LER-1979-086, B Shutdown Cooling Heat Exchanger Radiation Monitor Indication Found Increased. Caused by Small Vol Tube Leak in Heat Exchanger Tube Q74. Heat Exchangers & Tubes Examined.Tube Plugged |
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| 3681979086R03 - NRC Website |
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REVISED REPORT - PREVIOUS REPORT DATE 11/12/79 NRC,ORu ss u. s. hucLE An REcuL ATonv Comm $sioes LICENSEE EVENT REPORT EXHIBIT A
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[Hi] I During Mode 6 operation, it was discovered that the "B" shutdown cooling i i
mm I (SDC) heat exchAar.aer, 2E35B. radiation monitor indication had increased. I FET711 The heat exchancer was immcdiately isolated on both the service water & I i re: ctor coolant sides.
Interpretation of the SDC activity increase as iti n s t re ated to plant conditions indicated a small volume tube leak in the heat o a g i exchanger. Activity release was analyzed to be <MPC.
There have been noi i
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CAUSE DESCR.PTION AND CORREC OVE ACTIONS 27 l
1 The "B" SDC Heat Exchanger was taken out of service & visual inspection i
. o i i i revealed that tube #074 was the leaker (an outer opricheral tuhpl.
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The tubes in Rows A & B i'nside the U-Bend & 0.130" thickness) 1 E Lwere xamined at 200 MH7 and tuhot (enntinued on attachmentd 1
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,ssu,o 8 LYJ@l Media Account. Arkansas Gazette, 10/17/79 1 ii i iiiii;iiii e
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NAME OF PREPAnER-Chris N. Shively W%MM
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8.011.280 0852-
LER 50-368/79-086 Rev. 1 Unit II in Rows C through Y (0.098" thickness) were examined at a 200 KHz test frequency.
The test instrumentation sensitivity. was adjusted to allow calibration of the test equipment to a tube standard containing known defects.
Due to the initial inspection results,100% of the tubes in each heat exchanger were examined.
Tables I & II list tubes which exhibited tube wall degradation.
Twelve tubes were plugged in 2E35A and 19 tubes were plugged in 2E358.
Five of the tubes plugged in the "B" heat exchanger were plugged for precautionary measures, as they surrounded the " leaker" (Tube 74Q).
Additional Eddy current examinations were conducted on the "A" heat exchanger for further information on the SDC condition.
The tube support plate signals received during examination are large in magnitude relative to a signal generated from a small volume defect.
To optimize the phase separation between tube flaws and support plate signals, a test frequency of 150 KHz was used.
At this frequency a defect signal will tend to distort the con-figuration of the tube support plate signal.
Further, to enhance the ability to detect flaws, an electronic device known as a signal subtraction unit was employed.
This unit subtracts a stored clean support plate signal from the distorted signal being analyzed, leaving the defect signal which can then be analyzed to determine the depth of the flaw.
Rows F through Y were inspected, because of the greater U-bend radius which allowed for probing through the bend.
No additional defects were identified.
Following the examination of 2E35B, a section of tube # 74Q containing the fracture surface and a section of tube # 32Y which contained two defect indications w'ere extracted from the heat exchanger for failure analysis. Metallurgical analysis of the presence of periodic markings, or arrest marks, on the fracture surface of 74Q with a small adjacent region of ductile fracture, indicate fatigue as the mode of final failure.
Most of the fracture surface contained little or no fractografic information because of wear damage which occurred during or after the fracture; therefore, root cause of the failure could not be established.
Tube #32Y contained three chloride stress corrosion cracks which initiated in a region of localized intergranular attack.
Transgranular cracks then begin to penetrate the tube wall and are highly branched.
The localized intergranular attack is involved in the initiation orocess of the cracks, originating from a combination of possible factors (material sensitization, presence of chlorides in cooling water, stress in tubes, and operating in a temperature range conducive to chloride stress cracking).
An engineering evaluation is being conducted to determine if tube bundle replacement using an alloy which is not susceptable to chloride stress corrosion cracking should be pursued.
Presently, the chloride levels in the cooling water are being maintained as low as practical utilizing a wet layup technique with demineralized water.
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LER 50-368/79-086 Rev. 1 TABLE I SHUTDOWN COOLING HEAT EXCHANGER 2E-35-A LINE R0W LOCATION
% DEGRADATION 63 0
5B+8 72 10 L
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20 74 N
78 70 76 N
78 55 76 N
6B 80 73 P
78 76 75 P
7T 55 75 P
7B 55 75 P
68 65 75 P
5B 55 18 Q
7T-1 20 50 Q
7T+4 30 72 Q
7B 50 74 Q
ST 55 74 0
7T 55 74 Q
6B 55 74 Q
78 55 70 S
7T 55 70 5
78 80 27 V
3T-10 27
- Line 10 Row L anomaly is 6 inches long.
12 Tubes Plugged.
Location interpretation: Number indicates the support ! starting with the tube sheet which is designated as 0 Letter is T for Top Half or B for Botton Half of bundle, and the i # is inches away from indicated support.
LER 50-368/79-086 Rev. 1 TABLE II SHUTDOWN COOLING HEAT EXCHANGER 2E-35-B LINE R0W LOCATION
% DEGRADATION 10 C
6T-8 89 18 C
6B-6 93 36 C
5B+6 92 36 C
5B+5 78 36 C
5B-5 88 68 C
ST-8 94 72 C
ST+13 70 14 E
ST-5 90 21 F
6B-13 94 29 F
4T+15 79 77 F
5B-13 95 79 F
5B-13 88 48 G
1B+1 81 10 Q
68-6 86 74 Q
8B+1 20 74 Q
7T 100 32 Y
3T+3 83 32 Y
3T+2 70 32 Y
3T-5 87 14 Tubes Plugged + 5 Tubes Surrounding 74Q
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| 05000368/LER-1979-001-03, /03L-0 on 790102:refueling Water Tank Level Indicator Failed High.Caused by Frozen Transmitter Sensing Line.Line Was Thawed & Returned to Operable Status within 20-h | /03L-0 on 790102:refueling Water Tank Level Indicator Failed High.Caused by Frozen Transmitter Sensing Line.Line Was Thawed & Returned to Operable Status within 20-h | | | 05000313/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000313/LER-1979-001-03, /03L-0 on 790112:during Mode 5 Operation,Purge Supply Flow from VSF-30B Would Not Meet Surveillance Requirements.Caused by Supply Filter VFA-20B Collapsing from Water Restricting Air Flow.Filter Changed | /03L-0 on 790112:during Mode 5 Operation,Purge Supply Flow from VSF-30B Would Not Meet Surveillance Requirements.Caused by Supply Filter VFA-20B Collapsing from Water Restricting Air Flow.Filter Changed | | | 05000313/LER-1979-002-01, /01T-0 on 790205:during Startup,Nuclear Instrumentation Was Not Calibr as Required by Tech Spec 4.1, Table 4.1-1.Caused by Personnel Error.Occurrence Discussed W/Shift | /01T-0 on 790205:during Startup,Nuclear Instrumentation Was Not Calibr as Required by Tech Spec 4.1, Table 4.1-1.Caused by Personnel Error.Occurrence Discussed W/Shift | | | 05000313/LER-1979-002, Forwards LER 79-002/01T-0 | Forwards LER 79-002/01T-0 | | | 05000368/LER-1979-002-03, /03L-0 on 790103:refueling Water Level Transmitter Refroze.Caused by Frozen Transmitter Sensing Line.Addl Insulation & Heat Lamps Added to Sensing Lines & Transmitter Cabinets | /03L-0 on 790103:refueling Water Level Transmitter Refroze.Caused by Frozen Transmitter Sensing Line.Addl Insulation & Heat Lamps Added to Sensing Lines & Transmitter Cabinets | | | 05000313/LER-1979-003-01, /01T-0 on 790425:leak Discovered in Heat Affected Zone of 1 Inch Drainline Socket Weld in B Decay Heat Discharge Cross Connect to a Loop.Caused by Vibration Fatigue.Outer Drainline Isolation Valves Replaced | /01T-0 on 790425:leak Discovered in Heat Affected Zone of 1 Inch Drainline Socket Weld in B Decay Heat Discharge Cross Connect to a Loop.Caused by Vibration Fatigue.Outer Drainline Isolation Valves Replaced | | | 05000368/LER-1979-004-03, /03L-0 on 790107:during Power Escalation Testing, Both Control Element Assembly Clusters Declared Inoperable. Caused by Weak Reed Switch Position Transmitter Power Supply | /03L-0 on 790107:during Power Escalation Testing, Both Control Element Assembly Clusters Declared Inoperable. Caused by Weak Reed Switch Position Transmitter Power Supply | | | 05000313/LER-1979-004-03, /03L-0 on 790424:reactor Bldg Spray Pump Unresponsive to Engineered Safeguards Signal.Caused by Incorrect Agastat Time Relay Setting.Relay Adjusted | /03L-0 on 790424:reactor Bldg Spray Pump Unresponsive to Engineered Safeguards Signal.Caused by Incorrect Agastat Time Relay Setting.Relay Adjusted | | | 05000313/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000368/LER-1979-005-03, /03L-0 on 790109:during Power Escalation Testing, Bistable Primary Power System 6 C Failed,Rendering C Pressurizer Low Pressure Trip Inoperable | /03L-0 on 790109:during Power Escalation Testing, Bistable Primary Power System 6 C Failed,Rendering C Pressurizer Low Pressure Trip Inoperable | | | 05000313/LER-1979-005-03, /03L-0 on 790524:during Leak Rate Testing, Penetration V-1 Leaked in Excess of 50,000 Cubic Cm/Minute. Caused by Buildup of Boric Acid Crystals on Valve Seating Surfaces.Repairs Made & Penetrations Retested | /03L-0 on 790524:during Leak Rate Testing, Penetration V-1 Leaked in Excess of 50,000 Cubic Cm/Minute. Caused by Buildup of Boric Acid Crystals on Valve Seating Surfaces.Repairs Made & Penetrations Retested | | | 05000313/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000368/LER-1979-006-03, /03L-0 on 790109:during Power Escalation Testing, B Core Protection Computer Declared Inoperable When Low Pressurizer Pressure Trips Received.Investigation Showed Ground Fault Relays Fall Out on Low Bus Voltage | /03L-0 on 790109:during Power Escalation Testing, B Core Protection Computer Declared Inoperable When Low Pressurizer Pressure Trips Received.Investigation Showed Ground Fault Relays Fall Out on Low Bus Voltage | | | 05000368/LER-1979-006, Forwards Revised LER 79-006/03X-1 | Forwards Revised LER 79-006/03X-1 | | | 05000313/LER-1979-006-01, /01T-0 on 790607:vendor Notified Util of Possibility That Turbocharger Thrust Bearing Could Be Damaged Under Certain Repeat Start Operating Modes. Procedures Modifided & Improved Lube Oil Sys Being Designed | /01T-0 on 790607:vendor Notified Util of Possibility That Turbocharger Thrust Bearing Could Be Damaged Under Certain Repeat Start Operating Modes. Procedures Modifided & Improved Lube Oil Sys Being Designed | | | 05000313/LER-1979-006, Forwards LER 79-006/01T-0 | Forwards LER 79-006/01T-0 | | | 05000368/LER-1979-007, Forwards LER 79-007/03L-0 & LER 79-009/03L-0 | Forwards LER 79-007/03L-0 & LER 79-009/03L-0 | | | 05000368/LER-1979-007-03, /03L-0 on 790113:during Power Escalation Test, Control Element Assembly Position as Received by Core Protection Computer B Was Incorrect.Caused by Bad Multiplexer Card,Which Was Replaced | /03L-0 on 790113:during Power Escalation Test, Control Element Assembly Position as Received by Core Protection Computer B Was Incorrect.Caused by Bad Multiplexer Card,Which Was Replaced | | | 05000313/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000313/LER-1979-007-03, /03L-0 on 790616:during Heatup,Emergency Feedwater Pump Automatically Started W/Inadvertent Actuation.Caused by Valve Lineup Error.Outboard Pump Bearing Found to Be Hot Due to Faulty Installation.Maint Procedure Revised | /03L-0 on 790616:during Heatup,Emergency Feedwater Pump Automatically Started W/Inadvertent Actuation.Caused by Valve Lineup Error.Outboard Pump Bearing Found to Be Hot Due to Faulty Installation.Maint Procedure Revised | | | 05000313/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000368/LER-1979-008-03, /03L-0 on 790114:during Power Ascension Testing, Refueling Water Tank Level transmitter,2LT-5639-3,sensing Line Froze Due to Temporary Heat Lamp Burnout | /03L-0 on 790114:during Power Ascension Testing, Refueling Water Tank Level transmitter,2LT-5639-3,sensing Line Froze Due to Temporary Heat Lamp Burnout | | | 05000313/LER-1979-008-03, /03L-0 on 790621:emergency Feed Actuation Received When once-through Steam Generator a Startup Level Transmitter Selection Was Shifted.Caused by Overspeed Trips Due to Water in Steam Supply Line | /03L-0 on 790621:emergency Feed Actuation Received When once-through Steam Generator a Startup Level Transmitter Selection Was Shifted.Caused by Overspeed Trips Due to Water in Steam Supply Line | | | 05000368/LER-1979-009-03, /03L-0 on 790121:during Power Escalation Testing, Reactor Protection Sys Channel C Trip Path Solid State Relay Failed,Opening Reactor Trip Path Circuit Breakers 3 & 7.Relay Was Replaced;Within 4-h Circuit Breakers Closed | /03L-0 on 790121:during Power Escalation Testing, Reactor Protection Sys Channel C Trip Path Solid State Relay Failed,Opening Reactor Trip Path Circuit Breakers 3 & 7.Relay Was Replaced;Within 4-h Circuit Breakers Closed | | | 05000313/LER-1979-009, Forwards LER 79-009/03L-0 & 79-010/01T-0 | Forwards LER 79-009/03L-0 & 79-010/01T-0 | | | 05000313/LER-1979-009-03, /03L-0 on 790628:during Power Operation Reactor Bldg Hydrogen Purge Fan VSF-30A Tripped After 90 Minutes of 10-h Run.Caused by Overcurrent.Fan Restarted Using Less Sealing Water | /03L-0 on 790628:during Power Operation Reactor Bldg Hydrogen Purge Fan VSF-30A Tripped After 90 Minutes of 10-h Run.Caused by Overcurrent.Fan Restarted Using Less Sealing Water | | | 05000313/LER-1979-010, Forwards Updated LER 79-010/01X-1 | Forwards Updated LER 79-010/01X-1 | | | 05000313/LER-1979-010-01, /01T-0 on 790714:design of Main Steamline Restraints Did Not Consider Steam Hammer Transient Forces. Review Performed.Overstressed Area Will Be Modified | /01T-0 on 790714:design of Main Steamline Restraints Did Not Consider Steam Hammer Transient Forces. Review Performed.Overstressed Area Will Be Modified | | | 05000368/LER-1979-010-03, /03L-0 on 790124:pump Discharge valve,2CV-5667-2, Stroked Fully Open But Immediately Reclosed.Caused by sodium-hydroxide Tank Low Level Alarm & Indication Circuit Being Out of Alignment | /03L-0 on 790124:pump Discharge valve,2CV-5667-2, Stroked Fully Open But Immediately Reclosed.Caused by sodium-hydroxide Tank Low Level Alarm & Indication Circuit Being Out of Alignment | | | 05000368/LER-1979-011-03, /03L-0 on 790125:during Power Escalation,Channel B Core Protection Computer Failed,Resulting in Departure from Nucleate Boiling Ratio & Linear Power Density Trips. Caused by Movement of Temporary Cables Connected to B | /03L-0 on 790125:during Power Escalation,Channel B Core Protection Computer Failed,Resulting in Departure from Nucleate Boiling Ratio & Linear Power Density Trips. Caused by Movement of Temporary Cables Connected to B | | | 05000368/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000313/LER-1979-011, Forwards LER 79-011/01T-O | Forwards LER 79-011/01T-O | | | 05000313/LER-1979-011-01, /01T-0 on 790809:during NRC Performance Appraisal Team Interview,Discovered That Pressurizer Safety Relief Valve PSV-1002 Was Not Properly Tested in Mar 1978.Valve Retested 790812 W/No Adjustments Required | /01T-0 on 790809:during NRC Performance Appraisal Team Interview,Discovered That Pressurizer Safety Relief Valve PSV-1002 Was Not Properly Tested in Mar 1978.Valve Retested 790812 W/No Adjustments Required | | | 05000313/LER-1979-012, Forwards LER 79-012/03L-1 | Forwards LER 79-012/03L-1 | | | 05000313/LER-1979-012-03, Leak Rate Testing of Reactor Bldg Purge Valves at Penetration V-1 Indicated Leak Rate in Excess of Tech Spec Limits.Caused by Maladjusted Valve Seat Shims.Leak Rate Test Performed | Leak Rate Testing of Reactor Bldg Purge Valves at Penetration V-1 Indicated Leak Rate in Excess of Tech Spec Limits.Caused by Maladjusted Valve Seat Shims.Leak Rate Test Performed | | | 05000368/LER-1979-012-03, /03L-0 on 790127:core Protection Computer Channel B Failed,Resulting in Trips.Caused by Analog High Level Amplifier Card Improperly Seating in Connector.Card Reseated & Functional Test Conducted | /03L-0 on 790127:core Protection Computer Channel B Failed,Resulting in Trips.Caused by Analog High Level Amplifier Card Improperly Seating in Connector.Card Reseated & Functional Test Conducted | | | 05000313/LER-1979-013-03, /03L-0:on 790808,decay Heat Boron Concentration Was Not Monitored During Prescribed Interval & Inservice Decay Heat Loop Was Switched W/O Switching Sample Lineup. Caused by Communications Breakdown Between Depts | /03L-0:on 790808,decay Heat Boron Concentration Was Not Monitored During Prescribed Interval & Inservice Decay Heat Loop Was Switched W/O Switching Sample Lineup. Caused by Communications Breakdown Between Depts | | | 05000313/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000368/LER-1979-013-03, /03L-0 on 790127:control Element Assembly Cluster (Ceac) Deviation Alarms Received.Caused by Disturbance of Ceac Cable Connections | /03L-0 on 790127:control Element Assembly Cluster (Ceac) Deviation Alarms Received.Caused by Disturbance of Ceac Cable Connections | | | 05000313/LER-1979-014, Forwards LER 79-014/99X-0 | Forwards LER 79-014/99X-0 | | | 05000313/LER-1979-014-99, /99X-0:on 790813,w/75% Reactor Power,Switchyard Relay 21Z1 Failed,Causing Turbine Trip.Caused by Lug Failure on Terminal Leads to Turbine Lockout Relay 286-T.Failed Lug Replaced,Terminals Tightened & Turbine Interlocks Teste | /99X-0:on 790813,w/75% Reactor Power,Switchyard Relay 21Z1 Failed,Causing Turbine Trip.Caused by Lug Failure on Terminal Leads to Turbine Lockout Relay 286-T.Failed Lug Replaced,Terminals Tightened & Turbine Interlocks Tested | | | 05000368/LER-1979-014-03, /03-0 on 790127:plant Protection Sys C Containment Bldg Pressure Transmitter 2PT-5603-3N Failed, Causing Hi & Hi-Hi Containment Pressure Trips.Caused by Loose Output Connection,Which Was Subsequently Reconnected | /03-0 on 790127:plant Protection Sys C Containment Bldg Pressure Transmitter 2PT-5603-3N Failed, Causing Hi & Hi-Hi Containment Pressure Trips.Caused by Loose Output Connection,Which Was Subsequently Reconnected | | | 05000368/LER-1979-015-03, /03L-0 on 790128:failure of Core Protection Computer D & C,Resulting in Respective Channel Trips;One Caused by Tripped Power Supply & Other Appears non-repetitive.Both Channels Were Successfully Restarted | /03L-0 on 790128:failure of Core Protection Computer D & C,Resulting in Respective Channel Trips;One Caused by Tripped Power Supply & Other Appears non-repetitive.Both Channels Were Successfully Restarted | | | 05000313/LER-1979-015-99, /99X-0:on 790817,as Result of Analysis of Seismic Category I Pipe supports,37 Restraints Were Identified to Have Safety Factor of Less than Two.Supports Modified | /99X-0:on 790817,as Result of Analysis of Seismic Category I Pipe supports,37 Restraints Were Identified to Have Safety Factor of Less than Two.Supports Modified | | | 05000368/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000368/LER-1979-016-03, /03L-0 on 790130:during Power Escalation Testing, Mode 1 Operation,Safety Injection Tank D Pressure Dropped Below Tech Spec Limit.Caused by Excessive Leakage Due to Oversized Valve Body.Seal Ring Replaced W/Oversized Ring | /03L-0 on 790130:during Power Escalation Testing, Mode 1 Operation,Safety Injection Tank D Pressure Dropped Below Tech Spec Limit.Caused by Excessive Leakage Due to Oversized Valve Body.Seal Ring Replaced W/Oversized Ring | | | 05000313/LER-1979-016, Forwards Updated LER 79-016/03X-1 | Forwards Updated LER 79-016/03X-1 | | | 05000313/LER-1979-016-03, /03L-0:on 790827,diesel Generator 2 Tripped on Low Oil Pressure,Rendering Generator Inoperable.Caused by Leak Allowing Water to Enter Oil Sys,Causing High Crankcase Pressure.Oil Cooler Replaced | /03L-0:on 790827,diesel Generator 2 Tripped on Low Oil Pressure,Rendering Generator Inoperable.Caused by Leak Allowing Water to Enter Oil Sys,Causing High Crankcase Pressure.Oil Cooler Replaced | | | 05000368/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | |
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