ENS 42157
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ENS Event | |
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23:51 Nov 19, 2005 | |
Title | Unplanned Diesel Generator Starts on a Vaild Bus Undervoltage Signal |
Event Description | On November 19, 2005 at 1551 Pacific Standard Time Diablo Canyon Unit 2 [was] in Mode 1 (Power Operation) at approximately 100% power when the 230kv offsite power supply breaker (#212) opened. Diesel generators 2-1, 2-2, and 2-3 auto-started on a valid bus undervoltage signal.
The immediate cause of the event was the opening of the 230kv breaker (#212) due to a valid (but unintentional) startup transformer 1-1 sudden pressure switch activation due to maintenance being performed on the Unit 1 Startup Transformer 1-1. All equipment performed as expected. None of the diesel generators picked up load since the buses remained energized. The safety buses were powered by offsite power. Unit 1 is in a refueling outage and was not adversely affected. The diesel generators are currently being returned to a standby condition. The licensee will notify the NRC Resident Inspector. |
Where | |
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Diablo Canyon California (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000323/LER-2005-002 |
Time - Person (Reporting Time:+-3.5 h-0.146 days <br />-0.0208 weeks <br />-0.00479 months <br />) | |
Opened: | James M. Welsch 20:21 Nov 19, 2005 |
NRC Officer: | Pete Snyder |
Last Updated: | Nov 19, 2005 |
42157 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 567692023-10-01T03:14:0001 October 2023 03:14:00
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System Actuation Emergency Diesel Generators Start Due to Loss of Off Site Start Up Power ENS 430472006-12-12T21:22:00012 December 2006 21:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Circulating Water Pump Failure Causes Explosion in Intake Structure ENS 430422006-12-11T00:08:00011 December 2006 00:08:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rapid Shutdown and Manual Reactor Trip Due to High Reactor Coolant Pump Stator Temperature ENS 421572005-11-19T23:51:00019 November 2005 23:51:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Diesel Generator Starts on a Vaild Bus Undervoltage Signal ENS 412502004-12-09T10:04:0009 December 2004 10:04:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rps Actuation While Shutdown Due to Failed Fuse ENS 411682004-11-02T19:05:0002 November 2004 19:05:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Diesel Generator Start on a Valid Bus Undervoltage Signal 2023-10-01T03:14:00 | |
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