05000334/LER-1980-098-03, /03L-0:on 801122,main Steam Flow Indicator FI-MS-484 Was Pegged Low.Caused by Transmitter Bypass Valve FT-MS-484 Not Being Fully Closed.Valve Closed

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/03L-0:on 801122,main Steam Flow Indicator FI-MS-484 Was Pegged Low.Caused by Transmitter Bypass Valve FT-MS-484 Not Being Fully Closed.Valve Closed
ML19340D482
Person / Time
Site: Beaver Valley
Issue date: 12/18/1980
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19340D478 List:
References
LER-80-098-03L, LER-80-98-3L, NUDOCS 8012300670
Download: ML19340D482 (2)


LER-1980-098, /03L-0:on 801122,main Steam Flow Indicator FI-MS-484 Was Pegged Low.Caused by Transmitter Bypass Valve FT-MS-484 Not Being Fully Closed.Valve Closed
Event date:
Report date:
3341980098R03 - NRC Website

text

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NRC FCCM 364 U. S. NUCLE A3 fiEGULATO3Y COMMISSION (7-771

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8 40 63 QoCKET NUMgER the 69 EVENT DATE 74 il REPORT DATE 80 EVENTDESCRIPTION AND PROSASLE CONSEQUENCES @

g l At 1525 hours0.0177 days <br />0.424 hours <br />0.00252 weeks <br />5.802625e-4 months <br /> with the reactor operating at about 30 percent power, oporator I

surveillance of the board revealed that main steam flow indicator FI-MS-484 was l

gl [aj.;l pegged low.

Actual steam flow was about 1 million ihm/hr. All associated bistable l 1 o 15 I I switches were placed in " trip" as required by Technical Specifications 3.3.1.1 and l lo is ] I 3.3.1.2.

The health and safety of the ceneral public was not jeopardized since the l lo 7l l redu idan:. channel was operable and capable of actuation.

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23 34 05 36 37 40 44 42 43 4A a7 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l i l o l l The transmitter, FT-MS-484, bypass valve was not fully closed. The valve was fully i 12 iiiI closed and the channel checked for proper indication.

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Attachment To LER 80-98/03L Beaver Valley Power Station Duc,uesne Light Company Docket No. 50-334 No further information is available or needed to satisfy the reporting requirement l

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