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LER-1980-122, /03L-0:on 800811,during Steady State Operation at Full Power,While Performing HNP-2-3001,reactor High Pressure Instrument Test,Switch 2B21-N023C Actuated at 1,068 Psig. Caused by Setpoint Drift.Switch Recalibr |
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| 3661980122R03 - NRC Website |
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09.6 NLCAH REGULATCnY COP.211SSIOfJ (7 77)
LICENSEE EVENT REPORT coriinot ctocx: 1 I
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(PLE ASE PnifJT on TYPC ALL REOUtHED INFOnf.1ATION)
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[ o ; 3 ].l Reactor liigh Pressure Instrument Test, switch 2021-N023C was found to l
ggj [ actuate at 1068 psig inc.
The Tech Spec limit, Table 4.3.1-1, item 3, l
is $1015 +15.36 psig hccd correction.
No significant occurrences took l
gj l [idTi l i place due to this event. This is not a repetitive event.
Redundant j
jo [7] l switches 2821-N023A, B and D were all operable. There were no effects l
g) l upon public health and safety due to this event.
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lim switch m recali!:ratr:d I
0-]Tl L_cer HUP-2-5?79. Barksdele Prc ssure Swi tch Calibratjm_Jt was functinrally.
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[i l ci [ _ tested sucem. full y.
Unit I_also u;nc 'his J r suitch.
A generic re-l [TITl [_ view revealnd no inhorent kroblem.
The unit is inw in full comftliarn
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and nn furthor repAr_ ting is reguired.
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flARRATIVE REPORT Georgia Poucr Company Plant E.1. lla tch Baxley, Georgia 31513 Reportable Occurrence Report !!o. 50-356/1930-122.
During steady state operation at 100% power and perforraing H1P-2-3001, Reactor liigh Pressure Instrument. Test, reactor pressure switch 2821-k023C was found to actuate at 1068 psig inc.
The Tech Spec limit, Table 4.3.1-1,.
item 3 is $1045 psig increasing -115.36 psig head correction.
The cause of this event was switch setpoint dri f t.
The switch, a Barksdale
!!odel B2T-1112SS, uas recalibrated par H!1p-2-5279, Sarksdale Pressure Switch Calibration.
It was then functionally tested euccessfully per !!:1p-2-3001.
ilo significant occurreacts took place as a result of this event.
This is not a repetitive event on Unit II.
Redundant switches 2321-!!D23A, C and D were all operable.
Unit I also uses this type switch in this application. However e generic review re/ealtd no inherent problet.a.
There were no effccts upon public health and safety due to this event.
The unit is now in full cocapliance with thc recciire;.nnts end rio further reportinD is required.
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| 05000321/LER-1980-001-01, /01T-0:on 800103,while Performing Maint on RHR LPCI Injection Valve,Clevis Pin Found Missing from Strut on Drywell Penetration Restraint.Caused by Improper Installation.New Clevis Pin Installed | /01T-0:on 800103,while Performing Maint on RHR LPCI Injection Valve,Clevis Pin Found Missing from Strut on Drywell Penetration Restraint.Caused by Improper Installation.New Clevis Pin Installed | | | 05000366/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000366/LER-1980-001-03, /03L-0:on 800102,while Performing Narrow Range Torus Water Level Functional Test & Calibr,Level Transmitter 2T48-N021B Found Out of Tolerance.Caused by Range Drift. Transmitter Recalibr & Returned to Svc | /03L-0:on 800102,while Performing Narrow Range Torus Water Level Functional Test & Calibr,Level Transmitter 2T48-N021B Found Out of Tolerance.Caused by Range Drift. Transmitter Recalibr & Returned to Svc | | | 05000321/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000321/LER-1980-002-03, /03L-0:on 800112,while Performing HNP-1-3655,fan lT46-C001B Would Not Meet Flow Requirements Per Tech Specs. Ten Days Later,While Venting Drywell Per HNP-1-1500,flow Did Not Meet Tech Specs.Equipment Recalibr | /03L-0:on 800112,while Performing HNP-1-3655,fan lT46-C001B Would Not Meet Flow Requirements Per Tech Specs. Ten Days Later,While Venting Drywell Per HNP-1-1500,flow Did Not Meet Tech Specs.Equipment Recalibr | | | 05000321/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000366/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000366/LER-1980-002-01, /01T-0:on 800128,during Cold Shutdown,Ae Notified Util That Single Mode Failure Existed for Torus Gravity Fill Isolation Valve 2G51-F013.Caused by Design Deficiency. Standing Order Issued | /01T-0:on 800128,during Cold Shutdown,Ae Notified Util That Single Mode Failure Existed for Torus Gravity Fill Isolation Valve 2G51-F013.Caused by Design Deficiency. Standing Order Issued | | | 05000366/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000366/LER-1980-003-03, /03L-0:on 800117,while Applying Equalizing Charge to 125/250-volt Dc Station Svc Batteries,Hpci Automatic Flow Control Power Inverter Tripped.Caused by Instrument Drift. Instrument Recalibr Satisfactorily | /03L-0:on 800117,while Applying Equalizing Charge to 125/250-volt Dc Station Svc Batteries,Hpci Automatic Flow Control Power Inverter Tripped.Caused by Instrument Drift. Instrument Recalibr Satisfactorily | | | 05000321/LER-1980-003-03, While Performing RHR Valve Operability Procedure,Outboard Shutdown Cooling Isolation Valve F008 Opened in 25.8-S.Caused by Normal Wear & Human Reaction Time.Valve Operator Adjusted | While Performing RHR Valve Operability Procedure,Outboard Shutdown Cooling Isolation Valve F008 Opened in 25.8-S.Caused by Normal Wear & Human Reaction Time.Valve Operator Adjusted | | | 05000321/LER-1980-003, Forwards Revised LER 80-003/03X-1 | Forwards Revised LER 80-003/03X-1 | | | 05000321/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000321/LER-1980-004-03, /03L-0:on 800106,during Startup Mode,Main Steam Line Inboard Isolation Drain Valve Failed in mid-position. Caused by Failure of Valve Motor Winding.Motor Replaced & Valve Returned to Operable Status | /03L-0:on 800106,during Startup Mode,Main Steam Line Inboard Isolation Drain Valve Failed in mid-position. Caused by Failure of Valve Motor Winding.Motor Replaced & Valve Returned to Operable Status | | | 05000366/LER-1980-004-03, /03L-0:on 800118,during Steady State Power Operation Hydrogen Recombiner Inlet Valve 2T49-F003A Did Not Open.Caused by a Failed Torque Switch.Sys Returned to Operation After Switch Was Replaced | /03L-0:on 800118,during Steady State Power Operation Hydrogen Recombiner Inlet Valve 2T49-F003A Did Not Open.Caused by a Failed Torque Switch.Sys Returned to Operation After Switch Was Replaced | | | 05000366/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000321/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000321/LER-1980-005-03, /03L-0:on 800109,w/reactor Mode Switch in Run Mode,Discovered That Surveillance Procedure HNP-1-3007, Turbine Control Valve Fast Closure,Was Not Performed in Grace Period.Caused by Personnel Error | /03L-0:on 800109,w/reactor Mode Switch in Run Mode,Discovered That Surveillance Procedure HNP-1-3007, Turbine Control Valve Fast Closure,Was Not Performed in Grace Period.Caused by Personnel Error | | | 05000366/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000366/LER-1980-005-03, /03L-0:on 800119,during Power Operation,Tech Specs 4.8.1.1.1.a & 4.8.1.1.2a4 for Electrical Power Sources Were Not Performed within 1-h.Caused by Personnel Misinterpretation of Tech Spec Requirements | /03L-0:on 800119,during Power Operation,Tech Specs 4.8.1.1.1.a & 4.8.1.1.2a4 for Electrical Power Sources Were Not Performed within 1-h.Caused by Personnel Misinterpretation of Tech Spec Requirements | | | 05000321/LER-1980-006-03, /03L-0:on 800113,one Standby Gas Treatment Sys Rendered Inoperable W/Both Units in Power Operation.Unit Not Proven Operable within Required 4-h.Caused by Inability to Prove Filter Train Operable within 4-h | /03L-0:on 800113,one Standby Gas Treatment Sys Rendered Inoperable W/Both Units in Power Operation.Unit Not Proven Operable within Required 4-h.Caused by Inability to Prove Filter Train Operable within 4-h | | | 05000321/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000321/LER-1980-007-03, /03L-0:on 800114,while Testing Standby Svc Water Pump,Pump Would Not Meet Criteria.Caused by Disengagement of Pump First Stage Impeller Lock Collet.Lock Collet Replaced & Pump Reinstalled | /03L-0:on 800114,while Testing Standby Svc Water Pump,Pump Would Not Meet Criteria.Caused by Disengagement of Pump First Stage Impeller Lock Collet.Lock Collet Replaced & Pump Reinstalled | | | 05000321/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000366/LER-1980-007-01, /01T-0:on 800130,while Performing High Drywell Pressure Instrument (Reactor Protection Sys) Functional Test & Calibr,Instruments 2C71-N002A,B & D Exceeded Tech Specs.Caused by Instrument Drift | /01T-0:on 800130,while Performing High Drywell Pressure Instrument (Reactor Protection Sys) Functional Test & Calibr,Instruments 2C71-N002A,B & D Exceeded Tech Specs.Caused by Instrument Drift | | | 05000366/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000366/LER-1980-008-03, While Increasing Reactor Power by Rod Withdrawal,Operator Noticed Rod Select Matrix Backlighted & Rod Sequence Control Sys Not Initiating Rod Blocks Properly.Caused by Design Change | While Increasing Reactor Power by Rod Withdrawal,Operator Noticed Rod Select Matrix Backlighted & Rod Sequence Control Sys Not Initiating Rod Blocks Properly.Caused by Design Change | | | 05000366/LER-1980-008, Forwards LER 80-008/03L-1 | Forwards LER 80-008/03L-1 | | | 05000321/LER-1980-008-03, /03L-0:on 800115,during Steady State Power Operation,Secondary Containment Integrity Violated When Personnel Opened 164-ft Elevation Reactor Bldg & Turbine Bldg Airlock Doors Simultaneously.Procedure Revised | /03L-0:on 800115,during Steady State Power Operation,Secondary Containment Integrity Violated When Personnel Opened 164-ft Elevation Reactor Bldg & Turbine Bldg Airlock Doors Simultaneously.Procedure Revised | | | 05000321/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000366/LER-1980-009-03, /03L-0:on 800130,while Performing Procedure HNP-2-33-3,HPCI Min Flow Valve 2E41-F012 Failed to Close. Caused by Sticking Switch Contacts on Flow Switch 2E41-N006. Switch Contacts Cleaned & Procedure HNP-2-3303 Performed | /03L-0:on 800130,while Performing Procedure HNP-2-33-3,HPCI Min Flow Valve 2E41-F012 Failed to Close. Caused by Sticking Switch Contacts on Flow Switch 2E41-N006. Switch Contacts Cleaned & Procedure HNP-2-3303 Performed | | | 05000321/LER-1980-009-03, /03L-0:on 800118,during Normal Operation,Drywell/ Torus Temp Recorder 1T47-R611 Found Stamping Erratically, Making Drywall & Torus Air Temps & Water Temp Difficult to Ascertain.Caused by Failure of Microswitch.Switch Replace | /03L-0:on 800118,during Normal Operation,Drywell/ Torus Temp Recorder 1T47-R611 Found Stamping Erratically, Making Drywall & Torus Air Temps & Water Temp Difficult to Ascertain.Caused by Failure of Microswitch.Switch Replaced | | | 05000366/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000321/LER-1980-010-03, /03L-0:on 800118,during Normal Operation While Performing Standby Liquid Control Pump Operability Test & Relief Valve Test,Pump a Discharge Relief Valve 1C41-F029A Operated at 1,225 Psig.Caused by Setpoint Drift.Valve Reset | /03L-0:on 800118,during Normal Operation While Performing Standby Liquid Control Pump Operability Test & Relief Valve Test,Pump a Discharge Relief Valve 1C41-F029A Operated at 1,225 Psig.Caused by Setpoint Drift.Valve Reset | | | 05000321/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000366/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000366/LER-1980-010-03, /03L-0:on 800131,during Reactor Startup,At 58% Power,Max Total Peaking Factor Was Calculated at 3.0 Compared to Design Value of 2.38.Caused by Lower than Normal Xenon Distribution During Startup | /03L-0:on 800131,during Reactor Startup,At 58% Power,Max Total Peaking Factor Was Calculated at 3.0 Compared to Design Value of 2.38.Caused by Lower than Normal Xenon Distribution During Startup | | | 05000321/LER-1980-011-03, /03L-0:on 800120,while at Steady State Power, torus-to-drywell Differential Pressure recorder,LT48-R631B Had Low Reading.Cause Not Stated | /03L-0:on 800120,while at Steady State Power, torus-to-drywell Differential Pressure recorder,LT48-R631B Had Low Reading.Cause Not Stated | | | 05000366/LER-1980-011-03, /03L-0:on 800202,while Performing Reactor Core Isolation Cooling Shutdown Flow Test,Power Inverter for Remote Flow Control Loop Found to Be Tripped.Caused by Defective Input Filter Capacitors | /03L-0:on 800202,while Performing Reactor Core Isolation Cooling Shutdown Flow Test,Power Inverter for Remote Flow Control Loop Found to Be Tripped.Caused by Defective Input Filter Capacitors | | | 05000321/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000366/LER-1980-012-03, /03L-0:on 800214,while at Full Power,Rhr & Plant Svc Water Min Flow Line Found to Be Inadequately Supported. Caused by Design Deficiency.Design Change Request & Maint Request Implemented to Add Supports | /03L-0:on 800214,while at Full Power,Rhr & Plant Svc Water Min Flow Line Found to Be Inadequately Supported. Caused by Design Deficiency.Design Change Request & Maint Request Implemented to Add Supports | | | 05000321/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000366/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000321/LER-1980-012-03, /03L-0:on 800122,while Reactor Core Isolation Cooling Sys Was Tagged Out for Maint,Hpci Was Found Inoperable,Requiring Orderly Shutdown.Caused by Leak in Line to HPCI Booster Pump Discharged Pressure Gauge | /03L-0:on 800122,while Reactor Core Isolation Cooling Sys Was Tagged Out for Maint,Hpci Was Found Inoperable,Requiring Orderly Shutdown.Caused by Leak in Line to HPCI Booster Pump Discharged Pressure Gauge | | | 05000321/LER-1980-013, Forwards Updated LER 80-013/03X-1 | Forwards Updated LER 80-013/03X-1 | | | 05000321/LER-1980-013-03, Reactor Recirculation Pump a Tripped Causing Power Reduction.Caused by Electrical Short Circuit Due to Steam Leak in Drywell.Terminal Board Replaced & Tested | Reactor Recirculation Pump a Tripped Causing Power Reduction.Caused by Electrical Short Circuit Due to Steam Leak in Drywell.Terminal Board Replaced & Tested | | | 05000366/LER-1980-013-03, /03L-0:on 800203,while Maint Was Performed on 2082-K002 Static Inverter,Emergency Control Transfer Switch Was Placed in Emergency Position.Reactor Core Isolation Cooling Was Rendered Inoperable.Caused by Personnel Error | /03L-0:on 800203,while Maint Was Performed on 2082-K002 Static Inverter,Emergency Control Transfer Switch Was Placed in Emergency Position.Reactor Core Isolation Cooling Was Rendered Inoperable.Caused by Personnel Error | | | 05000366/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000366/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000366/LER-1980-014-03, /03L-0:on 800204,while Performing HNP-2-3054, Average Power Range Monitor C Failed.Caused by Instrument Drift.Instrument Adjusted Per Procedure & Returned to Svc | /03L-0:on 800204,while Performing HNP-2-3054, Average Power Range Monitor C Failed.Caused by Instrument Drift.Instrument Adjusted Per Procedure & Returned to Svc | |
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