ENS 49527
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ENS Event | |
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10:20 Nov 11, 2013 | |
Title | Unit 1 Commenced a Technical Specification Required Shutdown Due to Rcs Leakage |
Event Description | Oconee Nuclear Station identified a small Reactor Coolant System (RCS) pressure boundary leak on ONS [Oconee Nuclear Station] Unit 1 and initiated a Unit 1 shutdown at 0520 hours0.00602 days <br />0.144 hours <br />8.597884e-4 weeks <br />1.9786e-4 months <br /> [EST] on November 11, 2013 in accordance with procedures and Technical Specifications. Visual inspection confirmed the leak is located on the 1B2 loop High Pressure Injection Line. ONS Unit 1 was operating at full power when the leak was identified and a down power to 20% was commenced at 2141 hours0.0248 days <br />0.595 hours <br />0.00354 weeks <br />8.146505e-4 months <br /> [EST] on November 10, 2013 in order to characterize the leak and leak location. The measured RCS leak rate was 0.13 gpm [gallons per minute] at the time of commencing the down power.
This issue is reportable per 10 CFR 50.72(b)(2)(i) and 10 CFR 50.72(b)(3)(ii)(A). The NRC Resident Inspector has been notified. This event poses no threat to the public or station employees. Unit 1 entered TS 3.4.13 Condition B at 0520 EST on 11/11/13. This TS requires Unit 1 be in Mode 3 Hot Standby within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and Mode 5 Cold Shutdown within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. The generator is currently offline and the licensee anticipates entering Mode 3 at 1000 EST. Unit 1 entered their Abnormal Operating procedures for leak determination at 0442 EST on 11/09/13. |
Where | |
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Oconee South Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded | |
Time - Person (Reporting Time:+-1.53 h-0.0638 days <br />-0.00911 weeks <br />-0.0021 months <br />) | |
Opened: | Corey A. Gray 08:48 Nov 11, 2013 |
NRC Officer: | Steve Sandin |
Last Updated: | Nov 11, 2013 |
49527 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (20 %) |
After | Power Operation (13 %) |
Oconee with 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded | |
WEEKMONTHYEARENS 562212022-11-14T11:30:00014 November 2022 11:30:00
[Table view]10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Reactor Coolant System (RCS) Pressure Boundary Degraded ENS 561972022-11-01T18:33:0001 November 2022 18:33:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Reactor Coolant System (RCS) Pressure Boundary Degraded ENS 495272013-11-11T10:20:00011 November 2013 10:20:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Unit 1 Commenced a Technical Specification Required Shutdown Due to Rcs Leakage ENS 465262011-01-08T19:00:0008 January 2011 19:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Partial Closure of Letdown Line Isolation Valve 1Hp-5 ENS 426412006-06-14T18:00:00014 June 2006 18:00:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Leaking Decay Heat Removal Isolation Valve Bypass Line ENS 419662005-08-31T18:28:00031 August 2005 18:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unit 3 Experienced an Automatic Reactor Trip During Routine Testing ENS 414132005-02-16T18:31:00016 February 2005 18:31:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Degraded Condition - Reactor Building Normal Sump Level Increasing ENS 414022005-02-11T04:00:00011 February 2005 04:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Loss of Electrical Power Sources ENS 409022004-07-28T12:00:00028 July 2004 12:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Shutdown Required by Technical Specifications ENS 404332004-01-09T00:02:0009 January 2004 00:02:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Ts Required Shutdown at Oconee 1 Due to Unidentified Rcs Leakage 2022-11-14T11:30:00 | |
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