ENS 45499
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ENS Event | |
---|---|
03:42 Nov 16, 2009 | |
Title | Manual Reactor Trip Due to Main Generator Oil Leak |
Event Description | At 2242 [EST] on 11/15/09, the reactor was manually scrammed from 100% power due to a large oil leak on the main generator seal oil system. Condenser vacuum was broken immediately following the reactor trip, and the main turbine stopped rotating at 2324 [EST]. Following the reactor trip, the 'B' steam generator Main Steam Isolation Valve (MSIV) failed to fully close on demand, but was closed due to field actions at 2303 [EST]. The reactor remained stable at NOP/NOT following the reactor trip. Offsite power remained available throughout the event.
This condition is being reported as actuation of the reactor protection system in accordance with 10CFR 50.72(b)(2)(iv)(B). All control rods fully inserted and decay heat is being removed through the S/G relief valves to the atmospheric dumps. No known primary to secondary leakage exists. The plant remains stable in Mode 3. The licensee notified the NRC Resident Inspector. |
Where | |
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Harris North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-1.3 h-0.0542 days <br />-0.00774 weeks <br />-0.00178 months <br />) | |
Opened: | Lewis Rogers 02:24 Nov 16, 2009 |
NRC Officer: | Dong Park |
Last Updated: | Nov 16, 2009 |
45499 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 571552024-05-30T23:49:00030 May 2024 23:49:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 561892022-10-30T10:53:00030 October 2022 10:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip and Auxiliary Feedwater System Actuation ENS 560752022-08-28T07:29:00028 August 2022 07:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Auxiliary Feedwater System Actuation ENS 558682022-04-29T08:05:00029 April 2022 08:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Auxiliary Feedwater System Actuation ENS 550382020-12-16T13:51:00016 December 2020 13:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Generator Lockout ENS 548342020-08-13T13:38:00013 August 2020 13:38:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Dropped Control Rod ENS 545992020-03-23T14:13:00023 March 2020 14:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 522892016-10-08T05:50:0008 October 2016 05:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unplanned Reactor Trip and Safety Injection Due to Turbine Control Valve Transient ENS 454992009-11-16T03:42:00016 November 2009 03:42:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Main Generator Oil Leak ENS 444042008-08-11T04:49:00011 August 2008 04:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Degrading Condenser Vacuum ENS 436762007-09-29T02:32:00029 September 2007 02:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of a Startup Transformer ENS 428482006-09-19T14:00:00019 September 2006 14:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Generator Lockout Signal ENS 416542005-05-01T04:21:0001 May 2005 04:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Condensate Pump ENS 407302004-05-06T16:52:0006 May 2004 16:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip and Actuation of Auxiliary Feedwater System ENS 400842003-08-17T19:51:00017 August 2003 19:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of "a" Condensate Pump. 2024-05-30T23:49:00 | |
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