05000368/LER-1981-007, Updated LER 81-007/03L-1:on 810206 & 0318,control Room Emergency Chillers 2VE-1B & 2VE-1A,respectively,were Declared Inoperable.Caused by Low Oil Pressure in Former & Oil Unloader Relief Misadjustment in Latter

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Updated LER 81-007/03L-1:on 810206 & 0318,control Room Emergency Chillers 2VE-1B & 2VE-1A,respectively,were Declared Inoperable.Caused by Low Oil Pressure in Former & Oil Unloader Relief Misadjustment in Latter
ML19347E277
Person / Time
Site: Arkansas Nuclear 
Issue date: 04/17/1981
From: Pendergraft R
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19347E275 List:
References
LER-81-007-03L, LER-81-7-3L, NUDOCS 8104240506
Download: ML19347E277 (1)


LER-1981-007, Updated LER 81-007/03L-1:on 810206 & 0318,control Room Emergency Chillers 2VE-1B & 2VE-1A,respectively,were Declared Inoperable.Caused by Low Oil Pressure in Former & Oil Unloader Relief Misadjustment in Latter
Event date:
Report date:
3681981007R00 - NRC Website

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UPDATE REPORT - PREVIOUS REPORT DATE 3/4/81 O

N RC FORM 364 U. S, NUCLE AR REGUL ATORY COMMISSION LICENSEE EVENT REPORT EXHIBIT A CONTROL 8 LOCK: l l l l ] l lh (PLE ASE PRINT OR TYPE ALL REQU' RED INFORMATIONI l A] R l A l Nl 0 l 2 l@isl 010 l -10 l0 l 0l Og 0 l-l 0 l0 lg l1 [ 1l1 l 1lgl CAT 8g l

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8 60 65 ooCKET NUMetR 68 60 EVENT oATE le FS ME,oR T e4TE 80 EVENT OESCRIPTION AND PROBA8LE CONSEQUENCES h 1During Mode 1 operation, while performing monthly surveillance testing of 1 o 2 F5TO icontrol Room Emergency Chillers, 2VE-1B was declared inoperable on 2/6/81 I l o i i l& 2VE-1A on 3/18/81. The alternate Emergency Chiller remained operable ini ieach case.

Other occurrences involving the Emergency Control Room Chillers o s oa tare: LER's 50-368/79-050,79-053, 79-076,80-026, 80-054,80-070 & 80-0926 l Reportable per T.S. 6.9.1.9.b.

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