LER-1978-055, /01T-0:on 780605,safety Features Actuation Sys Sequencer Failed During Test.Caused by Design Deficiency in Sys Mod.Electrical Slide Link Uses & Mgt Controls for Slide Links to Be Reviewed |
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- . EVENT DESCRIPTICN AND PROSABLE CONSEQUENCES h The test failed due ]
I o 1: 1 l On 6/2/78, the "18 Month SFAS Surveillance Test" was conducted.'
Investigation l
l to an SFAS sequencer failing to properly operate in SFAS Channel 1.
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l o 4.: i i revealed there was a design deficiency cocbined with the slide links being incorrect y Had an SFAS actuation occurred, and if there was a loss of offsite power, j left open.
lois] I the sequencer would not have automatically sequenced ECCS loads onto the essential l
ic #s l I The operators would have been able to manually load the emergency diesel l
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[ has been written to correct the design deficiency.
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TOLEDO EPISON COMPANY l
DAVIS-SESSE UNIT ONE HUCLEAR POWER STATION SUPPLEMENTAL INFORMATION TO LER NP-32-78-05 j
DATE OF EVENT:, June 5, 1978 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Safety Features Actuation System (SFAS) Sequ,encer Failure Conditions Prior tc Occurrence:
The unit was in Mode 6 with Power (MRT) = 0, and
. Load (MWE; = 0.
Description of Occurrence: On June 2,1978, the "18 Month SFAS Surveillance Test",
ST 5031.07, was conducted. The test failed due to an SEAS sequencer failing to properly operate in SFAS Channel 1.
Troubleshooting was performed supported by Power Engineering personnel.
Investigation of the problem continued until June 5, 1978, at which time the apparent cause(s) of the problem was determined.
On that date,' Region III of the. U. S. Nuclear Regulatory Commission was notified of the problem by telephone. This occurrence is being reported per Technical Specifica-tion 6.9.1.8.1.
J Cause of Occurrence:
The cause was a design error in a system revision. The chronological sequence which follows should best illustrate the sequence of events and what led to the events of June 2, 1978.
(1) 12/76 - Bechtel Power Corporation issued a System Revision Notice, 'SRN 221E, which was designed to provide sequencer operation for two additional design conditions:
(a) If a diesel were stopped during an SFAS actuation and later offsite power was lost, the sequencer would be restarted; (b) If diesel were supplying essential busses and then an SEAS actuation occurred', the sequencer would be started. There was a design deficiency in SRN 221E which would inhibit proper function-of the SFAS sequencers.
(2) 2/14/77 - SRN 221E was installed by construction personnel, scheme checked per Construction Wotk Permits 48-E-12, 13 and 24-E-51.
Apparently at least four terminal block connecting links (slide links) were lef t open, thus negating
- - the condition (b) change of this SRN.
(3) 2/20 '- 2/23/77 - TP 310.02, "SFAS Integrated Test" was successfully. per-formed. This test procedure had been modified to test SRN. 221E changes.
It failed to detect the misapplication of the design due to the slide links being in the open position.
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DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION TO LER NS-32-78-05 PAGE 2 i.
(4) 2/23/77 - 6/2/78 - Sometime within this period all but two of the open ter-minal block slide links were closed enabling the design deficiency.
The actual date or reason for this event has not as yet been found.-
(5) 6/2/78 - SFAS 18 Month Test, ST 5031.07, was conducted. This test was a repeat of TP 310.02. The test failed when conducted on SA Channel 1, as a direct result of the slide links being closed and the design deficic'ncy j ;
1 in SRN 221E.
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'(6) 6/3/78 - In the course of troubleshooting, two SFAS relay contacts which h
were part of the circuitry described here, but not causing any test failures were found not to have wires going from the relays to the ' external connec-tions.
This'was a manufacturer's error that did not affect the test or the safety of the system because it was redundant wiring.
(7) 6/4/78 - Slide links in the open position were discovered in the channel il which appear.ed to function properly during ST 5031.07.
(8) 6/5/78 - Power Engineering personnel confirmed that a design, deficiency existed in both SA Channels 1 and 2.
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~~' Analysis of occurrence: Had an SFAS actuation occurred after the time when the slide links were closed, and if 'there was a loss of offsite power, the sequencer il would not have automatically sequenced emergency core cooling system loads onto il the essential busses. In all such cases, except condition (b), sequenced loads l
would not load onto the bus. The operators, however, in such conditions would have been able to manually load the emergency diesel generator.
In condition (b),
all normally sequenced loads could have immediately loaded onto the bus if they
!j received a simultaneous incident level 1, 2, 3 or 4 SFAS actuation.
The tripping il of various incident levels on SEAS is not calculated to occur simultaneously except for a major pipe break (28" or 36").
Incident levels 1 and 2 (high pressure injection pumps and containment air coolers) trip at a reactor coolant pressure less than 1600 psig. Incident level 3 (decay heat pumps)' trips at a reactor l.
coolant pressure less than 400 psig or a containment pressure less than 4 psig.
ll Incident level 4 (containment spray pumps) trips at a containment pre,ssure greater than 24 psig.
The component cooling water and service water pump would have
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been previously started when the loss of power occurred.
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Corrective Action
The corrective action taken will be a modification to correct the design and correct any hardware deficiencies (Facility Change Request 78-268).
ij Corrective actions include a review of slide link uses and =anagement controls for
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TOLEDO EDISON COMPAh7 DAVIS-BESSE UNIT'ONE NUCLEAR POWER. STATION PAGE 3 SUPPLDIENTAL INFORMATION FOR LER NP-32-78-05 slide links, a technical review of design control features versus surveillance test procedures and administratively controlling use of logic drawinigs (used '
as specification drawings) to insure that.they properly reflect vendor supplied equip =ent.
,l Failure Data: This is not a repetitive occurrence.
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| 05000346/LER-1978-002-03, /03L-0:on 780103,control Rod Group 5 Rod 12 Absolute Position Indication Declared Inoperable.Caused by Component Failure of Absolute Position Indicator Reed Switch.Switch Replaced | /03L-0:on 780103,control Rod Group 5 Rod 12 Absolute Position Indication Declared Inoperable.Caused by Component Failure of Absolute Position Indicator Reed Switch.Switch Replaced | | | 05000346/LER-1978-002, Forwards LER 78-002/03L-0 | Forwards LER 78-002/03L-0 | | | 05000346/LER-1978-003-03, /03L-0:on 780103,unidentified RCS Leakage Greater than 1,66 Gallon Per Minute.Caused by Loose Packing on Valve DH2735.Valve Repacked & Stroked | /03L-0:on 780103,unidentified RCS Leakage Greater than 1,66 Gallon Per Minute.Caused by Loose Packing on Valve DH2735.Valve Repacked & Stroked | | | 05000346/LER-1978-003, Forwards LER 78-003/03L-0 | Forwards LER 78-003/03L-0 | | | 05000346/LER-1978-004, Forwards LER 78-004/03L-0 | Forwards LER 78-004/03L-0 | | | 05000346/LER-1978-004-03, /03L-0:on 780105,inlet Balancing Dampers to Emergency Ventilation Sys Fans 1-1 & 1-2 Found Closed.Cause Unknown.Dampers Returned to Balance Position & Locknut Tightened | /03L-0:on 780105,inlet Balancing Dampers to Emergency Ventilation Sys Fans 1-1 & 1-2 Found Closed.Cause Unknown.Dampers Returned to Balance Position & Locknut Tightened | | | 05000346/LER-1978-005-03, /03L-0:on 780106,auxiliary Feed Pump Turbine 1-1 Speed Control Lost & Declared Inoperable.Caused by Short Circuits & Blown Fuses Due to Design Deficiency.Higher Current Rated Relays Installed & Circuit Modified | /03L-0:on 780106,auxiliary Feed Pump Turbine 1-1 Speed Control Lost & Declared Inoperable.Caused by Short Circuits & Blown Fuses Due to Design Deficiency.Higher Current Rated Relays Installed & Circuit Modified | | | 05000346/LER-1978-005, Forwards LER 78-005/03L-0 | Forwards LER 78-005/03L-0 | | | 05000346/LER-1978-006-03, /03L-0:on 780107,computer Alarm Indicated That Steam & Feedwater Rupture Control Sys Steam Generator to Feedwater Differential Pressure Channel 1 Had Tripped.Caused by Component Failure.Input Buffer 1-3 in Channel 1 Replaced | /03L-0:on 780107,computer Alarm Indicated That Steam & Feedwater Rupture Control Sys Steam Generator to Feedwater Differential Pressure Channel 1 Had Tripped.Caused by Component Failure.Input Buffer 1-3 in Channel 1 Replaced | | | 05000346/LER-1978-006, Forwards LER 78-006/03L-0 | Forwards LER 78-006/03L-0 | | | 05000346/LER-1978-007-03, /03L-0:on 780109,during Monthly Surveillance Test ST 5081.01,diesel Generator 1-1 Tripped on High Crankcase Pressure.Caused by Dirty Crankcase Vent Oil Collector.Vent Oil Collector Disassembled & Cleaned | /03L-0:on 780109,during Monthly Surveillance Test ST 5081.01,diesel Generator 1-1 Tripped on High Crankcase Pressure.Caused by Dirty Crankcase Vent Oil Collector.Vent Oil Collector Disassembled & Cleaned | | | 05000346/LER-1978-007, Forwards LER 78-007/03L-0 | Forwards LER 78-007/03L-0 | | | 05000346/LER-1978-008-03, /03L-0:on 780112,both Containment Spray Pumps Found Inoperable.Caused by Personnel Error.Spray Pump Circuit Breakers re-energized | /03L-0:on 780112,both Containment Spray Pumps Found Inoperable.Caused by Personnel Error.Spray Pump Circuit Breakers re-energized | | | 05000346/LER-1978-008, Forwards LER 78-008/03L-0 | Forwards LER 78-008/03L-0 | | | 05000346/LER-1978-009-03, /03L-0:on 780112,component Cooling Water Heat Exchanger 1-1 Outlet Isolation Valve SW 1424 Declared Inoperable.Caused by Component Failure.Solenoid Valve in Control Scheme Found Burned Out.Unit Removed | /03L-0:on 780112,component Cooling Water Heat Exchanger 1-1 Outlet Isolation Valve SW 1424 Declared Inoperable.Caused by Component Failure.Solenoid Valve in Control Scheme Found Burned Out.Unit Removed | | | 05000346/LER-1978-009, Forwards LER 78-009/03L-0 | Forwards LER 78-009/03L-0 | | | 05000346/LER-1978-010-03, /03L-0:on 780115, Reactor Coolant Pump Monitor on Channel 1 Found Out of Tolerance & Reactor Protection Sys Declared Inoperable.Caused by Defective Module.New Module Calibr & Installed | /03L-0:on 780115, Reactor Coolant Pump Monitor on Channel 1 Found Out of Tolerance & Reactor Protection Sys Declared Inoperable.Caused by Defective Module.New Module Calibr & Installed | | | 05000346/LER-1978-010, Forwards LER 78-010/O3L-0 | Forwards LER 78-010/O3L-0 | | | 05000346/LER-1978-011, Forwards LER 78-011/03L-0 | Forwards LER 78-011/03L-0 | | | 05000346/LER-1978-011-03, /03L-0:on 780116,during Surveillance Test,Decay Heat Pump 1-1 Failed to Start.Caused by Fuses in Breaker for Decay Heat Motor Failing to Make Proper Contact.Control Power Fuese Pulled & Reinserted.Pump Returned to Svc | /03L-0:on 780116,during Surveillance Test,Decay Heat Pump 1-1 Failed to Start.Caused by Fuses in Breaker for Decay Heat Motor Failing to Make Proper Contact.Control Power Fuese Pulled & Reinserted.Pump Returned to Svc | | | 05000346/LER-1978-012, Forwards LER 78-012/03L-0 | Forwards LER 78-012/03L-0 | | | 05000346/LER-1978-012-03, /03L-0:on 780124,personnel Airlock Failed Leak Rate Test.Caused by Loose Shaft Seal Due to Routine Use of Personnel & Escape Lock (Exit/Entry to Containment).Shaft Seals Tightened to Prevent Excessive Leakage | /03L-0:on 780124,personnel Airlock Failed Leak Rate Test.Caused by Loose Shaft Seal Due to Routine Use of Personnel & Escape Lock (Exit/Entry to Containment).Shaft Seals Tightened to Prevent Excessive Leakage | | | 05000346/LER-1978-013-03, /03L-0:780119,Cell 32 in Station Battery 1N Electrolyte Specific Gravity Decreased 0.003 Greater than Allowed by Tech Spec 3.8.2.3.Caused by Electrolyte Stratification Due to Low Battery Loading | /03L-0:780119,Cell 32 in Station Battery 1N Electrolyte Specific Gravity Decreased 0.003 Greater than Allowed by Tech Spec 3.8.2.3.Caused by Electrolyte Stratification Due to Low Battery Loading | | | 05000346/LER-1978-013, Forwards LER 78-013/03L-0 | Forwards LER 78-013/03L-0 | | | 05000346/LER-1978-014, Forwards LER 78-014/03L-0 | Forwards LER 78-014/03L-0 | | | 05000346/LER-1978-014-03, /03L-0:on 780123,quandrant Power Tilt in Excess of Steady State & Transient Limits Indicated by Unit Process Computer.Caused by Detector Inadvertently Left Off Scan After Testing.Test Procedure Being Modified | /03L-0:on 780123,quandrant Power Tilt in Excess of Steady State & Transient Limits Indicated by Unit Process Computer.Caused by Detector Inadvertently Left Off Scan After Testing.Test Procedure Being Modified | | | 05000346/LER-1978-015, Forwards LER 78-015/03L-0 | Forwards LER 78-015/03L-0 | | | 05000346/LER-1978-015-03, /03L-0:on 780131,feedwater Steam Generator 1 Channel 2 Pressure Differential Switch Did Not Actuate at Desired Setpoint During Surveillance Test.Caused by Pressure Differential Switch Out of Tolerance | /03L-0:on 780131,feedwater Steam Generator 1 Channel 2 Pressure Differential Switch Did Not Actuate at Desired Setpoint During Surveillance Test.Caused by Pressure Differential Switch Out of Tolerance | | | 05000346/LER-1978-016-03, /03L-1:on 780202,absolute Position Indicator for Group 5,Rod 12,declared Inoperable.Caused by Component Failure in Penetration Area.Containment Conductors Connected to Spare Penetration Connector | /03L-1:on 780202,absolute Position Indicator for Group 5,Rod 12,declared Inoperable.Caused by Component Failure in Penetration Area.Containment Conductors Connected to Spare Penetration Connector | | | 05000346/LER-1978-016, Forwards LER 78-016/03L-1,LER 78-021/03L-1,LER 78-100/03L-1, LER 78-034-03L-1 & LER 78-024/03L-1 | Forwards LER 78-016/03L-1,LER 78-021/03L-1,LER 78-100/03L-1, LER 78-034-03L-1 & LER 78-024/03L-1 | | | 05000346/LER-1978-017, Forwards LER 78-017/03L-0 | Forwards LER 78-017/03L-0 | | | 05000346/LER-1978-017-03, /03L-0:on 780126,all Meteorological Channels Became Inoperable During Blizzard.Caused by Instrumentation Power Loss Due to Tripped Breaker at Meteorological Tower. Breaker Reset on 780128 | /03L-0:on 780126,all Meteorological Channels Became Inoperable During Blizzard.Caused by Instrumentation Power Loss Due to Tripped Breaker at Meteorological Tower. Breaker Reset on 780128 | | | 05000346/LER-1978-018-03, /03L-0:on 780208,diesel Generator 1-1 Making Unusual Noises During Monthly Test.Unusual Noise Traced to Turbocharger.Exact Cause Undetermined.Turbocharger Replaced & Diesel Generator Monthly Test Completed | /03L-0:on 780208,diesel Generator 1-1 Making Unusual Noises During Monthly Test.Unusual Noise Traced to Turbocharger.Exact Cause Undetermined.Turbocharger Replaced & Diesel Generator Monthly Test Completed | | | 05000346/LER-1978-018, Forwards LER 78-018/03L-0 | Forwards LER 78-018/03L-0 | | | 05000346/LER-1978-019-03, /03L-1:on 780210,decay Heat Cooler Outlet Valve DH14A & DH14B Mechanical Stops Found Incorrectly Opened. Caused by Personnel Incorrectly Resetting Stops After Previous Work Completion.Stops Tagged & Records Marked | /03L-1:on 780210,decay Heat Cooler Outlet Valve DH14A & DH14B Mechanical Stops Found Incorrectly Opened. Caused by Personnel Incorrectly Resetting Stops After Previous Work Completion.Stops Tagged & Records Marked | | | 05000346/LER-1978-020, Forwards LER 78-020/03L-0 | Forwards LER 78-020/03L-0 | | | 05000346/LER-1978-020-03, /03L-0:on 780210,reactor Protection Sys Channel 3 Hot Leg Temp String TI-RC3B4 Declared Inoperable.Caused by Loose Wire Connection.Loose Terminal at Temp Element Tightened,Rendering TI-RC3B4 Operable | /03L-0:on 780210,reactor Protection Sys Channel 3 Hot Leg Temp String TI-RC3B4 Declared Inoperable.Caused by Loose Wire Connection.Loose Terminal at Temp Element Tightened,Rendering TI-RC3B4 Operable | | | 05000346/LER-1978-021-03, /03L-1:on 780220,absolute Position Indicator for Control Rod 12 of Group 5 Declared Inoperable.Caused by Component Failure in Penetration Area.Conductors Connected W/Spare Penetration Connectors | /03L-1:on 780220,absolute Position Indicator for Control Rod 12 of Group 5 Declared Inoperable.Caused by Component Failure in Penetration Area.Conductors Connected W/Spare Penetration Connectors | | | 05000346/LER-1978-022-03, /03L-0:on 780223,flow Transmitter FTRC1A3 Found Inoperable.Caused by Defective Flow Transmitter Amplifier. Amplifier Replaced & Flow Transmitter FTRC1A3 Returned to Svc on 780226 | /03L-0:on 780223,flow Transmitter FTRC1A3 Found Inoperable.Caused by Defective Flow Transmitter Amplifier. Amplifier Replaced & Flow Transmitter FTRC1A3 Returned to Svc on 780226 | | | 05000346/LER-1978-022, Forwards LER 78-022/03L-0 | Forwards LER 78-022/03L-0 | | | 05000346/LER-1978-023-03, /03L-0:on 780224,temp Indication for Reactor Protection Sys Channel 2 Spiked Tripping Channel & Shut Down Reactor.Caused by Faulty Connector Due to Dirt on Contacts. Channel 2 Temp String Modules Removed & Connectors Cleaned | /03L-0:on 780224,temp Indication for Reactor Protection Sys Channel 2 Spiked Tripping Channel & Shut Down Reactor.Caused by Faulty Connector Due to Dirt on Contacts. Channel 2 Temp String Modules Removed & Connectors Cleaned | | | 05000346/LER-1978-023, Forwards LER 78-023/03L-0 | Forwards LER 78-023/03L-0 | | | 05000346/LER-1978-024-03, /03L-1:on 780228,MSIV MS-101 Rendered Inoperable to Allow Maint Personnel to Remove Raised Metal on Two of Four Spring Guide Tubes.Cause of Raised Metal Unknown.Metal Filed Down,Valve Closing Time Adjusted & Valve Tested | /03L-1:on 780228,MSIV MS-101 Rendered Inoperable to Allow Maint Personnel to Remove Raised Metal on Two of Four Spring Guide Tubes.Cause of Raised Metal Unknown.Metal Filed Down,Valve Closing Time Adjusted & Valve Tested | | | 05000346/LER-1978-025-03, /03L-0:on 780304,RCS Leakage Found Greater than 1 Gallon Per Minute.Leakage Cause Undetermined.Leakages Processed Through Normal Containment Sump.Unidentified RCS Leakage Reduced Below 1 Gallon Per Minute in 5.5-h | /03L-0:on 780304,RCS Leakage Found Greater than 1 Gallon Per Minute.Leakage Cause Undetermined.Leakages Processed Through Normal Containment Sump.Unidentified RCS Leakage Reduced Below 1 Gallon Per Minute in 5.5-h | | | 05000346/LER-1978-025, Forwards LER 78-025/03L-0 | Forwards LER 78-025/03L-0 | | | 05000346/LER-1978-026, Forwards LER 78-026/03L-0 | Forwards LER 78-026/03L-0 | | | 05000346/LER-1978-026-03, /03L-0:on 780309,radiation Monitor Re 5029 Found Inoperable Due to Low Sample flow.12 Previous Radiation Monitor Inoperabilities Not Reported.Caused by Pump Motor Bearing Seizure Due to High Ambient Temp | /03L-0:on 780309,radiation Monitor Re 5029 Found Inoperable Due to Low Sample flow.12 Previous Radiation Monitor Inoperabilities Not Reported.Caused by Pump Motor Bearing Seizure Due to High Ambient Temp | | | 05000346/LER-1978-027, Forwards LER 78-027/03L-0 | Forwards LER 78-027/03L-0 | | | 05000346/LER-1978-027-03, /03L-0:on 780316,stop Valve AF3870 Failed to Open During Testing.Caused by High Differential Pressure Due to Check Valve AF39 & AF72 Leakage.Motor Operator Initially Not Adjusted for This Pressure,Causing Operator to Torque | /03L-0:on 780316,stop Valve AF3870 Failed to Open During Testing.Caused by High Differential Pressure Due to Check Valve AF39 & AF72 Leakage.Motor Operator Initially Not Adjusted for This Pressure,Causing Operator to Torque Out | | | 05000346/LER-1978-028-03, /03L-0:on 780318,channel 1 Steam Generator 1-1 Declared Inoperable.Caused by Water in Level Transmitter SP09B8 Connecting Box Due to Steam Leak.Connection Box Cleaned & Dried.Waterproof Fitting Will Be Installed | /03L-0:on 780318,channel 1 Steam Generator 1-1 Declared Inoperable.Caused by Water in Level Transmitter SP09B8 Connecting Box Due to Steam Leak.Connection Box Cleaned & Dried.Waterproof Fitting Will Be Installed | |
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