05000368/LER-1980-023-03, /03L-0:on 800506,while Performing Inservice Testing of Sodium Hydroxide Addition Tank Discharge Valve, Spray Sys Tripped During Cycle Manuver.Caused by Flex Electrical Conduit Being Stepped On.Conductor Reinsulated

From kanterella
Revision as of 19:50, 31 December 2024 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
/03L-0:on 800506,while Performing Inservice Testing of Sodium Hydroxide Addition Tank Discharge Valve, Spray Sys Tripped During Cycle Manuver.Caused by Flex Electrical Conduit Being Stepped On.Conductor Reinsulated
ML19323G069
Person / Time
Site: Arkansas Nuclear 
Issue date: 05/29/1980
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19323G066 List:
References
LER-80-023-03L, LER-80-23-3L, NUDOCS 8005300335
Download: ML19323G069 (1)


LER-1980-023, /03L-0:on 800506,while Performing Inservice Testing of Sodium Hydroxide Addition Tank Discharge Valve, Spray Sys Tripped During Cycle Manuver.Caused by Flex Electrical Conduit Being Stepped On.Conductor Reinsulated
Event date:
Report date:
3681980023R03 - NRC Website

text

O:

i h C FORM 34 U.S. huCLE AR REGULATORY COMMtsSION LICENSEE EVENT REPORT EXHIBIT A

.h CONTROL OLOCK: l l l l l l l

(PLE ASE PRINT OR TYPE ALL REQUIRED INFORMAT80N) y l AlR l Al N] 0 l 2 lgl6010 l - 10 l 0 [ 0l 0l 0 ]- l 0 l0 lg l1 l 1 l1 l 1 lgl l lg i

e 9 teCINsii C"Ag a4 1

44CiNS NVwe t h 25 A

tactNs. g5,6 JO bi C AT ie CON'T

",0,0 LL_J@l015 p 101013 >6 18 )@t015 i 016 i 810 l@l 0151219 I 810 l@

o i 8

to 4'

ooc 8Lif huugg.

MB 69 aviNT DAY.

34 75 saf O.TDATi 80 EVENT DESCRIPTION ANO PROBA8LE CONSEQUENCES h F6TF1 I During Mode 1 operation, while performino Irservice Testino of the Na0H I e i addition tank discharge valve, 2CV-5667, to the R.B. spray system, 2CV-5667 I tripped durina its cycle manuver.

The redundant Sodium Hydroxide Addition o 4 o s i System remained operable.

LER 50-368/79-080 also involved the loss of i

i 2CV-5667. This occurrence is reportable per T.S. 6.9.1.9.b.

i o e Lo_Li_J i

[

o e i I

'N' "

'[cie' sNES:

E JNa 3NTS:

o..wi~vcou.

FTO I S IH 18 L,E_j@ [A_J@ IV l A lL JV I E lX (@ [_Ejg [D j @

,o u

~

w i~,.i..

t'<%'.';"

"M " '"'

'17t

" O'"

o

@,arg...o 1 8101 L-J 10 12131 a,,

1013 1 L.L_J L. -J LO_J

,a i

_m.

n n

u z.

2 u

T&EiN A T ON 7

Mit wou $ 22

.T

,om UM

$U[L[ _j@ l z l 9'lh""I 9l@

WAN

'[.

LBJ@LZ_J@ Lzj@

tz_.j@

l0lOf Q ul LNj@

dj@

3J 34 3b 36 Ji ao el 42 43 se er CAUSE DESCRIPTION ANO CORRECflVE ACTIONS h i,io,1 The flex electrical conduit had been stepped on at the valve operator i

i,i,,i cutting the wire insulation and exposing the conductor.

This created i a ground fault which blew the control power supply fuse. The conductor l was reinsulated, the valve tested and declared operable meeting Action i

, 3 r i i. i i Statement T.S. 3.6.2.2.

i

'd'A'Us'

"? "$, v'

[ _j@l Inservice Tes'. 63Y oesCpte,fioN @

%,0Wi.

oTM e. 87 ATUS O

m [E_J@ l 01 410 l@l NA l

ting l

' !r,,,,,iu.sio o,svi=1 nuovur o,4ctivity @ "

tocar.oo,.euiss@

c

=

asu ase LZ_J @ [Z_j @ l NA l

l NA l

i c

,,v.,0~~..... ' *. o, ",,

a n

o 5c.,v.o @

rvn 10101 Ol@[2_J@l NA l

i 7

' ' n so.=.~i t'.~;u'.',esoisc..no=@

a

~u..

1010l0 l@l NA l

i =

' ho,ogo" ce'[on c.urv g a

llj@l NA l

i o

" :sy s....,_ e a

~RC ex -,

ud ei NA 7 e i iiiiiiiiiiiii Chris N. Shively 505/968-2519 NAME OF PRdPARER

,,,m 8005300 % $