ML19341A428

From kanterella
Revision as of 17:33, 24 December 2024 by StriderTol (talk | contribs) (StriderTol Bot change)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
Interim Deficiency Rept,Originally Reported on 801217,re Breakdowns in Mfg,Cleaning & Insp Processes on Shutdown Heat Exchangers.Caused by Contamination of Tube Side Matl Surfaces.Exchangers Returned to Supplier for Exam & Repair
ML19341A428
Person / Time
Site: Cherokee Duke Energy icon.png
Issue date: 01/15/1981
From: Dail L
DUKE POWER CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
10CFR-050.55E, 10CFR-50.55E, IE-81-01-5PS-49, IE-81-1-5PS-49, NUDOCS 8101230502
Download: ML19341A428 (2)


Text

.

i DUKE POWER COMPANY

.5,'

GENERAL OFFICES

'"""ff[.".o#!

422 SOUTH CHURCH STREE!

CHARLO'l'I'E. N. C. 28242

~

~.

l s'anuary 15, d81 Mr. J. P. O'Reilly, Director U. S. Nuclear Regulatory Commission 101 Marietta Street, Suite 3100 Atlanta, Georgia 30303 Re:

Cherokee Nuclear Station, Unit 1 Docket No. 50-491 IE 81/01-5PS-491 NSSS-Shutdown Heat Exchanger Duke Files: CK-1412.ll-1

Dear Mr. O'Reilly:

Attached is Duke's interim report on the referenced 10CFR50.55(e) reportable item.

Another report will be submitted by July 15, 1981 Initial notification was made by telephone to Mr. Rausch of your office on December 17, 1980.-

Very truly yours, f

Li C. Dail, Vice-President Design Engineering Department JEB/pam Attachment cc: Director of Inspection & Enforcement U.S. Nuclear Regulatory Commission Washington, DC 20555 gen

.5

/f l

810128 05cas

o*

O DUKE POWER C0.

CHEROKEE NUCLEAR STATION Report Number:

IE 81/01-5PS-491 Report Date: January 15, 1981 Facility: Cherokee Nuclear Station - Unit #1 Identification of Deficiency:

Apparent breakdowns in manufacturing, cleaning, and inspection processes on Shutdown Heat Exchangers (SDHX's).

Description of Deficiency:

On December 17,196., Mr. R. E. Miller and Mr. W. H. Bradley informed Mr. John Rausch, NRC of potential deficiencies in the Shutdown Heat Exchangers, supplied by Combustion Engineering as part of the NSSS contract, on the following basis:

1.

Due to problems encountered on the WPPSS Unit #3 SDHX, and since the Duke SDHX's were manufactured by the' same vendor (Ametek), CE advised Duke that these heat exchangers were suspect.

2.

The Duke Unit #1 SDHX's were preliminarily inspected at the site, and were found to have problems with the stainless steel cladding and contamination of tube side material surfaces.

Analysis of Safety Implications:

The SDHX's provide a safety related function in both the containment spray and shutdown cooling modes of operation of the Containment Spray System.

The containment spray mode is designed to remove heat from the containment atmosphere in the event of a LOCA or MSLB inside the containment. The SDHX cools the containment s ray water as it recirculates from the containment recirculation sump to the spray nozzles.

Loss of one SDHX would delete redundancy in the containment spray mode, while the simultaneous loss of both SDHX's could compromise this mode of heat removal.

In the shutdown cooling mode the SDHX's remove heat during both cooldown and shutdown. During cooldown they remove core decay heat, Reactor Coolant System sensible heat, and safeguards pump heat; during shutdown they remove decay heat, containment spray pump heat, and low pressure safety injection pump heat.

Loss of one SDHX in the shutdown cooling mode would delete redundancy and increase the normal cooldown time for plant shutdown, whi?e the simultaneous loss of both SDHX's could compromise this mode of heat removal.

Corrective Actions:

Duke will remove the Unit l A and IB SDHX's from the Reactor Building, and return them to the original supplier for examination and repair.

Specific corrective actions will be determined over the next 6-12 months. Similar problems will be precluded on Cherokee, Unit 2 and subsequent units not yet under construction.

<