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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr 1990-01-08
[Table view] Category:RO)
MONTHYEARML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr 1990-01-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000461/LER-1999-010-01, Inoperability of Div 2 EDG Caused by Fuel Leaking Into Lube Oil, Cancelled1999-10-0707 October 1999 Inoperability of Div 2 EDG Caused by Fuel Leaking Into Lube Oil, Cancelled U-603277, Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers 05000461/LER-1998-020, :on 980609,inadequate Flow Balancing of Shutdown Water Sys Resulted in Less than Required Flow to Water Sys Loads.Caused by Inadequate Initial Design.New SX Min Flow Path for Div I & II SX Pumps Has Been Established1999-09-14014 September 1999
- on 980609,inadequate Flow Balancing of Shutdown Water Sys Resulted in Less than Required Flow to Water Sys Loads.Caused by Inadequate Initial Design.New SX Min Flow Path for Div I & II SX Pumps Has Been Established
05000461/LER-1996-010, :on 960906,plant Shutdown Occurred Due to Unidentified RCS Leakage from Degraded Reactor Recirculation Pump Seal Greater than TS Limit.Procedures Will Be Revised, Failed Seal Will Be Replaced & Seal Design Will Be Improved1999-09-13013 September 1999
- on 960906,plant Shutdown Occurred Due to Unidentified RCS Leakage from Degraded Reactor Recirculation Pump Seal Greater than TS Limit.Procedures Will Be Revised, Failed Seal Will Be Replaced & Seal Design Will Be Improved
05000461/LER-1999-011, :on 990816,improper Restoration of a APRM Caused Monitor to Not Meet Seismic Qualification Requirements.Caused by Lack of Knowledge.Page Latches for Other APRMs Were Inspected & No Anomolies Were Found1999-09-10010 September 1999
- on 990816,improper Restoration of a APRM Caused Monitor to Not Meet Seismic Qualification Requirements.Caused by Lack of Knowledge.Page Latches for Other APRMs Were Inspected & No Anomolies Were Found
05000461/LER-1999-010, :on 990809,declared Div 2 EDG Inoperable Due to Fuel Leaking Into Lube Oil.Replaced Fuel Return Line from Engine Number 12 Cylinder on Div 2 Edg.With1999-09-0808 September 1999
- on 990809,declared Div 2 EDG Inoperable Due to Fuel Leaking Into Lube Oil.Replaced Fuel Return Line from Engine Number 12 Cylinder on Div 2 Edg.With
U-603267, Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With U-603245, Monthly Operating Rept for Jul 1999 for CPS Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for Jul 1999 for CPS Unit 1.With ML20211C9621999-07-26026 July 1999 ISI Summary Rept 05000461/LER-1999-009, :on 990617,failure to Satisfy Secondary Containment Bypass Leakage Rate TS Was Noted.Caused by Failure to Properly Classify Containment Penetrations. Procedures Revised.With1999-07-15015 July 1999
- on 990617,failure to Satisfy Secondary Containment Bypass Leakage Rate TS Was Noted.Caused by Failure to Properly Classify Containment Penetrations. Procedures Revised.With
U-603232, Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted1999-07-0909 July 1999 Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted U-603233, Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With U-603222, Monthly Operating Rept for May 1999 for Clinton Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Clinton Power Station.With 05000461/LER-1999-006, :on 990419,values Used for Containment & Drywell Free Vols Found to Be Smaller than Originally Analyzed Due to Inadequate Calculation Control During Initial Plant Const.With 9905517 Ltr1999-05-17017 May 1999
- on 990419,values Used for Containment & Drywell Free Vols Found to Be Smaller than Originally Analyzed Due to Inadequate Calculation Control During Initial Plant Const.With 9905517 Ltr
05000461/LER-1998-014-01, Design Failure Analysis for FW Piping Does Not Match Fatigue Analysis for FW Nozzles Resulting in Condition Outside of Design Basis for Plant, Has Been Cancelled1999-05-13013 May 1999 Design Failure Analysis for FW Piping Does Not Match Fatigue Analysis for FW Nozzles Resulting in Condition Outside of Design Basis for Plant, Has Been Cancelled ML20210K8391999-05-11011 May 1999 British Energy Annual Rept & Accounts 1998-99 ML20206H1231999-05-0505 May 1999 Illinois Power Co CPS Main CR Simulator Certification Rept U-603204, Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR211999-04-30030 April 1999 Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR21 U-603210, Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With 05000461/LER-1998-030-01, Insufficient Suppression Pool Makeup Volume to Meet Design Basis Suppression Pool Level Requirements Following LOCA, Has Been Cancelled1999-04-19019 April 1999 Insufficient Suppression Pool Makeup Volume to Meet Design Basis Suppression Pool Level Requirements Following LOCA, Has Been Cancelled U-603192, Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With ML20205D3861999-03-26026 March 1999 Safety Evaluation Supporting Amend 122 to License NPF-62 U-603182, Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue1999-03-12012 March 1999 Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue ML20207H0201999-03-0808 March 1999 Safety Evaluation Supporting Amend 121 to License NPF-62 U-603176, Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With 05000461/LER-1999-004, :on 990126,plant Was Operating Outside Design Basis.Caused Because Design for CR Operator Dose Calculation Did Not Consider Single Failure of CR Ventilation Sys. Revised CR Operator Dose Calculation.With1999-02-25025 February 1999
- on 990126,plant Was Operating Outside Design Basis.Caused Because Design for CR Operator Dose Calculation Did Not Consider Single Failure of CR Ventilation Sys. Revised CR Operator Dose Calculation.With
ML20207F2031999-02-10010 February 1999 Rev 1 to CPS COLR for Reload 6 Cycle 7 05000461/LER-1999-002, :on 990106,loss of Offsite Power to SR Electrical Buses Was Noted.Caused by Offsite Fault on in Service Offsite Electrical Supply Line.Repairs Were Made to Faulted Line & Leaning Support Structure.With1999-02-0404 February 1999
- on 990106,loss of Offsite Power to SR Electrical Buses Was Noted.Caused by Offsite Fault on in Service Offsite Electrical Supply Line.Repairs Were Made to Faulted Line & Leaning Support Structure.With
ML20202J0181999-02-0303 February 1999 SER Accepting Changes in Quality Assurance Program,Which Continues to Meet Requirements of App B to 10CFR50 ML20199L3581999-01-20020 January 1999 Safety Evaluation Supporting Amend 120 to License NPF-62 ML20199L3871999-01-20020 January 1999 Safety Evaluation Supporting Amend 119 to License NPF-62 U-603223, Illinova Corp 1998 Annual Rept. with1998-12-31031 December 1998 Illinova Corp 1998 Annual Rept. with U-603144, Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With U-603115, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components1998-12-0404 December 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components U-603124, Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With U-603114, Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor1998-11-25025 November 1998 Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor 05000461/LER-1998-036, :on 981018,loss of Shutdown Cooling Was Noted. Caused by Personnel Opening Incorrect Electrical Cubicle Door.Learning Opportunities Re Incorrect Cubicle Door Were Communicated to Personnel & Training Will Be Improved1998-11-17017 November 1998
- on 981018,loss of Shutdown Cooling Was Noted. Caused by Personnel Opening Incorrect Electrical Cubicle Door.Learning Opportunities Re Incorrect Cubicle Door Were Communicated to Personnel & Training Will Be Improved
U-603103, Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With U-603101, Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site1998-10-28028 October 1998 Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site ML20154J0001998-10-0909 October 1998 Safety Evaluation Supporting Amend 117 to License NPF-62 ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves ML20154B6351998-10-0101 October 1998 Safety Evaluation Supporting Amend 116 to License NPF-62 U-603091, Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With ML20153F9871998-09-17017 September 1998 Safety Evaluation Accepting 980225 Proposed Rev 26 to Illinois Power Nuclear Program Qam ML20151U1391998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Clinton Power Station,Unit 1 ML20237E3991998-08-27027 August 1998 SER Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode, for Clinton Power Station ML20237D7041998-08-13013 August 1998 Safety Evaluation Supporting Amend 115 to License NPF-62 ML20237A1521998-08-0707 August 1998 SER Re Mgt Services Agreement at Clinton Power Station. Approval Under 10CFR50.80 Not Required ML20151Y6591998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Clinton Power Station,Unit 1 1999-09-08
[Table view] |
Text
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ILLINDIS POWER COMPANY .
l CLINTON POntR STATION. P.O. BOX 678. CLINTON. ILLINOIS 01727 ,
, i January 18, 1990 !
l i- 10CFR50.73 !
l l l l l
Docket No. 50 461' ,
U.S. Nuclear Regulatory Commission Document Control Desk
-Washington, D.C.- 20555
Subject:
Clinton Power Station - Unit 1 Licensee Event Recort No. 89 042 00
Dear Sir:
Please find enclosed Licensee Event Report No. 89 042-00:
Sensor System Desien Causes False Reactor Core Isolation Cooline (RCIC)
Steam Line Differential Pressure Hich Sirnal and RCIC Isolation. This report is being submitted'in accordance with the requirements of 10CFR50.73.
Sincerely yours,
% 2 /A ~
D. L. Iloltzscher Acting Manager -
Licensing and Safety TSA/krm l> Enclosure L cc: .NRC Resident Office.
NRC Region III, Regional Administrator INPO Records Center Illinois Department. of Nuclear Safety NRC Clinton Licensing Project Manager -/
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- UCENSEE EVENT REPORT (LER) Ec1"i#T" 'T"Gfo'i*o'fv"(*&"s'i,'MAit TO'ut ftc c n"oS
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" " ' ' ' ' Sensor System Design Causes False Reactor Core Isolation Cooling (RCIC) Steam lane Differential Pressure High Signal and RCIC Isolation EVit(T DAf t (61 LtR wuuttR t6l REPORT DAf t (71 OTHER 8 ACILITill INVOLVED 101 CONTM DAY vtAR vtAR Sigy 4, atjf,Q MONT u DAv ytAR ' AciLIT v aawts DOCRif NUM$t his)
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X Ji E F I TI I Rt3l6l9 N I i l l l l l l l I I I I I i ! ! I I I I SUPPLEMINT AL REPORT IXPECTIO Hel MONTH Day vtAR SU9M185f04 i tti Itt vee. temp,ere (APLCTio SUOe0tSSION OA Til NO l l l An u ACT ,t ne. , m ,- e..,#.e - .. e.,,nNee .y e ,s.v ,e . ,H i On December 19, 1989, at approximately 1555 hours0.018 days <br />0.432 hours <br />0.00257 weeks <br />5.916775e-4 months <br />, with the plant in Mode 1 (POWER OPERATION), at eighty-four percent reactor power, a false Reactor Core Isolation Cooling (RCIC) Division I steam line differential l pressure high signal caused valve IE51-F064, the RCIC turbine steam supply containment isolat'.on valve, to shut and the RCIC turbine to trip.
The cause of this event is attributed to the sensor system design. The system's sensitivity to minor changes in sensing line pressure resulted in the falso RCIC Division I steam line differential pressure high ,
( signal. The sensitivity of transmitter IE31 N084A was reduced by l implementing Field Alteration C F031 for that transmitter. At 2235 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.504175e-4 months <br />, on December 24, 1989, implementation of Field C F031 Alteration was completed for lE31 N084A, and RCIC was declared operable. This Field Alteration will be installed as necessary on other transmitters which exhibit similar sensitivity to minor changes in sensing line pressure.
- l. NRC Form 300 (6491 l~
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voci n--. . = anc , an w nri DESCRIPTION OF EVENT on December 19, 1989, at approximately 1555 hours0.018 days <br />0.432 hours <br />0.00257 weeks <br />5.916775e-4 months <br />, with the plant in Mode 1 (POWER OPERATION), at eighty four percent reactor [RCT) power, a false Reactor Core Isolation Cooling (RCIC) [BN) Division I steam line !
differential pressure high signal caused valve 1E51 F064, the RCIC l turbine [TRB] steam supply containment isolation valve (ISV), to shut *
(isolating RCIC) and the RCIC turbine to trip. ;
control room operators immediately verified that valve 1E51*F031, the RCIC pump [P) suppression pool suction 1.olation valve, was closed and that the RCIC Division I steam line differential pressure' high
At 1615 hours0.0187 days <br />0.449 hours <br />0.00267 weeks <br />6.145075e-4 months <br />, operators attempted to restore steam to RCIC by opening valve 1E51 F064 and then opening valves 1E51-F025 and 1E51 F026, the RCIC steam supply condensate return control valves, locally. Operators checked the RCIC steam line flow ATMs and noted erratic readings, between
-30 and 20 inches of water, for 1E31 N684A and a zero reading for 1E31 N683A. Valve 1E51 F064 shut again on a false RCIC Division I steam line differential pressure high signal. ,
No additional attempts were made to open valve 1E51 F064 and restore steam to RCIC. A maintenance work request (MWR), D19199, was initiated to investigate and repair the cause of the RCIC isolation.
On December 21, 1989, Control and Instrumentation (C&I) technicians began investigating the isolation in accordance with MWR D19199, The investigation determined that the isolation was caused by the sensitivity of steam line flow transmitter [FT) 1E31 N084A to minor changes in sensing line pressure.
i on December 22, 1989, C&I to:hnicians replaced the amplifier [ AMP) and calibration cards in transmitter 1E31 N084A in accordance with Field Alteration C-F031 and Field Engineering Change Notice (FECN) 24557. The new cards have an adjustable inherent time delay which reduces the sensitivity of the transmitter. At 2235 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.504175e-4 months <br />, on December 24, 1989, implementation of Field Alteration C F031 was completed for 1E31-N084A, !
and RCIC was declared operable.
l No automatic or manually initiated safety system responses were necessary to place the plant in a safe and stable condition. No equipment or -
components were inoperable at the start of this event such that their inoperable condition contributed to this event.
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- - 0F 0l3 CAUSE OF EVENT The cause of this event is attributed to the sensor system design. The system's sensitivity to minor changes in sensing line pressure resulted in the false RCIC Livision I steam line differential pressure high signal.
CORRECTIVE ACTION The sensitivity of transmitter 1E31 N084A was reduced by implementing Field Alterction C F031 for that transmitter.
This Field Alteration allows for the installation of the adjustable time delay feature on other transmitters which exhibit sensitivity to minor changes in sensing line pressure. This Field Alteration will be installed as the affected systems become available for work.
ANALYSIS OF EVENT Assessment of the safety consequences and implications of this event indicates that this event was not nuclear safety significant. The RCIC system isolated as designed, in response to the RCIC Division I steam line differential pressure high signal. The liigh Pressure Core Spray (llPCS) system [BG), the alternate means of providing reactor core cooling under high reactor pressure vessel pressure conditions, was available at the time of this event.
This event is reportable under the provisions of 10CFR50.73(a)(2)(iv) because of an automatic isolation of the RCIC system. RCIC was isolated and inoperable from 1555 hours0.018 days <br />0.432 hours <br />0.00257 weeks <br />5.916775e-4 months <br /> on December 19, 1989 until 2235 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.504175e-4 months <br /> on December 24, 1989.
ADDITIONAL INFORMATION The flow transmitter discussed in this LER is a model number 1153DBSPC manufactured by Rosemount, Incorporated.
LER 88 022 01 discusses an HPCS initiation caused by an oversensitive reactor pressure vessel water level transmitter resulting from the sensor system design.
LER 87 052-00 discusses an RCIC isolation caused by personnel error while investigating erratic readings on the Division II RCIC steam flow indication, j
for further information regarding this event, contact R. D. Freeman, Manager - Nuclear Station Engineering Department at (217) 935 8881, extension 3538.
l N "" " e U 8 Gro 1606+434486/466