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nC eem 354 U 5. NUCLEAR KEGULATORY COMMisslON f
APPROVED OM8 NO 31504104 i
LICENSEE EVENT REPORT (LER)
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t F ACILITY NAME (11 DOCKET NUM0ER (2)
PAGE 63e 1
Fermi 2 o 15 I o Io I o i 31411 1 loFl013 Inadequate Communication Results in Automatic Isolation of RWCU During Calibration Activity EVENT DATE ISI LER NUM8ER 161 REPORT DATE 171 OTHER F ACILITIES INVOLVED (8)
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NAME TELEPMONE NUMBER ARE A CODE Lewis P. Bregni, Compliance Engineer 313 5 i 8,6l-iSi3i l3 i i 1
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At 0110 hours0.00127 days <br />0.0306 hours <br />1.818783e-4 weeks <br />4.1855e-5 months <br /> on January 26, 1987 Fermi 2 was in OPERATIONAL CONDITION 1 (POWER OPERATION), operating at 925 psig, 530 degrees Fahrenheit, and 10 percent reactor power.
While performing calibration activities for a differential temperature switch in a leak detection circuit for the Reactor Water Cleanup System (RWCU) an automatic Engineered Safety Feature (ESF) isolation actuation was received.
The isolation occurred when an Instrument Repairman lif ted the thermocouple leads to the differential temperature switch.
This event was caused by a shared personnel error, and resulted from inadequate communication between an Instrument Repairman and shift personnel.
As corrective actions, Instrument Repairmen have been instructed to provide the details and consequences of their activities to operations prior to work initiation, and Instrument Foremen have been instructed to discuss work packages which could impact plant operations with the assigned repairman prior to work initiation.
Additionally, information has been provided to selected Operations personnel to encourage better communications.
This event was not contributed to by any failed components, i
structures, or systems.
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e= =.wm At 0110 hours0.00127 days <br />0.0306 hours <br />1.818783e-4 weeks <br />4.1855e-5 months <br /> on January 26, 1987 Fermi 2 was in OPERATIONAL CONDITION 1 (POWER OPERATION), operating at 925 psig, 530 degrees Fahrenheit, and 10 percent reactor power.
While performing calibration activities for a differential temperature switch (TDT) in a leak detection circuit for the Reactor Water Cleanup System (RWCU) an automatic Engineered Safety Feature (ESF) (JE) isolation actuation was received.
Prior to the event, Operations personnel had noted that the common differential temperature meter for the RWCU rooms was not reading at zere when no input signal was applied to it.
As a result, a request was issued to have the meter needle zero adjusted and an Instrument Repairman (non-licensed, contractor) was assigned to investigate and adjust the meter needle zero.
The work request document stated that the meter needle zero was reading incorrectly and needed to be adjusted.
However, since adjusting the needle zero can. affect the span of the meter calibration, the repairman interpreted his assignment to also include calibration of the dif ferential temperature switch.
The procedure used to calibrate the differential temperature switch requires that the thermocouple leads to the switch be determinated.
Lifting a lead to the temperature switch can cause an isolation of the outboard RWCU isolation valve if it results in the circuit output exceeding the switch setpoint.
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After receiving his work assignment, the repairman reported to the main Control Room (NA) to obtain work authorization.
The Instrument Repairnan understood that the calibration activity he was going to perform would probably result in an RWCU isolation at this time.
Since the Nuclear Assistant Shift Supervisor (NASS) (licensed,
utility) believed that the repairman was only going to adjust the meter needle zero he did not ask for details concerning the work that was about to performed.
Conversely, since the repairman had interpreted his work assignment differently than the NASS, he believed that the NASS had taken the necessary actions to preempt an RWCU isolation, and did not indicate to the NASS the ef fect of his intended actions.
l At 0110 hours0.00127 days <br />0.0306 hours <br />1.818783e-4 weeks <br />4.1855e-5 months <br /> an ESF isolation of the outboard RWCU isolation valve (G33-F004) was automatically initiated in response to the repairman lif ting the leads to the dif ferential temperature switch (G33-N602D).
Following the isolation, the NASS reported to the location where the repairman was working and the leads had been lifted to inform the repairman of the isolation actuation.
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At 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> the differential temperature switch leads were restored and the affected isolation valve was reopened.
This event was caused by a shared personnel error by the NASS and the Instrument Repairman and resulted from a lack of communication between the repairman and the NASS.
This event did not involve actions which were not in accordance with procedures, an error in a procedure, or an activity which is not described in a procedure.
This event was not contributed to by any unusual conditions of the workplace, or any components, structures, or systems that were inoperable at the start of the event, or that failed.
As corrective actions, Instrument Repairmen have been counseled to ensure that they provide the details and consequences of their activities to Operations prior to work initiation, and Instrument Foremen have been instructed to discuss work packages which could impact plant operations with repairmen prior to work initiation.
Additionally, information has been provided to selected Operations personnel to encourage better communications.
During this event, plant conditions requiring isolation of the RWCU system did not exist.
As a result, this event did not affect the safe operation of the plant or the safety of the public.
Had an RWCU isolation been required by plant conditions, system l
isolation capability was demonstrated to be available during the event by the proper operation of the RWCU isolation actuation j
logic and components.
A previous event involving maintenance activity for an RWCU room differential temperature switch was described in Licensee Event Repcrt 86-046.
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DI 10CFR50.73 rermi2 Edison HEEN m,,
operations February 25, 1987 NP870lll U. S. Nuclear Regulatory Commission Attention:
Document Control Desk Washington, D.C. 20555 Gentlemen:
Reference:
Fermi 2 NRC Docket No. 50-341 Facility Operating License No. NPF-43
Subject:
Transmittal of Licensee Event Recort 87-001-00
+
Please find enclosed LER No. 87-001-00, dated February 25, 1987, for a reportable event that occurred on January 26, 1987.
As indicated below, a copy of this LER is being sent to the Administrator Region III.
If you have any questions, please contact us.
S ince r ely, R.
S. Lenart f
Plant Manager
Enclosure:
NRC Forms 366, 366A cc:
J. R. Eckert J. G. Keppler W. G. Rogers J. J. Stefano 7
)hgjL '
Wayne County Emergency
!!anagement Division I
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| 05000341/LER-1987-001, :on 870126,during Calibr Activities in RWCU Sys,Esf Isolation Actuation Received.Caused by Inadequate Communication Between Instrument Repairman & Shift Personnel.Personnel Counseled |
- on 870126,during Calibr Activities in RWCU Sys,Esf Isolation Actuation Received.Caused by Inadequate Communication Between Instrument Repairman & Shift Personnel.Personnel Counseled
| | | 05000341/LER-1987-002, :on 870226,tubine Tripped Initiating Reactor Scram.Caused by Aluminum Strip Used as Assembly Aid for iso- Phase Bus Cooling Duct,Breaking Free & Contacting y-phase Bus Causing Ground Fault.Relay Replaced |
- on 870226,tubine Tripped Initiating Reactor Scram.Caused by Aluminum Strip Used as Assembly Aid for iso- Phase Bus Cooling Duct,Breaking Free & Contacting y-phase Bus Causing Ground Fault.Relay Replaced
| | | 05000341/LER-1987-005, :on 870212,leakage Through Demineralizer Vessel Gasket Triggered Differential Flow Alarm Causing Manual ESF RWCU Isolation.Caused by Failure of Gasket Insert for Vessel Head.Gasket Design Modified & Replaced |
- on 870212,leakage Through Demineralizer Vessel Gasket Triggered Differential Flow Alarm Causing Manual ESF RWCU Isolation.Caused by Failure of Gasket Insert for Vessel Head.Gasket Design Modified & Replaced
| | | 05000341/LER-1987-006, :on 870211,damage to HPCI Turbine Occurred. Caused by Closed Governor Bearing Oil Supply Valve & Repositioned Thrust Bearing Oil Supply Valve.Governor Bearing & Turbine Shaft Replaced |
- on 870211,damage to HPCI Turbine Occurred. Caused by Closed Governor Bearing Oil Supply Valve & Repositioned Thrust Bearing Oil Supply Valve.Governor Bearing & Turbine Shaft Replaced
| | | 05000341/LER-1987-007-01, :on 870317,steam Flashing Occurred in RHR Pipes Causing Reactor Protection Sys & Automatic ESF Isolation. Caused by Failure of 24 Inch Injection Check Valve to Open. Open Limit Switch Adjusted & Procedure Issued |
- on 870317,steam Flashing Occurred in RHR Pipes Causing Reactor Protection Sys & Automatic ESF Isolation. Caused by Failure of 24 Inch Injection Check Valve to Open. Open Limit Switch Adjusted & Procedure Issued
| | | 05000341/LER-1987-007, :on 870317,while Preparing Unit for Shutdown for Outage,Operators Voided RHR Piping Resulting in ESF & Reactor Protection Sys Actuation.Caused by Inadequate Procedure.Procedure Being Reviewed |
- on 870317,while Preparing Unit for Shutdown for Outage,Operators Voided RHR Piping Resulting in ESF & Reactor Protection Sys Actuation.Caused by Inadequate Procedure.Procedure Being Reviewed
| | | 05000341/LER-1987-008, :on 870301,power to Portions of Turbine Control Circuitry Lost Resulting in ESF Valve Isolation,Reactor Protection Sys Actuation & Reactor Scram.Caused by Personnel Error.Alarm Response Procedures Revised |
- on 870301,power to Portions of Turbine Control Circuitry Lost Resulting in ESF Valve Isolation,Reactor Protection Sys Actuation & Reactor Scram.Caused by Personnel Error.Alarm Response Procedures Revised
| | | 05000341/LER-1987-009, :on 870325,RHR Pump C Tripped Due to Inboard Isolation Valve Closing.Caused by Intermittent Failure of Master Trip Unit.Futher Investigation of Master Trip Unit Will Be Made by Mfg.Isolation Logic Reset |
- on 870325,RHR Pump C Tripped Due to Inboard Isolation Valve Closing.Caused by Intermittent Failure of Master Trip Unit.Futher Investigation of Master Trip Unit Will Be Made by Mfg.Isolation Logic Reset
| | | 05000341/LER-1987-011, :on 870406,during APRM Functional Testing, Reactor Scrammed.Caused by Personnel Error.Procedures for Performing APRM Functional Testing Revised & Individual Involved Couseled |
- on 870406,during APRM Functional Testing, Reactor Scrammed.Caused by Personnel Error.Procedures for Performing APRM Functional Testing Revised & Individual Involved Couseled
| | | 05000341/LER-1987-012, :on 870410,HPCI & RCIC Declared Inoperable Due to Blown Fuse.Caused by Failed Fixed Capacitor C-25 in Isolation Instrumentation.Hpci & RCIC Restored |
- on 870410,HPCI & RCIC Declared Inoperable Due to Blown Fuse.Caused by Failed Fixed Capacitor C-25 in Isolation Instrumentation.Hpci & RCIC Restored
| | | 05000341/LER-1987-013, :on 870313,cracks Found on Some Termination Box Adaptors of Reactor Bldg Cooling Unit Fan Motors.Operability Review Completed on 870421.Caused by Weight of Components, Vibration & Overtightening of Mounting Bolts |
- on 870313,cracks Found on Some Termination Box Adaptors of Reactor Bldg Cooling Unit Fan Motors.Operability Review Completed on 870421.Caused by Weight of Components, Vibration & Overtightening of Mounting Bolts
| | | 05000341/LER-1987-014, :on 870426,actuation of Reactor Protection Sys Occurred Due to Leakage Through Isolation Valves.Caused by Lack of Procedural Guidance.Procedure Used for ANSI & ASME Pressure Testing Will Be Revised |
- on 870426,actuation of Reactor Protection Sys Occurred Due to Leakage Through Isolation Valves.Caused by Lack of Procedural Guidance.Procedure Used for ANSI & ASME Pressure Testing Will Be Revised
| | | 05000341/LER-1987-015, :on 870416,sodium Pentaborate Concentrations in Standby Liquid Control Storage Tank Exceeded Tech Spec Limits.Caused by Personnel Errors & Inadequate Procedures. Procedures 77.000.04 & 78.000.72 Revised |
- on 870416,sodium Pentaborate Concentrations in Standby Liquid Control Storage Tank Exceeded Tech Spec Limits.Caused by Personnel Errors & Inadequate Procedures. Procedures 77.000.04 & 78.000.72 Revised
| | | 05000341/LER-1987-016, :on 870510,reactor Protection Sys Actuated & ESFs Challenged Due to Transient in Common Ref Leg.Caused by Repairman Attempt to Crack Open Ref Leg Isolation Valve. Valves to Improve Repairman Control Installed |
- on 870510,reactor Protection Sys Actuated & ESFs Challenged Due to Transient in Common Ref Leg.Caused by Repairman Attempt to Crack Open Ref Leg Isolation Valve. Valves to Improve Repairman Control Installed
| | | 05000341/LER-1987-017, :on 870513,south Reactor Feed Pump Turbine (Srfpt) Tripped Due to Apparent Srfpt High Pressure Casing Drain Valve Being Closed During Startup.Caused by Inadequate Procedure.Procedure Revised |
- on 870513,south Reactor Feed Pump Turbine (Srfpt) Tripped Due to Apparent Srfpt High Pressure Casing Drain Valve Being Closed During Startup.Caused by Inadequate Procedure.Procedure Revised
| | | 05000341/LER-1987-018, :on 870520,during Troubleshooting of Leakage Discovered in Drywell,Rwcu Inboard Isolation Valve Isolated Twice & Outboard Isolation Valve Once.Caused by Latent Heat Migration in Sys Piping.Valve Repacked |
- on 870520,during Troubleshooting of Leakage Discovered in Drywell,Rwcu Inboard Isolation Valve Isolated Twice & Outboard Isolation Valve Once.Caused by Latent Heat Migration in Sys Piping.Valve Repacked
| | | 05000341/LER-1987-019, :on 870523,standby Gas Treatment Sys Manual Actuation Puff Test Incorrectly Scheduled.Caused by Personnel Error.Program Revised to Reflect Correct Test Frequency |
- on 870523,standby Gas Treatment Sys Manual Actuation Puff Test Incorrectly Scheduled.Caused by Personnel Error.Program Revised to Reflect Correct Test Frequency
| | | 05000341/LER-1987-020, :on 870528,automatic Start of Div II Emergency Diesel Generators Occurred.Caused by Repairman Working within Wrong Cabinet During Surveillance.Personnel Counseled & Events Details Will Be Reviewed W/Repairmen |
- on 870528,automatic Start of Div II Emergency Diesel Generators Occurred.Caused by Repairman Working within Wrong Cabinet During Surveillance.Personnel Counseled & Events Details Will Be Reviewed W/Repairmen
| | | 05000341/LER-1987-021, :on 870607,RCS Leakage Limit Surveillance Interval,Including 25% Max Allowable Extension,Exceeded by 1 H.Caused by Personnel Error.Instructions Given to Personnel Re Completing Surveillance on Time |
- on 870607,RCS Leakage Limit Surveillance Interval,Including 25% Max Allowable Extension,Exceeded by 1 H.Caused by Personnel Error.Instructions Given to Personnel Re Completing Surveillance on Time
| | | 05000341/LER-1987-022, :on 870601,actuation of Recirculation Mode of Control Ctr HVAC Occurred.Caused by Inadequate Review While Preparing Work Package.Fuse Replaced,Control Ctr HVAC Sys Placed in Normal Mode & Personnel Counseled |
- on 870601,actuation of Recirculation Mode of Control Ctr HVAC Occurred.Caused by Inadequate Review While Preparing Work Package.Fuse Replaced,Control Ctr HVAC Sys Placed in Normal Mode & Personnel Counseled
| | | 05000341/LER-1987-023, :on 870710,isolation of RCIC Occurred During Functional Test.Caused by Repairman Leaving volt-ohm Meter Connected Across Relay in Channel D Simulating Closed Contact Condition.Channels Tested |
- on 870710,isolation of RCIC Occurred During Functional Test.Caused by Repairman Leaving volt-ohm Meter Connected Across Relay in Channel D Simulating Closed Contact Condition.Channels Tested
| | | 05000341/LER-1987-024, :on 870625,plant Shut Down Due to Inoperabilty of Reactor Recirculation Sys Loop.Caused by Loss of Spring Pressure on Brush Due to Excessively Worn Brush.Increased Insp Frequency Implemented |
- on 870625,plant Shut Down Due to Inoperabilty of Reactor Recirculation Sys Loop.Caused by Loss of Spring Pressure on Brush Due to Excessively Worn Brush.Increased Insp Frequency Implemented
| | | 05000341/LER-1987-025, :on 870625,reactor Protection Sys Actuated & Several ESFs Challenged.Caused by Pressure Spike Sensed by Reactor Vessel Water Level Transmitters on Common Ref Leg. Multi-turn Needle Valves Will Be Installed |
- on 870625,reactor Protection Sys Actuated & Several ESFs Challenged.Caused by Pressure Spike Sensed by Reactor Vessel Water Level Transmitters on Common Ref Leg. Multi-turn Needle Valves Will Be Installed
| | | 05000341/LER-1987-026, :on 870625,RWCU Sys Isolation Occurred.Caused by Shutdown of RWCU Pumps While Reactor Operating Above Ambient Temps.Evaluation Being Made to Revise Sys Operating Procedure |
- on 870625,RWCU Sys Isolation Occurred.Caused by Shutdown of RWCU Pumps While Reactor Operating Above Ambient Temps.Evaluation Being Made to Revise Sys Operating Procedure
| | | 05000341/LER-1987-027, :on 870626,inadvertent Increase in Reactor Coolant Temp During Operational Condition 4 (Cold Shutdown) Occurred.Caused by Personnel Error.Personnel Disciplined & Control Room Annunciator & Displays Modified |
- on 870626,inadvertent Increase in Reactor Coolant Temp During Operational Condition 4 (Cold Shutdown) Occurred.Caused by Personnel Error.Personnel Disciplined & Control Room Annunciator & Displays Modified
| | | 05000341/LER-1987-028, :on 870627,emergency Equipment Cooling Water Sys Actuation Occurred.Caused by Inadequate Procedure Rev. Procedure Revised |
- on 870627,emergency Equipment Cooling Water Sys Actuation Occurred.Caused by Inadequate Procedure Rev. Procedure Revised
| | | 05000341/LER-1987-029, :on 870615,surveillance Requirement for Determining Operability of Circuits Inadequate.Caused by Misinterpretation of Tech Spec.Surveillance Procedure Revised to Reflect Surveillance Requirement |
- on 870615,surveillance Requirement for Determining Operability of Circuits Inadequate.Caused by Misinterpretation of Tech Spec.Surveillance Procedure Revised to Reflect Surveillance Requirement
| | | 05000341/LER-1987-031, :on 870720,high Vibration Signal Caused Turbine Control Valve Fast Closure & Reactor Scram Resulted.Caused by Erroneous High Vibration Signal from Faulty Shaft Rider Sensor Connection.Design Change Being Prepared |
- on 870720,high Vibration Signal Caused Turbine Control Valve Fast Closure & Reactor Scram Resulted.Caused by Erroneous High Vibration Signal from Faulty Shaft Rider Sensor Connection.Design Change Being Prepared
| | | 05000341/LER-1987-032, :on 870726,control Ctr HVAC Sys Shifted from Normal Operation to Chlorine Mode.Caused by Use of two-way Radio.Surveillance Procedure for Fire Detection Operability & Functional Test Revised |
- on 870726,control Ctr HVAC Sys Shifted from Normal Operation to Chlorine Mode.Caused by Use of two-way Radio.Surveillance Procedure for Fire Detection Operability & Functional Test Revised
| | | 05000341/LER-1987-033, :on 870729,RWCU Containment Isolation Valve Closed Due to High Effluent Temp.Caused by Personnel Error & Failure of Alarms to Annunciate.Operator Disciplined & Investigation Into Alarm Failure Will Be Made |
- on 870729,RWCU Containment Isolation Valve Closed Due to High Effluent Temp.Caused by Personnel Error & Failure of Alarms to Annunciate.Operator Disciplined & Investigation Into Alarm Failure Will Be Made
| | | 05000341/LER-1987-034, :on 870730,scheduling of Fire Brigade Practices Discovered to Be Inconsistent W/Operation Procedures.Caused by Misinterpretation of Training Schedule.Fire Protection Program Will Be Rewritten |
- on 870730,scheduling of Fire Brigade Practices Discovered to Be Inconsistent W/Operation Procedures.Caused by Misinterpretation of Training Schedule.Fire Protection Program Will Be Rewritten
| | | 05000341/LER-1987-035, :on 870731,reactor Shutdown Initiated Due to Excessive Primary Containment Valve Leakage.Caused by Random Component Failure & Reactor Power Level Increase.Check Valve Repaired.Addl Training Will Be Administered |
- on 870731,reactor Shutdown Initiated Due to Excessive Primary Containment Valve Leakage.Caused by Random Component Failure & Reactor Power Level Increase.Check Valve Repaired.Addl Training Will Be Administered
| | | 05000341/LER-1987-036, :on 870802,improper Valve Line Up During Fill & Vent Operation of RHR Caused Reactor Water to Divert from Reactor Vessel to Suppression Pool Causing Reactor Scram to Occur.Caused by Operator Error |
- on 870802,improper Valve Line Up During Fill & Vent Operation of RHR Caused Reactor Water to Divert from Reactor Vessel to Suppression Pool Causing Reactor Scram to Occur.Caused by Operator Error
| | | 05000341/LER-1987-037, :on 870804,inadvertent Closure of Inboard MSIVs Occurred During Transfer of Reactor Protection Sys Bus Power Sources.Caused by Inadequate Procedure.Procedure Revised to Require Energization of Ac Solenoids |
- on 870804,inadvertent Closure of Inboard MSIVs Occurred During Transfer of Reactor Protection Sys Bus Power Sources.Caused by Inadequate Procedure.Procedure Revised to Require Energization of Ac Solenoids
| | | 05000341/LER-1987-038, :on 870815,automatic Initiation of Div I Emergency Equipment Cooling Water (EECW) Occurred.Caused by Inadequate Sys Design for Pressure compensation.Motor- Operated Valves Installed to EECW Makeup Tanks |
- on 870815,automatic Initiation of Div I Emergency Equipment Cooling Water (EECW) Occurred.Caused by Inadequate Sys Design for Pressure compensation.Motor- Operated Valves Installed to EECW Makeup Tanks
| | | 05000341/LER-1987-039, :on 870807,backup Manual Scram Breaker a Failed to Trip.Caused by Inadequate Instruction & Poor Work Practices by Plant Personnel.Breaker Tested for Normal Trip Function & Replaced |
- on 870807,backup Manual Scram Breaker a Failed to Trip.Caused by Inadequate Instruction & Poor Work Practices by Plant Personnel.Breaker Tested for Normal Trip Function & Replaced
| | | 05000341/LER-1987-040, :on 870827,reactor Protection Sys (RPS) motor- Generator Set Tripped Causing Loss of Power to RPS Bus a & Div I Isolation Signal.Cause Not Determined.Poteniometer Will Be Cleaned on Regular Basis |
- on 870827,reactor Protection Sys (RPS) motor- Generator Set Tripped Causing Loss of Power to RPS Bus a & Div I Isolation Signal.Cause Not Determined.Poteniometer Will Be Cleaned on Regular Basis
| | | 05000341/LER-1987-041, :on 870329,accident Range Monitor Inoperable. Caused by Inadequate Sys Turn Over Following Preoperational Testing.Channel Parameters Will Be Verified Daily & Tech Spec Interpretation Issued |
- on 870329,accident Range Monitor Inoperable. Caused by Inadequate Sys Turn Over Following Preoperational Testing.Channel Parameters Will Be Verified Daily & Tech Spec Interpretation Issued
| | | 05000341/LER-1987-042, :on 870902,control Ctr HVAC Sys Shifted to Chlorine Mode W/No Chlorine Present.Cause Unknown. Availability & Design of Less Radio Frequency Sensitive Detectors Under Study.Radio Use Restricted |
- on 870902,control Ctr HVAC Sys Shifted to Chlorine Mode W/No Chlorine Present.Cause Unknown. Availability & Design of Less Radio Frequency Sensitive Detectors Under Study.Radio Use Restricted
| | | 05000341/LER-1987-043-01, :on 870902,control Ctr HVAC Sys Shifted from Normal to Recirculation Mode.Investigation Continuing to Determine Cause of Event.Corrective Actions Will Be Based on Results of Investigation |
- on 870902,control Ctr HVAC Sys Shifted from Normal to Recirculation Mode.Investigation Continuing to Determine Cause of Event.Corrective Actions Will Be Based on Results of Investigation
| | | 05000341/LER-1987-044, :on 870903,discovered That 82 Test,Vent & Drain Connections & 5 Bonnet Taps Not Verified Closed Per Tech Spec.Caused by Inadequate Containment Integrity Surveillance Procedures.Procedures Revised |
- on 870903,discovered That 82 Test,Vent & Drain Connections & 5 Bonnet Taps Not Verified Closed Per Tech Spec.Caused by Inadequate Containment Integrity Surveillance Procedures.Procedures Revised
| | | 05000341/LER-1987-045, :on 870908,fuse Removed Resulting in Loss of Dc Control Power Causing Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves.Caused by Personnel Error.Dc Control Circuitry for Bus 72C Redesigned |
- on 870908,fuse Removed Resulting in Loss of Dc Control Power Causing Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves.Caused by Personnel Error.Dc Control Circuitry for Bus 72C Redesigned
| | | 05000341/LER-1987-046, :on 870820,identified Deficiencies in Raychem Installations.Caused by Inadequacies in Training of Raychem Installers,Lack of Insp Requirement & Previous Specification Deficiencies.Installations Repaired & Replaced |
- on 870820,identified Deficiencies in Raychem Installations.Caused by Inadequacies in Training of Raychem Installers,Lack of Insp Requirement & Previous Specification Deficiencies.Installations Repaired & Replaced
| | | 05000341/LER-1987-047, :on 870918,discovered That Div I of Control Ctr HVAC Chiller Pump & Valve Operability Surveillance Had Not Been Completed by Critical Completion Date.Caused by Inadequate Training of Operators |
- on 870918,discovered That Div I of Control Ctr HVAC Chiller Pump & Valve Operability Surveillance Had Not Been Completed by Critical Completion Date.Caused by Inadequate Training of Operators
| | | 05000341/LER-1987-048, :on 871008,channel Check for Reactor Protection Sys Drywell High Pressure Instrumentation Omitted in Surveillance Procedure.Caused by Incomplete Surveillance Procedure.Procedure Revised |
- on 871008,channel Check for Reactor Protection Sys Drywell High Pressure Instrumentation Omitted in Surveillance Procedure.Caused by Incomplete Surveillance Procedure.Procedure Revised
| | | 05000341/LER-1987-049, :on 870925,three Deficiencies Identified in Fire Protection Program.Cause Not Stated.Fire Brigade Training Program Revised,Valve Locked Into Position, Procedure Revised & Training Classes Held |
- on 870925,three Deficiencies Identified in Fire Protection Program.Cause Not Stated.Fire Brigade Training Program Revised,Valve Locked Into Position, Procedure Revised & Training Classes Held
| | | 05000341/LER-1987-050, :on 870821,discovered RWCU Sys Operating Procedure Allowed RWCU HX to Be Placed in Bypass When Reactor Coolant Temp Reached 544 F.Caused by Failure of Engineering Dept to Identify Limitation |
- on 870821,discovered RWCU Sys Operating Procedure Allowed RWCU HX to Be Placed in Bypass When Reactor Coolant Temp Reached 544 F.Caused by Failure of Engineering Dept to Identify Limitation
| | | 05000341/LER-1987-051, :on 870929,differential Pressure Actuation of Emergency Equipment Cooling Water Occurred.Caused by Design Deficiency in Reactor Bldg Closed Cooling Water Sys.Time Delay on Pressure Switches Lengthened |
- on 870929,differential Pressure Actuation of Emergency Equipment Cooling Water Occurred.Caused by Design Deficiency in Reactor Bldg Closed Cooling Water Sys.Time Delay on Pressure Switches Lengthened
| | | 05000341/LER-1987-052, :on 871017,determined Violation of Primary Containment Integrity May Have Occurred.Caused by Lack of Communication Between Util & Nrc.Temporary Exemption from GDC 56 Applied for & Verbally Granted |
- on 871017,determined Violation of Primary Containment Integrity May Have Occurred.Caused by Lack of Communication Between Util & Nrc.Temporary Exemption from GDC 56 Applied for & Verbally Granted
| | | 05000341/LER-1987-053, :on 871024,2 H Tech Spec Time Constraint for Allowing Instrument Channel to Be Inoperable Exceeded. Caused by Personnel Error.Checklist Developed as Guide for Performing Surveillance Procedure 44.020.015 |
- on 871024,2 H Tech Spec Time Constraint for Allowing Instrument Channel to Be Inoperable Exceeded. Caused by Personnel Error.Checklist Developed as Guide for Performing Surveillance Procedure 44.020.015
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