ENS 51952
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ENS Event | |
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05:50 Mar 28, 2016 | |
Title | Invalid Actuation of Inboard Isolation Logic |
Event Description | On Monday, March 28, 2016, Unit 1 was in OPCON 5 (Refueling) conducting a refueling outage. A modification was being installed for an NSSSS [Nuclear Steam Supply Shutoff System] Test Box on Division 1A Group 1 NSSSS logic. At 0150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br />, a logic jumper was removed as directed by the work order and a logic fuse failed. The fuse failure caused an unplanned invalid actuation of the inboard isolation logic. The isolations were reset and the valves were restored to initial conditions at 0246 hours0.00285 days <br />0.0683 hours <br />4.06746e-4 weeks <br />9.3603e-5 months <br />. On Sunday, April 3, 2016, at 0134 hours0.00155 days <br />0.0372 hours <br />2.215608e-4 weeks <br />5.0987e-5 months <br />, one additional logic fuse opening event occurred during the testing which also caused an invalid actuation which was reset at 0405 hours0.00469 days <br />0.113 hours <br />6.696429e-4 weeks <br />1.541025e-4 months <br />. The fuse openings occurred during jumper manipulations as the modification was tested on the Division 1A and 1D logic during the refuel outage. The investigation determined the fuse openings were due to the testing process. The suspected devices that caused the condition are not permanent plant equipment and there is no degradation of the actual circuit. They were part of a temporary configuration that was installed to support modification installation and acceptance testing. The temporary devices have been removed.
The portion of the primary containment isolation system that received an actuation signal functioned successfully. All of the affected open isolation valves automatically closed. The isolation was a partial actuation. This 60-day ENS report is being made per 10CFR 50.73(a)(2)(iv)(A) and 10CFR50.73(a)(1) to report invalid automatic actuations of systems listed in paragraph (a)(2)(iv)(B). The listed system that actuated was general containment isolation signals affecting containment isolation valves in more than one system. Primary containment isolation valves (PCIVs) closed on reactor water cleanup (RWCU), drywell chilled water (DWCW), primary containment instrument gas (PCIG), drywell sumps and the suppression pool cleanup systems. The licensee has notified the NRC Resident Inspector. |
Where | |
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Limerick Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1372.37 h57.182 days <br />8.169 weeks <br />1.88 months <br />) | |
Opened: | John Harkins 10:12 May 24, 2016 |
NRC Officer: | Dong Park |
Last Updated: | May 24, 2016 |
51952 - NRC Website
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WEEKMONTHYEARENS 564642023-02-16T12:05:00016 February 2023 12:05:00
[Table view]Other Unspec Reqmnt, 10 CFR 50.73(a)(1), Submit an LER 60 Day Notification for an Invalid Actuation of the Emergency Service Water System ENS 562832022-11-02T23:29:0002 November 2022 23:29:00 10 CFR 50.73(a)(1), Submit an LER 60-DAY Telephonic Notification - Invalid Specific System Actuation ENS 553452021-05-13T11:00:00013 May 2021 11:00:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Signal ENS 540832019-04-18T06:49:00018 April 2019 06:49:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of a Unit 2 Containment Isolation Logic Due to a Blown Fuse ENS 540142019-02-22T15:30:00022 February 2019 15:30:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of a Unit 1 Containment Isolation Logic Due to a Blown Fuse ENS 519522016-03-28T05:50:00028 March 2016 05:50:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Inboard Isolation Logic ENS 485752012-10-13T23:41:00013 October 2012 23:41:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification of Invalid Multiple System Actuations ENS 468832011-04-02T16:18:0002 April 2011 16:18:00 10 CFR 50.73(a)(1), Submit an LER Loss of Rps/Ups Power Supply ENS 459622010-04-03T01:56:0003 April 2010 01:56:00 10 CFR 50.73(a)(1), Submit an LER Overvoltage Condition Causes Reactor Protective System Actuation ENS 455182009-10-19T16:05:00019 October 2009 16:05:00 10 CFR 50.73(a)(1), Submit an LER Automatic Closure of Primary Containment Isolation Valves Due to Invalid Signal ENS 442602008-04-09T08:16:0009 April 2008 08:16:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Notification for Invalid Specified System Actuation ENS 433662007-03-19T06:20:00019 March 2007 06:20:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuations During Testing ENS 428302006-07-09T22:49:0009 July 2006 22:49:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of the B Esw Pump ENS 425722006-03-14T21:40:00014 March 2006 21:40:00 10 CFR 50.73(a)(1), Submit an LER Inadvertant Core Spray Pump Actuation ENS 416672005-03-06T19:07:0006 March 2005 19:07:00 10 CFR 50.73(a)(1), Submit an LER Invalid Safety System Actuation During an Outage ENS 408952004-05-26T20:22:00026 May 2004 20:22:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Invalid Automatic Actuation Report: Containment Isoaltion Valves in More than One System 2023-02-16T12:05:00 | |
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