillance Channel Checks of Loop Average Temp Channels. Caused by Misinterpretation of Info in Operating Logs. Revised Control Room Operating Logs
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1997-012-03, :on 970907,declared Reactor Coolant Loop 24 Overtemperature Differential Temp Inoperable Due to Differential Temp Being Lower than Acceptable.Returned Loop 23 Pressure Instrumentation to Service |
- on 970907,declared Reactor Coolant Loop 24 Overtemperature Differential Temp Inoperable Due to Differential Temp Being Lower than Acceptable.Returned Loop 23 Pressure Instrumentation to Service
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1997-013-01, :on 970902,unplanned Entry Into TS 3.0.3 Was Noted Due to Two Inoperable Pressurizer Level Channels. Caused by Error in RCS P&ID Drawing.Pressurizer Channel I Was Restored within Six Minutes of Event |
- on 970902,unplanned Entry Into TS 3.0.3 Was Noted Due to Two Inoperable Pressurizer Level Channels. Caused by Error in RCS P&ID Drawing.Pressurizer Channel I Was Restored within Six Minutes of Event
| | | 05000272/LER-1997-013-02, :on 970702,determined That EDG Should Have Been Declared Inoperable W/Test Instrumentation Connected.Caused by Personnel Error.Performed Satisfactory follow-up Test, Removed Equipment & Signed Off Procedure |
- on 970702,determined That EDG Should Have Been Declared Inoperable W/Test Instrumentation Connected.Caused by Personnel Error.Performed Satisfactory follow-up Test, Removed Equipment & Signed Off Procedure
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1997-014-01, :on 971002,Unit 2 Manually Tripped.Caused by Failure of Analog Input Circuit Board in Westrac Data Acquistion Sys.Westrac Data Acquisition Sys Removed from Digital Fws |
- on 971002,Unit 2 Manually Tripped.Caused by Failure of Analog Input Circuit Board in Westrac Data Acquistion Sys.Westrac Data Acquisition Sys Removed from Digital Fws
| | | 05000311/LER-1997-016-01, :on 970909,loss of Fire Protection Water to Auxiliary Bldgs & Containment Was Noted.Caused by Human Error Due to Inattention to Detail.Loss Prevention Tours Have Been Revised to Include Once Per Shift Verification |
- on 970909,loss of Fire Protection Water to Auxiliary Bldgs & Containment Was Noted.Caused by Human Error Due to Inattention to Detail.Loss Prevention Tours Have Been Revised to Include Once Per Shift Verification
| | | 05000272/LER-1997-016, ;on 970909,loss of FP Water to Salem,Units 1 & 2 Auxiliary Buildings & Containment Was Noted.Caused by Inadequate Control of 1RP5.Valves Were Opened & Locally Verified by Loss Prevention Personnel | ;on 970909,loss of FP Water to Salem,Units 1 & 2 Auxiliary Buildings & Containment Was Noted.Caused by Inadequate Control of 1RP5.Valves Were Opened & Locally Verified by Loss Prevention Personnel | | | 05000311/LER-1997-016-02, :on 971125,inadequate TS Testing Main Steam Isolation Valve Hydraulic Unit Override Contacts Were Noted. Caused by Lack of Adequate Controls.Operability of MSIV Hydraulic Unit Will Be Verified |
- on 971125,inadequate TS Testing Main Steam Isolation Valve Hydraulic Unit Override Contacts Were Noted. Caused by Lack of Adequate Controls.Operability of MSIV Hydraulic Unit Will Be Verified
| 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1997-016, Forwards LER 97-016-00 Re Loss of Fire Protection Water to Auxiliary Bldgs & Containments.Ler Was Originally Submitted on 971015 as LER 97-003-00.Encl Is Being Resubmitted W/Next Sequential LER Number | Forwards LER 97-016-00 Re Loss of Fire Protection Water to Auxiliary Bldgs & Containments.Ler Was Originally Submitted on 971015 as LER 97-003-00.Encl Is Being Resubmitted W/Next Sequential LER Number | | | 05000311/LER-1997-017-01, :on 971212,discovered That non-essential Heat Loads for Chilled Water Sys Were Not Isolated IAW TS Action Statement 3.7.10.a.1.Caused by Personnel Error.Personnel Involved Held Accountable & Revised Procedures |
- on 971212,discovered That non-essential Heat Loads for Chilled Water Sys Were Not Isolated IAW TS Action Statement 3.7.10.a.1.Caused by Personnel Error.Personnel Involved Held Accountable & Revised Procedures
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1997-018-01, :on 971125,inadequate TS Testing of MSIV Hydraulic Unit Override Contacts,Was Identified.Caused by Lack of Adequate Controls.Procedure S1(2).OP-ST.MS-0003(Q) Revised to Include Testing of MSIV Hydraulic Unit Override |
- on 971125,inadequate TS Testing of MSIV Hydraulic Unit Override Contacts,Was Identified.Caused by Lack of Adequate Controls.Procedure S1(2).OP-ST.MS-0003(Q) Revised to Include Testing of MSIV Hydraulic Unit Override
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1997-018, Forwards LER 97-018-00, Inadequate TS Testing - Main Steam Isolation Valve Hydraulic Unit Override Contacts. LER Was Originally Submitted on 971224 as LER 97-016.Number Was Already Assigned to Special Rept | Forwards LER 97-018-00, Inadequate TS Testing - Main Steam Isolation Valve Hydraulic Unit Override Contacts. LER Was Originally Submitted on 971224 as LER 97-016.Number Was Already Assigned to Special Rept | |
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