05000219/LER-1980-049-01, /01T-0:on 801105,when Isolation Condenser B Was Removed from Svc to Repair Steam Leak,Vent Isolation Valves V-14-1 & V-14-19 Apparently Failed to Close.Cause Undertermined.Stem Packing Replaced & Tested

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/01T-0:on 801105,when Isolation Condenser B Was Removed from Svc to Repair Steam Leak,Vent Isolation Valves V-14-1 & V-14-19 Apparently Failed to Close.Cause Undertermined.Stem Packing Replaced & Tested
ML19345A982
Person / Time
Site: Oyster Creek
Issue date: 11/20/1980
From: Crosby P
JERSEY CENTRAL POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19345A981 List:
References
LER-80-049-01T, LER-80-49-1T, NUDOCS 8011250534
Download: ML19345A982 (1)


LER-1980-049, /01T-0:on 801105,when Isolation Condenser B Was Removed from Svc to Repair Steam Leak,Vent Isolation Valves V-14-1 & V-14-19 Apparently Failed to Close.Cause Undertermined.Stem Packing Replaced & Tested
Event date:
Report date:
2191980049R01 - NRC Website

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io ;,; I on vent.. isolation valve V-14-19 and possible degradation of the reactor l

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ii ei; I on vent isolation valve V-14-19.

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