LER-1978-083, /03L-0:on 780720,containment vessel-to-annulus Differential Pressure Exceeded Tech Spec Limit.Caused by Personnel & Procedural Error.Rate of Pressure Increase Too Great for Shift Check Monitoring.St 5099.01 Modified |
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4 EVENT DESCRIPTION AND PRC8ASLE CONSECUENCES h l o 121 l' At 0820 hours0.00949 days <br />0.228 hours <br />0.00136 weeks <br />3.1201e-4 months <br /> on 7/20/78, it was noted that containment vessel to annulus differential l l pressure exceeded the TS 3.6.1.4 limit of +25 inches water gage by 1 inch water gage.
I o 3 Contain-I gTlq l At 1047 hours0.0121 days <br />0.291 hours <br />0.00173 weeks <br />3.983835e-4 months <br /> on 7/20/78, the purge of the conta4=ent building commenced.
lo i s i I ment vessel to annulus differential pressure was within allowable limits at 1050 hours0.0122 days <br />0.292 hours <br />0.00174 weeks <br />3.99525e-4 months <br /> ;
There was no ' threat to the health and safety of the public or unit person g Io is 1 l on 7/20/78.
The slight increase above the TS limit would not cause contaiment vessel inter y fij-l7l l nel.
(NP-33-78-100) nal pressure to exceed the design pressure if a LOCA had occurred.
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p TOLEDO EDISON COMPANY DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION FOR LER NP-33-78-100 DATE OF OCCURRENCE: July 20, 1978 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Containment Vessel to Annulus High Differential Pressure on Plant Startup Conditions Prior to Occurrence: The unit was in Mode 3, with Power (WT) = 0, and Load (MWE) = 0.
Description of Occurrence: At 0820 hours0.00949 days <br />0.228 hours <br />0.00136 weeks <br />3.1201e-4 months <br /> on July 20, 1978, it was noted that coneminment vessel to annuius differential pressure exceeded the Technical Speci-fication limit of +25 inches water gage by 1 inch water gage. This placed the unit in the Action Statement of Technical Specification 3.6.1.4.
Plant Startup Frocedure, PP 1102.02 was in progress. At 0350 hours0.00405 days <br />0.0972 hours <br />5.787037e-4 weeks <br />1.33175e-4 months <br /> on July 20, 1978, a courninment purge permit was initiated due to a containment vessel to annulus differential pressure of +23 inches water gage. At 0820 hours0.00949 days <br />0.228 hours <br />0.00136 weeks <br />3.1201e-4 months <br /> on July 20, V) At 1047 hours0.0121 days <br />0.291 hours <br />0.00173 weeks <br />3.983835e-4 months <br /> on July 1978, the containment vessel to annulus differential pressure exceeded +25 inches.
s 20, 1978, the purge of the containment building commenced.
Containment vessel to annulus differential pressure was within allowable limits at 1050 hours0.0122 days <br />0.292 hours <br />0.00174 weeks <br />3.99525e-4 months <br /> on July 20, 1978, which removed the unit from the Action Statement of Technical Specification 3.6.1.4.
Designation of Apnarent Cause of Occurrence: The cause of this occurrence is both procedural and personnel error. The containment vessel to annulus differential pressure was being monitored by ST 5099.01, " Miscellaneous Instrument Shift Check",
uhich is performed once every eight hours. The rate of increase of containment vessel to annulus differential pressure was too great to be adequately monitored by the shift check.
Additionally, the time span between initiation of corrective action (preparation of the containment purge permit) and actual commencement of die containment vessel purge (6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and 57 minutes) was ercessive. Proper urgency and followup with regard to the processing of the contaicment purge permit would have prevented e:.-
ceeding the technical specification limit.
l Analysis of Occurrence: There was no threat to the health and safety of the public or to unit personnel. The slight increase above the technical specification limit would not cause containment vessel internal pressure to exceed the design pressure of 40 psig during a loss of coolant accident condition.
V LER #78-083
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,e TOLEDO EDISON COMPANY DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION PAGE 2 SUPPLDfENTAL INFORE\\ TION FOR LER NP-33-78-100 ST 5099.01, " Miscellaneous Instrument Shift checks" has been
Corrective Action
modified to provide additional guidance to the operator concerning when to initiate Containment vessel to annulus corrective action to prevent exceeding the limit.
differential pressure has been added to the control room reading sheets (read approximately once every four hours) to provide the operator with trend information.
All affected personnel will be notified of the delay in implementing the release Permit and requested to accelerate this process.
the containment vessel to annulus differential Failure Data:. On October 18, 1977, pressure technical specification limit was exceeded (Licensee Event Report NP-33-7 It was believed the cause of the October,1977 occurrence was the operation of only j
j one contain= ant air cooler; therefore, the startup procedure was modified to assure Since both containrient air coolers two containment air coolers were in operation.
were in operation prior to this occurrence, this addit'ional operational experience has shown further corrective action was necessary.
LER #78-083 i
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| 05000346/LER-1978-002-03, /03L-0:on 780103,control Rod Group 5 Rod 12 Absolute Position Indication Declared Inoperable.Caused by Component Failure of Absolute Position Indicator Reed Switch.Switch Replaced | /03L-0:on 780103,control Rod Group 5 Rod 12 Absolute Position Indication Declared Inoperable.Caused by Component Failure of Absolute Position Indicator Reed Switch.Switch Replaced | | | 05000346/LER-1978-002, Forwards LER 78-002/03L-0 | Forwards LER 78-002/03L-0 | | | 05000346/LER-1978-003-03, /03L-0:on 780103,unidentified RCS Leakage Greater than 1,66 Gallon Per Minute.Caused by Loose Packing on Valve DH2735.Valve Repacked & Stroked | /03L-0:on 780103,unidentified RCS Leakage Greater than 1,66 Gallon Per Minute.Caused by Loose Packing on Valve DH2735.Valve Repacked & Stroked | | | 05000346/LER-1978-003, Forwards LER 78-003/03L-0 | Forwards LER 78-003/03L-0 | | | 05000346/LER-1978-004, Forwards LER 78-004/03L-0 | Forwards LER 78-004/03L-0 | | | 05000346/LER-1978-004-03, /03L-0:on 780105,inlet Balancing Dampers to Emergency Ventilation Sys Fans 1-1 & 1-2 Found Closed.Cause Unknown.Dampers Returned to Balance Position & Locknut Tightened | /03L-0:on 780105,inlet Balancing Dampers to Emergency Ventilation Sys Fans 1-1 & 1-2 Found Closed.Cause Unknown.Dampers Returned to Balance Position & Locknut Tightened | | | 05000346/LER-1978-005-03, /03L-0:on 780106,auxiliary Feed Pump Turbine 1-1 Speed Control Lost & Declared Inoperable.Caused by Short Circuits & Blown Fuses Due to Design Deficiency.Higher Current Rated Relays Installed & Circuit Modified | /03L-0:on 780106,auxiliary Feed Pump Turbine 1-1 Speed Control Lost & Declared Inoperable.Caused by Short Circuits & Blown Fuses Due to Design Deficiency.Higher Current Rated Relays Installed & Circuit Modified | | | 05000346/LER-1978-005, Forwards LER 78-005/03L-0 | Forwards LER 78-005/03L-0 | | | 05000346/LER-1978-006-03, /03L-0:on 780107,computer Alarm Indicated That Steam & Feedwater Rupture Control Sys Steam Generator to Feedwater Differential Pressure Channel 1 Had Tripped.Caused by Component Failure.Input Buffer 1-3 in Channel 1 Replaced | /03L-0:on 780107,computer Alarm Indicated That Steam & Feedwater Rupture Control Sys Steam Generator to Feedwater Differential Pressure Channel 1 Had Tripped.Caused by Component Failure.Input Buffer 1-3 in Channel 1 Replaced | | | 05000346/LER-1978-006, Forwards LER 78-006/03L-0 | Forwards LER 78-006/03L-0 | | | 05000346/LER-1978-007-03, /03L-0:on 780109,during Monthly Surveillance Test ST 5081.01,diesel Generator 1-1 Tripped on High Crankcase Pressure.Caused by Dirty Crankcase Vent Oil Collector.Vent Oil Collector Disassembled & Cleaned | /03L-0:on 780109,during Monthly Surveillance Test ST 5081.01,diesel Generator 1-1 Tripped on High Crankcase Pressure.Caused by Dirty Crankcase Vent Oil Collector.Vent Oil Collector Disassembled & Cleaned | | | 05000346/LER-1978-007, Forwards LER 78-007/03L-0 | Forwards LER 78-007/03L-0 | | | 05000346/LER-1978-008-03, /03L-0:on 780112,both Containment Spray Pumps Found Inoperable.Caused by Personnel Error.Spray Pump Circuit Breakers re-energized | /03L-0:on 780112,both Containment Spray Pumps Found Inoperable.Caused by Personnel Error.Spray Pump Circuit Breakers re-energized | | | 05000346/LER-1978-008, Forwards LER 78-008/03L-0 | Forwards LER 78-008/03L-0 | | | 05000346/LER-1978-009-03, /03L-0:on 780112,component Cooling Water Heat Exchanger 1-1 Outlet Isolation Valve SW 1424 Declared Inoperable.Caused by Component Failure.Solenoid Valve in Control Scheme Found Burned Out.Unit Removed | /03L-0:on 780112,component Cooling Water Heat Exchanger 1-1 Outlet Isolation Valve SW 1424 Declared Inoperable.Caused by Component Failure.Solenoid Valve in Control Scheme Found Burned Out.Unit Removed | | | 05000346/LER-1978-009, Forwards LER 78-009/03L-0 | Forwards LER 78-009/03L-0 | | | 05000346/LER-1978-010-03, /03L-0:on 780115, Reactor Coolant Pump Monitor on Channel 1 Found Out of Tolerance & Reactor Protection Sys Declared Inoperable.Caused by Defective Module.New Module Calibr & Installed | /03L-0:on 780115, Reactor Coolant Pump Monitor on Channel 1 Found Out of Tolerance & Reactor Protection Sys Declared Inoperable.Caused by Defective Module.New Module Calibr & Installed | | | 05000346/LER-1978-010, Forwards LER 78-010/O3L-0 | Forwards LER 78-010/O3L-0 | | | 05000346/LER-1978-011, Forwards LER 78-011/03L-0 | Forwards LER 78-011/03L-0 | | | 05000346/LER-1978-011-03, /03L-0:on 780116,during Surveillance Test,Decay Heat Pump 1-1 Failed to Start.Caused by Fuses in Breaker for Decay Heat Motor Failing to Make Proper Contact.Control Power Fuese Pulled & Reinserted.Pump Returned to Svc | /03L-0:on 780116,during Surveillance Test,Decay Heat Pump 1-1 Failed to Start.Caused by Fuses in Breaker for Decay Heat Motor Failing to Make Proper Contact.Control Power Fuese Pulled & Reinserted.Pump Returned to Svc | | | 05000346/LER-1978-012, Forwards LER 78-012/03L-0 | Forwards LER 78-012/03L-0 | | | 05000346/LER-1978-012-03, /03L-0:on 780124,personnel Airlock Failed Leak Rate Test.Caused by Loose Shaft Seal Due to Routine Use of Personnel & Escape Lock (Exit/Entry to Containment).Shaft Seals Tightened to Prevent Excessive Leakage | /03L-0:on 780124,personnel Airlock Failed Leak Rate Test.Caused by Loose Shaft Seal Due to Routine Use of Personnel & Escape Lock (Exit/Entry to Containment).Shaft Seals Tightened to Prevent Excessive Leakage | | | 05000346/LER-1978-013-03, /03L-0:780119,Cell 32 in Station Battery 1N Electrolyte Specific Gravity Decreased 0.003 Greater than Allowed by Tech Spec 3.8.2.3.Caused by Electrolyte Stratification Due to Low Battery Loading | /03L-0:780119,Cell 32 in Station Battery 1N Electrolyte Specific Gravity Decreased 0.003 Greater than Allowed by Tech Spec 3.8.2.3.Caused by Electrolyte Stratification Due to Low Battery Loading | | | 05000346/LER-1978-013, Forwards LER 78-013/03L-0 | Forwards LER 78-013/03L-0 | | | 05000346/LER-1978-014, Forwards LER 78-014/03L-0 | Forwards LER 78-014/03L-0 | | | 05000346/LER-1978-014-03, /03L-0:on 780123,quandrant Power Tilt in Excess of Steady State & Transient Limits Indicated by Unit Process Computer.Caused by Detector Inadvertently Left Off Scan After Testing.Test Procedure Being Modified | /03L-0:on 780123,quandrant Power Tilt in Excess of Steady State & Transient Limits Indicated by Unit Process Computer.Caused by Detector Inadvertently Left Off Scan After Testing.Test Procedure Being Modified | | | 05000346/LER-1978-015, Forwards LER 78-015/03L-0 | Forwards LER 78-015/03L-0 | | | 05000346/LER-1978-015-03, /03L-0:on 780131,feedwater Steam Generator 1 Channel 2 Pressure Differential Switch Did Not Actuate at Desired Setpoint During Surveillance Test.Caused by Pressure Differential Switch Out of Tolerance | /03L-0:on 780131,feedwater Steam Generator 1 Channel 2 Pressure Differential Switch Did Not Actuate at Desired Setpoint During Surveillance Test.Caused by Pressure Differential Switch Out of Tolerance | | | 05000346/LER-1978-016-03, /03L-1:on 780202,absolute Position Indicator for Group 5,Rod 12,declared Inoperable.Caused by Component Failure in Penetration Area.Containment Conductors Connected to Spare Penetration Connector | /03L-1:on 780202,absolute Position Indicator for Group 5,Rod 12,declared Inoperable.Caused by Component Failure in Penetration Area.Containment Conductors Connected to Spare Penetration Connector | | | 05000346/LER-1978-016, Forwards LER 78-016/03L-1,LER 78-021/03L-1,LER 78-100/03L-1, LER 78-034-03L-1 & LER 78-024/03L-1 | Forwards LER 78-016/03L-1,LER 78-021/03L-1,LER 78-100/03L-1, LER 78-034-03L-1 & LER 78-024/03L-1 | | | 05000346/LER-1978-017, Forwards LER 78-017/03L-0 | Forwards LER 78-017/03L-0 | | | 05000346/LER-1978-017-03, /03L-0:on 780126,all Meteorological Channels Became Inoperable During Blizzard.Caused by Instrumentation Power Loss Due to Tripped Breaker at Meteorological Tower. Breaker Reset on 780128 | /03L-0:on 780126,all Meteorological Channels Became Inoperable During Blizzard.Caused by Instrumentation Power Loss Due to Tripped Breaker at Meteorological Tower. Breaker Reset on 780128 | | | 05000346/LER-1978-018-03, /03L-0:on 780208,diesel Generator 1-1 Making Unusual Noises During Monthly Test.Unusual Noise Traced to Turbocharger.Exact Cause Undetermined.Turbocharger Replaced & Diesel Generator Monthly Test Completed | /03L-0:on 780208,diesel Generator 1-1 Making Unusual Noises During Monthly Test.Unusual Noise Traced to Turbocharger.Exact Cause Undetermined.Turbocharger Replaced & Diesel Generator Monthly Test Completed | | | 05000346/LER-1978-018, Forwards LER 78-018/03L-0 | Forwards LER 78-018/03L-0 | | | 05000346/LER-1978-019-03, /03L-1:on 780210,decay Heat Cooler Outlet Valve DH14A & DH14B Mechanical Stops Found Incorrectly Opened. Caused by Personnel Incorrectly Resetting Stops After Previous Work Completion.Stops Tagged & Records Marked | /03L-1:on 780210,decay Heat Cooler Outlet Valve DH14A & DH14B Mechanical Stops Found Incorrectly Opened. Caused by Personnel Incorrectly Resetting Stops After Previous Work Completion.Stops Tagged & Records Marked | | | 05000346/LER-1978-020, Forwards LER 78-020/03L-0 | Forwards LER 78-020/03L-0 | | | 05000346/LER-1978-020-03, /03L-0:on 780210,reactor Protection Sys Channel 3 Hot Leg Temp String TI-RC3B4 Declared Inoperable.Caused by Loose Wire Connection.Loose Terminal at Temp Element Tightened,Rendering TI-RC3B4 Operable | /03L-0:on 780210,reactor Protection Sys Channel 3 Hot Leg Temp String TI-RC3B4 Declared Inoperable.Caused by Loose Wire Connection.Loose Terminal at Temp Element Tightened,Rendering TI-RC3B4 Operable | | | 05000346/LER-1978-021-03, /03L-1:on 780220,absolute Position Indicator for Control Rod 12 of Group 5 Declared Inoperable.Caused by Component Failure in Penetration Area.Conductors Connected W/Spare Penetration Connectors | /03L-1:on 780220,absolute Position Indicator for Control Rod 12 of Group 5 Declared Inoperable.Caused by Component Failure in Penetration Area.Conductors Connected W/Spare Penetration Connectors | | | 05000346/LER-1978-022-03, /03L-0:on 780223,flow Transmitter FTRC1A3 Found Inoperable.Caused by Defective Flow Transmitter Amplifier. Amplifier Replaced & Flow Transmitter FTRC1A3 Returned to Svc on 780226 | /03L-0:on 780223,flow Transmitter FTRC1A3 Found Inoperable.Caused by Defective Flow Transmitter Amplifier. Amplifier Replaced & Flow Transmitter FTRC1A3 Returned to Svc on 780226 | | | 05000346/LER-1978-022, Forwards LER 78-022/03L-0 | Forwards LER 78-022/03L-0 | | | 05000346/LER-1978-023-03, /03L-0:on 780224,temp Indication for Reactor Protection Sys Channel 2 Spiked Tripping Channel & Shut Down Reactor.Caused by Faulty Connector Due to Dirt on Contacts. Channel 2 Temp String Modules Removed & Connectors Cleaned | /03L-0:on 780224,temp Indication for Reactor Protection Sys Channel 2 Spiked Tripping Channel & Shut Down Reactor.Caused by Faulty Connector Due to Dirt on Contacts. Channel 2 Temp String Modules Removed & Connectors Cleaned | | | 05000346/LER-1978-023, Forwards LER 78-023/03L-0 | Forwards LER 78-023/03L-0 | | | 05000346/LER-1978-024-03, /03L-1:on 780228,MSIV MS-101 Rendered Inoperable to Allow Maint Personnel to Remove Raised Metal on Two of Four Spring Guide Tubes.Cause of Raised Metal Unknown.Metal Filed Down,Valve Closing Time Adjusted & Valve Tested | /03L-1:on 780228,MSIV MS-101 Rendered Inoperable to Allow Maint Personnel to Remove Raised Metal on Two of Four Spring Guide Tubes.Cause of Raised Metal Unknown.Metal Filed Down,Valve Closing Time Adjusted & Valve Tested | | | 05000346/LER-1978-025-03, /03L-0:on 780304,RCS Leakage Found Greater than 1 Gallon Per Minute.Leakage Cause Undetermined.Leakages Processed Through Normal Containment Sump.Unidentified RCS Leakage Reduced Below 1 Gallon Per Minute in 5.5-h | /03L-0:on 780304,RCS Leakage Found Greater than 1 Gallon Per Minute.Leakage Cause Undetermined.Leakages Processed Through Normal Containment Sump.Unidentified RCS Leakage Reduced Below 1 Gallon Per Minute in 5.5-h | | | 05000346/LER-1978-025, Forwards LER 78-025/03L-0 | Forwards LER 78-025/03L-0 | | | 05000346/LER-1978-026, Forwards LER 78-026/03L-0 | Forwards LER 78-026/03L-0 | | | 05000346/LER-1978-026-03, /03L-0:on 780309,radiation Monitor Re 5029 Found Inoperable Due to Low Sample flow.12 Previous Radiation Monitor Inoperabilities Not Reported.Caused by Pump Motor Bearing Seizure Due to High Ambient Temp | /03L-0:on 780309,radiation Monitor Re 5029 Found Inoperable Due to Low Sample flow.12 Previous Radiation Monitor Inoperabilities Not Reported.Caused by Pump Motor Bearing Seizure Due to High Ambient Temp | | | 05000346/LER-1978-027, Forwards LER 78-027/03L-0 | Forwards LER 78-027/03L-0 | | | 05000346/LER-1978-027-03, /03L-0:on 780316,stop Valve AF3870 Failed to Open During Testing.Caused by High Differential Pressure Due to Check Valve AF39 & AF72 Leakage.Motor Operator Initially Not Adjusted for This Pressure,Causing Operator to Torque | /03L-0:on 780316,stop Valve AF3870 Failed to Open During Testing.Caused by High Differential Pressure Due to Check Valve AF39 & AF72 Leakage.Motor Operator Initially Not Adjusted for This Pressure,Causing Operator to Torque Out | | | 05000346/LER-1978-028-03, /03L-0:on 780318,channel 1 Steam Generator 1-1 Declared Inoperable.Caused by Water in Level Transmitter SP09B8 Connecting Box Due to Steam Leak.Connection Box Cleaned & Dried.Waterproof Fitting Will Be Installed | /03L-0:on 780318,channel 1 Steam Generator 1-1 Declared Inoperable.Caused by Water in Level Transmitter SP09B8 Connecting Box Due to Steam Leak.Connection Box Cleaned & Dried.Waterproof Fitting Will Be Installed | |
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