05000368/LER-1979-089-03, /03L-0:on 791124,during Mode 3 Operation,Emergency Feedwater Flow Control Valve 2CV-1025-1 Failed to Close on Demand from Control Room.Caused by Trash in Valve Operator Hydraulic Sys & Hydraulic Snubber Out of Adjustment

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/03L-0:on 791124,during Mode 3 Operation,Emergency Feedwater Flow Control Valve 2CV-1025-1 Failed to Close on Demand from Control Room.Caused by Trash in Valve Operator Hydraulic Sys & Hydraulic Snubber Out of Adjustment
ML19256G496
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 12/21/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19256G491 List:
References
LER-79-089-03L, LER-79-89-3L, NUDOCS 7912310393
Download: ML19256G496 (1)


LER-1979-089, /03L-0:on 791124,during Mode 3 Operation,Emergency Feedwater Flow Control Valve 2CV-1025-1 Failed to Close on Demand from Control Room.Caused by Trash in Valve Operator Hydraulic Sys & Hydraulic Snubber Out of Adjustment
Event date:
Report date:
3681979089R03 - NRC Website

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NRC F ORM 366 U. S. NUCLE AR REGUL ATORY COMMIS$10N LICENSEE EVENT REPORT EXHIBIT A CONTROL S LOCK: l l l l \\ l lh (PLE ASE PRINT OR TYPE ALL REOutRED INFORMATION) l AlR l A] Nj 0 l 2 lgl 0 l0 l -l0 l 0 ] 0l Oj 0 l-l 0 l0 lg l1 l 1]l l 1lg; j lg o

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DOCstET N' Jut ER 68 69 EVENT DATE 74 75 HEPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEOUENCES h 1 Durino Mode 3 operation, with the electric driven Emercacy Feed. water i

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e i pump, 2P7B, in service as an auxiliary feedwater pump for normal startup i I Steam Generator feed. EFW flow control valve. 2CV-1026-1. failed tn clnsel o

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The valve failed in the EFW. or safe.

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All redundant EFW valves were su cessfully stroked from th9 I

a i l Control Room. This occurrence is similar to LER 50-368/79-088 and 79-043L are co-168/79-06R.74-094. 70 ns1 1 i Other ocqyrrences involvino 2CV-1025-1 o

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