ENS 44404
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ENS Event | |
---|---|
04:49 Aug 11, 2008 | |
Title | Manual Reactor Trip Due to Degrading Condenser Vacuum |
Event Description | At 0049 EDT on 8/11/2008, the Harris Nuclear Plant was manually scrammed from 21% power due to indications of degrading condenser vacuum. At the time, a reactor shutdown was in progress with indications of a degraded condenser boot seal. The unit was stabilized in Mode 3 with no additional equipment failures or other complications.
The reactor is currently at normal operating pressure and temperature. The highest vacuum observed was 8". All rods inserted into the core after the manual trip. Auxiliary feed water did not start as a result of the trip. Steam generator level is being maintained via normal feed water flow path. Decay heat is being removed via the steam dumps to atmosphere. There is no known primary to secondary leakage. No power-operated or manual reliefs lifted during the transient. The grid is stable and loads are being supplied via the station start-up transformer. The licensee has notified the NRC Resident Inspector. |
Where | |
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Harris North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-0.47 h-0.0196 days <br />-0.0028 weeks <br />-6.43806e-4 months <br />) | |
Opened: | Scott Faulkner 04:21 Aug 11, 2008 |
NRC Officer: | Howie Crouch |
Last Updated: | Aug 11, 2008 |
44404 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (21 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 571552024-05-30T23:49:00030 May 2024 23:49:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 561892022-10-30T10:53:00030 October 2022 10:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip and Auxiliary Feedwater System Actuation ENS 560752022-08-28T07:29:00028 August 2022 07:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Auxiliary Feedwater System Actuation ENS 558682022-04-29T08:05:00029 April 2022 08:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Auxiliary Feedwater System Actuation ENS 550382020-12-16T13:51:00016 December 2020 13:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Generator Lockout ENS 548342020-08-13T13:38:00013 August 2020 13:38:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Dropped Control Rod ENS 545992020-03-23T14:13:00023 March 2020 14:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 522892016-10-08T05:50:0008 October 2016 05:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unplanned Reactor Trip and Safety Injection Due to Turbine Control Valve Transient ENS 454992009-11-16T03:42:00016 November 2009 03:42:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Main Generator Oil Leak ENS 444042008-08-11T04:49:00011 August 2008 04:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Degrading Condenser Vacuum ENS 436762007-09-29T02:32:00029 September 2007 02:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of a Startup Transformer ENS 428482006-09-19T14:00:00019 September 2006 14:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Generator Lockout Signal ENS 416542005-05-01T04:21:0001 May 2005 04:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Condensate Pump ENS 407302004-05-06T16:52:0006 May 2004 16:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip and Actuation of Auxiliary Feedwater System ENS 400842003-08-17T19:51:00017 August 2003 19:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of "a" Condensate Pump. 2024-05-30T23:49:00 | |
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