ENS 54599
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ENS Event | |
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14:13 Mar 23, 2020 | |
Title | Automatic Reactor Trip |
Event Description | On March 23, 2020, at 1013 EDT, with Harris Nuclear Plant Unit 1 in Mode 1, at 100 percent power, an unplanned actuation of the reactor protection system occurred. This resulted in an automatic reactor trip. The trip occurred during the restoration of the auto-stop turbine trip function during a planned maintenance evolution.
All safety systems functioned as expected. Auxiliary Feedwater started as designed and was secured. Steam generator levels are being maintained by normal feedwater through the feedwater regulator bypass valves. Decay heat is being removed by using the condenser steam dump flow path. Due to the unplanned Reactor Protection System actuation while critical and the expected Auxiliary Feedwater actuation, this event is being reported as a four hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
Where | |
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Harris North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-0.62 h-0.0258 days <br />-0.00369 weeks <br />-8.49276e-4 months <br />) | |
Opened: | Adam Zimandy 13:36 Mar 23, 2020 |
NRC Officer: | Ossy Font |
Last Updated: | Mar 23, 2020 |
54599 - NRC Website
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WEEKMONTHYEARENS 571552024-05-30T23:49:00030 May 2024 23:49:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 561892022-10-30T10:53:00030 October 2022 10:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip and Auxiliary Feedwater System Actuation ENS 560752022-08-28T07:29:00028 August 2022 07:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Auxiliary Feedwater System Actuation ENS 558682022-04-29T08:05:00029 April 2022 08:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Auxiliary Feedwater System Actuation ENS 550382020-12-16T13:51:00016 December 2020 13:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Generator Lockout ENS 548342020-08-13T13:38:00013 August 2020 13:38:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Dropped Control Rod ENS 545992020-03-23T14:13:00023 March 2020 14:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 522892016-10-08T05:50:0008 October 2016 05:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unplanned Reactor Trip and Safety Injection Due to Turbine Control Valve Transient ENS 454992009-11-16T03:42:00016 November 2009 03:42:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Main Generator Oil Leak ENS 444042008-08-11T04:49:00011 August 2008 04:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Degrading Condenser Vacuum ENS 436762007-09-29T02:32:00029 September 2007 02:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of a Startup Transformer ENS 428482006-09-19T14:00:00019 September 2006 14:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Generator Lockout Signal ENS 416542005-05-01T04:21:0001 May 2005 04:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Condensate Pump ENS 407302004-05-06T16:52:0006 May 2004 16:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip and Actuation of Auxiliary Feedwater System ENS 400842003-08-17T19:51:00017 August 2003 19:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of "a" Condensate Pump. 2024-05-30T23:49:00 | |
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