05000366/LER-1979-053-03, /03L-0 on 790611:high Trip Setpoint of Monitor 2D11-K603D Was Higher than Tech Spec Limits.Caused by Personnel Error.Setpoint Corrected

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/03L-0 on 790611:high Trip Setpoint of Monitor 2D11-K603D Was Higher than Tech Spec Limits.Caused by Personnel Error.Setpoint Corrected
ML19241A763
Person / Time
Site: Hatch 
Issue date: 06/26/1979
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19241A761 List:
References
LER-79-053-03L, LER-79-53-3L, NUDOCS 7907090363
Download: ML19241A763 (1)


LER-1979-053, /03L-0 on 790611:high Trip Setpoint of Monitor 2D11-K603D Was Higher than Tech Spec Limits.Caused by Personnel Error.Setpoint Corrected
Event date:
Report date:
3661979053R03 - NRC Website

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['. lith the unit in startup a11d the MSIt S closed during performance of HNP-2-3005, main j n

2 ga gteaa line high radiation FT&C, the high trip setpoint of monitcr 2Dll-K603D was g [found higher than tFeallowable tolerance at 4900 MR/HR.

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CAU:,E DESCRIP TIC'. AND CC7RECTIVE AC N CNS 27 [j.l, o l [The cause of incorrect setpoint was cersonnel error The wtpoint.as changed on

& [6/3/79 at the request of countina roca personnel as author: xd per H4P-7450.

The de-l 11 j'_] [ sired setpoint was not legible on the work order The tec nnici m atteTpted to verify j il i the desired setpoint and this vias cominunicated incorre"th Thus it was set incw rect 1 i

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Tne setecint was cnrr_oct.ed on 6/11/79 per HNP-2-5100 md HNP-2-3005 was completed.l r-m, Yb y

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