SCH08-032, Quarterly Remedial Action Progress Report, Fourth Quarter 2007 PSEG Nuclear, LLC, Salem Generating Station

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Quarterly Remedial Action Progress Report, Fourth Quarter 2007 PSEG Nuclear, LLC, Salem Generating Station
ML080930203
Person / Time
Site: Salem  PSEG icon.png
Issue date: 03/25/2008
From: Suey G
Public Service Enterprise Group
To: Tuccillo K
Office of Nuclear Reactor Regulation, State of NJ, Dept of Environmental Protection, Bureau of Nuclear Engineering
References
SCH08-032
Download: ML080930203 (90)


Text

PSEG Nuclear LLC P.O. Box 236, Hancock Bridge, NJ 08038-0236 CERTIFIED MAIL 0 PSEG Nuclear LLC March 25, 2008 " .2 ,/I7 SCH08-032 Karen Tuccillo Radiation Protection Programs Bureau of Nuclear Engineering New Jersey Department of Environmental Protection 33 Arctic Parkway Trenton, New Jersey 08625 QUARTERLY REMEDIAL ACTION PROGRESS REPORT, FOURTH QUARTER 2007 PSEG NUCLEAR, LLC, SALEM GENERATING STATION

Dear Ms. Tuccillo:

PSEG Nuclear LLC (PSEG) has prepared this Quarterly Remedial Action Progress Report (RAPR) summarizing groundwater remediation activities performed in 2007 including activities performed since the submission of the previous RAPR in December 2007 at the PSEG Nuclear, LLC, Salem Generating Station (Station).

The Station is located on Artificial Island in Hancock's Bridge, Salem County, New Jersey.Groundwater remediation activities are being conducted to address tritium detected in shallow groundwater adjacent to and south of the Salem Unit 1 Reactor Containment and Fuel Handling Building.

The Station site plan is depicted in Figure 1.The release of tritium contaminated water to the environment ceased in February 2003 when the Salem Unit 1 telltale drains were cleared and the Spent Fuel Pool (SFP) water that had accumulated behind the liner was drained. Following draining activities, a regular program was instituted whereby the telltale drains are monitored for flow and the seismic gap is continuously drained.Short-lived gamma-emitting radioisotopes, which are associated with site operations, had not been consistently detected in groundwater collected from the seismic gap since May 2004 until recently.

Since May 2007 cobalt 58 (Co-58) has been sporadically detected in groundwater collected from within the seismic gap. However, short-lived gamma-emitting radioisotopes have not been detected and tritium concentrations have continued to decline in groundwater collected outside of the seismic gap indicating that current draining protocols are adequately capturing groundwater.

At present, it is estimated that the previous estimate of 2 to 5 Curies of tritium in the plume where it exists above the NJDEP Ground Water Quality Criteria (GWQC) has been reduced by approximately 0.6 Curies since the first quarter of 2006. The range is.W dependant on the amount of tritium drawn back through the seismic gap, the actual degree of variability in the tritium concentrations of the groundwater, and the amount of mass held in dead end pore space.The following sections present the background of environmental investigation and remedial action at the site, the details and results of activities conducted since the submittal of the December 2007 RAPR, the progress of remedial actions conducted to date, and provide a discussion of upcoming activities projected for the next reporting period.1 Project Background In April 2004, a Remedial Investigation Report (RIR) was submitted to the New Jersey Department of Environmental Protection Bureau of Nuclear Engineering (NJDEP-BNE) presenting the details and results of a groundwater investigation conducted following the discovery of tritium in groundwater adjacent to Salem Unit 1. The results of the remedial investigation indicated that the source of tritium detected in groundwater was the Spent Fuel Pool, the tritium release to the environment had been stopped, and that tritium had not migrated to the property boundary above the New Jersey GWQC.Based on the results of the remedial investigation a remedial action strategy was developed to hydraulically limit further migration and reduce the concentration of tritium remaining in groundwater adjacent to Salem Unit 1. In April 2004, PSEG initiated a pilot* study designed to demonstrate the effectiveness of groundwater extraction for achieving remedial objectives.

The pilot study proved to be effective, and in July 2004, a Remedial Action Work Plan (RAWP) proposing the operation of a full-scale groundwater extraction system was prepared and submitted to the NJDEP-BN.

The RAWP was approved by the NJDEP-BNE in November 2004 and a full-scale groundwater extraction system was subsequently installed.

Further, in September 2005, weekly draining of the Unit I seismic gap was initiated to ensure that the flow of water entering the seismic gap was directed toward the interior of the building for treatment rather than outward toward the environment.

Continuous draining of the Unit 1 seismic gap was initiated in late February 2007.2 Continued Groundwater Monitoring Groundwater monitoring activities continued through this reporting period in accordance with the schedule provided to NJDEP-BNE.

The sampling program is designed to provide representative data necessary to evaluate plume containment.

Monitoring activities include the periodic collection of groundwater samples from the 36 Station monitoring wells. A summary of monitoring well construction details is presented in Table 1. Monitoring well locations are depicted on Figure 1.*1 Groundwater samples are initially submitted to Salem Chemistry for analysis for tritium and short-lived gamma-emitting radioisotopes.

Samples indicating tritium 2 concentrations less than 50,000 picocuries per liter (pCi/L) are sent to Maplewood Testing Services for more refined analysis.Historical and current analytical data indicate that plant related gamma-emitting radioisotopes have not been detected in groundwater from any monitoring well since monitoring was initiated in 2003. Detailed historic analytical radioisotope groundwater results were presented in the previously submitted RIR and RAPRs and are not presented herein.Historical analytical tritium results for groundwater collected from the Station monitoring wells are presented on Figure 1 and Table 2. Included on Figure 1 are: panel 1) the extent of tritium in groundwater at the completion of the remedial investigation (Baseline Plume); panel 2) the extent of tritium in groundwater one year ago in December 2006;and, panel 3) the extent of tritium in groundwater in December 2007. Based on a review of Figure 1, it is apparent that the mass of tritium in groundwater has been significantly reduced by the remedial efforts occurring at the site. Details regarding these activities are discussed below.The analytical results for groundwater samples collected from the monitoring wells were evaluated based on the water-bearing zone in which they are screened.

The three primary water-bearing units investigated beneath the Station are: 1) the Vincentown Formation;

2) the shallow water-bearing unit within the limits of the cofferdam surrounding Salem Unit 1; and, 3) the shallow, water-bearing unit outside the limits of the cofferdam.

2.1 Tritium Analytical Results for the Vincentown Formation The following wells are screened in the Vincentown Formation:

Well V, Well K, Well L, Well P, Well Q, and, Well CB. Groundwater quality for Well K, Well L, Well P, and Well Q is currently monitored on a semi-annual basis. Groundwater quality for Well V and Well CB is currently monitored on a quarterly and monthly basis, respectively.

Tritium has consistently not been detected above laboratory detection limits or detected at relatively low levels in groundwater at all monitoring wells screened within the Vincentown formation since the initiation of monitoring at these locations.

The groundwater monitoring results continue to indicate that the previous release of tritium impacted water from the SFP has not significantly migrated below the shallow water-bearing unit.2.2 Tritium Analytical Results for Wells Installed Within the Limits of the Cofferdam The following wells are screened in the shallow, water-bearing unit within the limits of the cofferdam:

Well M, Well N, Well 0, Well R, Well AC, Well AE, Well Al, Well AM, 3 Well AN, and Well AO. Groundwater quality for these wells is currently monitored on a monthly basis. However, Well AO has been inaccessible due to site constraints and has not been sampled since January 2007.Groundwater collected from Well AC, Well AM, and Well AN exhibit the highest concentrations of tritium at the Site, likely due to their location relative to the previous release from the Salem Unit 1 seismic gap. However, groundwater at these wells exhibits general decreasing temporal tritium concentration trends since the initiation of monitoring in 2003. For instance, tritium concentrations at Well AC, located directly southeast of the Salem Unit 1 seismic gap, have steadily declined from a maximum of 15,000,000 pCi/L in April 2003 to 53,500 pCi/L during the most recent sampling event in December 2007. Further, the decrease in tritium concentrations at Well AC is additional confirmation that tritium impacted groundwater is no longer being released from the seismic gap and the remedial groundwater recovery system is effectively reducing concentrations of previously released tritium. Well AM exhibits fluctuating concentrations which continue to be addressed using the mobile groundwater extraction unit. The mobile unit has previously been used with success at this and other wells to remediate localized portions of the tritium plume and will continue to be used in this manner.Tritium concentrations at Well 0 are typically below GWQC. However, some seasonal fluctuation is typically observed in this area. Fluctuations are believed to be associated with the changes. that occur in the plume as a result of seasonal variation in the groundwater flow patterns within this area.Tritium concentrations at Well M, Well N, Well R, Well AE, Well Al, and Well AO are below GWQC and generally show consistent declining temporal trends. Tritium concentrations at all well locations within the cofferdam have generally decreased by one order of magnitude or more since the initiation of monitoring, indicating that remedial activities are effectively removing mass from the areas of greatest concentration.

2.3 Tritium Analytical Results for Wells Installed Outside the Limits of the Cofferdam The wells installed in the shallow, water-bearing unit beyond the limits of the cofferdam are Well S, Well T, Well U, Well W, Well Y, Well Z, Well AA, Well AB, Well AD, Well AF, Well AG (Shallow and Deep), Well AH (Shallow and Deep), Well AJ, Well AL, Well AP, Well AQ, Well AR, Well AS, Well AT, and Well CA. These wells are screened either just above the clay confining unit that separates the shallow water-bearing unit from the Vincentown Formation, or in the interval indicating the highest tritium concentrations found in the shallow water-bearing unit at each boring location at the time of the Supplemental' Investigation completed in August 2003.4

  • As discussed in previous RAPRs, increased concentrations of tritium were detected in Wells W and AP in 2005. In response the mobile groundwater extraction unit was activated to spot remediate these wells. As a result, concentrations of tritium in groundwater at these well locations exhibited a general downward temporal trend.Tritium concentrations at these wells are currently below the GWQC.Recently higher concentrations of tritium (around 80,000 pCiIL) have been observed in groundwater samples from Well AR these are believed to be associated with the higher concentrations observed in Well AM during May of 2006. These slightly elevated concentrations represent material not captured by the operation of the mobile groundwater recovery unit during the summer of 2006. The mobile unit was deployed to Well AR to capture this additional volume and as a resulting in decreased tritium concentrations.

Tritium concentration trends for wells screened in the shallow, water-bearing unit indicate that the groundwater extraction system has demonstrated the ability to achieve the remedial action objectives (i.e., reduce the mass of tritium in groundwater, and maintain hydraulic control).

The current distribution of tritium in groundwater (December 2007) is presented on Figure 1, along with the distribution of tritium prior to the initiation of the pilot study (March 2004) and in December 2006. As shown on Figure 1, the mass of tritium in groundwater has continued to decrease through the operation of the groundwater extraction pilot study system and operation of the full-scale system..3 Groundwater Extraction Groundwater extraction as a remedial strategy at the site was initiated with the operation of a pilot test from April 2004 to February 2005. In accordance with the RAWF' developed for the site, a full-scale groundwater recovery system (GRS) was subsequently implemented in February 2005 and has continued to operate to the present.3.1 Full-Scale System The objectives of the full-scale GRS consist of: 1) maintaining hydraulic containment of the tritium plume; and, 2) reducing tritium concentrations in groundwater.

The present operation of the GRS consists of groundwater extraction from Wells AB, AD, AJ, AN, AS, and AT. Well. S is not currently operating and has not been. in operation during 2006 or 2007 as a result of its low yield and resulting pump failures.Groundwater extracted from the wells is processed in accordance with the Station's United States Nuclear Regulatory Commission (USNRC) license and plant procedures.

Details of the extracted effluent are discussed below.3.2 Mobile Groundwater Recovery Unit 5 The mobile groundwater recovery unit was designed and built to target specific areas of the plume exhibiting greater tritium activity.

The mobile unit typically operates between March and November (weather permitting).

The mobile unit collects water in nominal 1,000 gallon batches for handling in accordance with the station's permits. The mobile unit has historically been used successfully at Wells AP and AM. Recently it has operated at Wells AR and AM which have shown relatively elevated concentrations with respect to the remainder of the plume 3.3 Total System Effluent Data and Evaluation The GRS became operational on February 16, 2005. The system operated in various configurations as part of the optimization process for approximately the first month. The GRS discharges continuously in accordance with the Station's USNRC permit allowing the GRS to be more effective and efficient than the pilot-scale system. As of December 31, 2007, the GRS has recovered greater than 17 million gallons of groundwater.

This is equivalent to an average .recovery rate of approximately 12 gallons per minute or greater than 17 times the recharge rate for the extraction area (calculated to be 0.7 gallons per minute, based upon an assumed percentage of annual precipitation).

Table 3 presents a summary of the full-scale system discharges through December 31, 2007.3.4 Water-Level Data and Evaluation Water level measurements from the extraction and select observation wells have been monitored to confirm hydraulic containment of the tritium groundwater plume. Water levels are periodically collected and evaluated according to the schedule described in the Q4 2006 RAPR submitted in February 2007. Groundwater elevation contours developed from water level measurements collected in August 2007 and January 2008 are presented in Figure 2 and. Figure 3, respectively.

These contours indicate that the GRS system continues to be effective at capturing the extent of the tritium groundwater plume. Table 4 presents the water level measurement data.3.5 Cumulative Curies Removed The various groundwater recovery activities conducted to date have been successful in recovering tritium from groundwater at and downgradient of the Salem Unit 1 seismic gap.Figure 4 summarizes the results of groundwater remediation activities conducted using the well field and including both the pilot study and the permanent system. As shown on Figure 4 and Table 3, greater than 2.6 curies of tritium have been recovered from the operation of the GRS through December 31, 2007. Approximately 0.93 curies of tritium were removed by the pilot system. As the mass remaining in the plume 6 decreases so will the rate of tritium recovery by the GRS. The effectiveness of the GIRS is emphasized by the decrease and stabilization of system effluent concentrations since the activation of the full scale system in February 2005. System effluent concentrations averaged 21,510 pCiIL during the fourth quarter of 2007. This indicates that the GIRS has been successful at significantly decreasing tritium concentrations in groundwater as discharge concentrations are now less than 25 percent of the peak concentration (109,000) observed in March 2005. The mass of tritium in the plume was .recalculated in early 2006 to be approximately 2 to 5 Curies (depending on the amount of tritium drawn back through the seismic gap, the actual variability in discharge concentrations and the amount of tritium remaining in dead end pore spaces) at concentrations above the NJDEP GWQC. Based upon the tritium removed since the last recalculation, the present estimate would indicate that the plume retains 1.2 to 4.2 Curies of tritium.Therefore, GRS operations may achieve end criteria for tritium removal ahead of the previously communicated schedule.

Ongoing data collection will provide additional data to confirm this preliminary conclusion later in 2008.4.0 Operation of the Seismic Gap Drain In addition to the operation of the GIRS and mobile groundwater recovery unit, the seismic gap drains in Salem Unit 1 and Unit 2 are being used to continuously drain the water from these gaps, resulting in the recovery of residual tritium concentrations recovering concentrations from the seismic gap. The operation of these permanent gap drains creates an inward gradient towards the gaps facilitating the recovery of water from low accessibility areas.Water samples from the seismic gap drains are periodically collected for tritium analysis.

Table 5 and Figure 5 summarizes the results of periodic tritium analysis from the seismic gap. A comparison of Figure 1 and Figure 5 reveals the concentrations of tritium in water recovered in the Unit 1 seismic gap have been consistently significantly higher than those detected in groundwater samples collected from Well AC and Well AM located to the southeast and southwest of the seismic gap, respectively.

Thus, continuous operation of the Unit 1 seismic gap drain is effectively removing residual SEP water in the seismic gap, resulting in the reduction of tritium concentrations in groundwater adjacent to the seismic gap. Significant concentrations of tritium continue to be removed from the Unit 1 seismic gap however the exact mass removed can no longer be accurately determined due to monitoring limitations imposed at the initiation of continuous draining.

The concentration distribution of tritium at the gap drains will vary with the source of the water being drained, the amount of precipitation since the last draining, and the movement of the water within the seismic gap.During the winter of 2006 to 2007, increased levels of tritium were detected in samples collected from the Unit 1 seismic gap drain. Concentrations began declining in early January and by late January had decreased significantly from the peak concentrations.

Since mid-February tritium concentrations have fluctuated around a mean of 70 million pCi/L. During July the lowest concentration since early 2005 was reported in the Unit 1 7 seismic gap. Additionally, the highest concentration since January 2007 was detected in September.

Relatively high concentrations have continued through December 2007.Increased tritium concentrations detected in water collected from the seismic gap drains suggests that under the continuous draining program, instituted in late February 2007, portions of the seismic gap previously unaffected by the draining program may be supplying water to the gap drain.Continuous or nearly continuous draining provides a positive assurance of an inward gradient of groundwater to the seismic gap and assures that there is no further potential to discharge to the environment.

Concentrations of tritium from the Unit I seismic gap (summarized by week) are shown on Figure 5.Monitoring of water drained from the Unit 2 seismic gap acts as a screen for a potential release from the Unit 2 SFP. Currently, plant related gamma-emitting radioisotopes have not been detected in samples collected from the Unit 2 seismic gap drain.Short-lived gamma-emitting radioisotopes Were not consistently detected in samples collected from the Unit I gap for the period between May 2004 and May 2007.Beginning in May 2007 sporadic detections

'of Co-58 and Sb-125 have occurred in water collected from the Unit-i seismic gap drain. PSEG is presently evaluating the gap draining program. Although continuous draining ensures an inward gradient, the elevation to which the gap is drained could be optimized to ensure a continuous inward gradient with a lower volume discharge.

The lack of the presence of short-lived gamma-emitting radioisotopes and decreasing tritium concentrations in groundwater at well locations outside of the Unit 1 seismic gap suggest that these radioisotopes are not migrating beyond the Unit-I seismic gap.Water samples will continue to be periodically obtained from the Unit 1 and Unit 2*seismic gap drain to evaluate the potential for the release of radioisotopes to the environment.

5.0 Upcoming Activities Activities projected for the first half of 2008 (January through June) include the following:

  • Ongoing evaluation of the Unit I Seismic Gap to refine the procedures and protocols as necessary to adaptively manage the operation and sampling of the GRS;* Continue to measure groundwater levels and evaluate flow and plume containment;
  • Continued groundwater sampling and analysis; and," Continued operation and evaluation of the GRS performance.
  • Continue to monitor continuous draining of seismic gap drains 8 If you have any questions or comments regarding the contents of this report, please do not hesitate to contact me at (856) 339-5066.Sincerely, Greg Suey Manager -Salem Chemistry, Environmental, and Radwaste C Ron Nimitz- NRC NRC -Salem Resident Inspector NRC -Document Room 9 BC: Chris White H15 George Gellrich S05 Ben Neufeld S07 Edward Keating N21 John Valeri Jr. T5 File#Groundwater EXTERNAL Peter Milionis, ARCADIS Bradley Pierce, ARCADIS Scott Potter, PhD., ARCADIS Christopher Sharpe, ARCADIS 10 a Well Construction Details, PSEG Nuclear, LLC, Salem Generating Station, Hancock's Bridge, New Jersey.I of 2 Table 01.Installation Construction Diameter Total Depth Monitoring Monitored MP MP Northing Easting Well ID Date Details (inches) (feet bgs) Interval Hydrogeologic Elevation Elevation (NAD 83) (NAD 83)(feet bgs) Unit (feet RPD) (feet amsl)Well K Feb-03 Sch-40 PVC 2 80.0 70.0- 80.0 Vincentown 1 102.00 12.08 231,435 199,697 Well L Jan-03 Sch-40 PVC 2 80.0 70.0-80.0 Vincentown 1 101.46 11.54 230,933 199,263 Well M May-03 Sch-40 PVC 1 20.0 10.0 -20.0 Cofferdam 2 102.17 12.25 230,843 199,546 Well N Jan-03 Sch-40 PVC 2 20.0 10.0-20.0 Cofferdam 2 101.65 11.73 230,777 199,661 Well 0 Jan-03 Sch-40 PVC 2 20.0 10.0-20.0 Cofferdam 2 101.33 11.41 230,804 199,839 Well P Mar-03 Sch-40 PVC 2 80.0 70.0-80.0 Vincentown

' 101.13 11.21 230,336 200,000 Well Q Mar-03 Sch-40 PVC 2 80.0 70.0-80.0 Vincentown

' 106.59 16.67 230,645 201,196 Well R Jun-03 Sch-40 PVC 1 19.0 9.0- 19.0 Cofferdam 2 102.35 12.43 230,906 199,640 Well S 4 May-03 Sch-40 PVC 2 34.7 24.7-34.7 Shallow 3 99.04 9.12 230,711 199,613 Well T Jun-03 Sch-40 PVC 2 31.2 21.2-31.2 Shallow 3 104.13 14.21 231,575 199,575 Well U 4 May-03 Sch-40 PVC 2 32.2 27.2-32.2 Shallow3 98.57 8.65 231,370 199,618 Well V 4 Jun-03 Sch-40 PVC 2 79.5 69.5-79.5 Vincentown

' 98.74 8.82 231,355 199,548 Well W 4 Jun-03 Sch-40 PVC 2 35.0 25.0- 35.0 Shallow 3 98.26 8.34 230,777 199,450 Well Y Sep-03 Sch-40 PVC 2 37.0 27.0-35.0 Shallow 3 101.81 11.89 230,771 199,343 Well Z Sep-03 Sch-40 PVC 2 37.5 27.5-37.5 Shallow 3 101.86 11.94 230,681 199,399 Well AA 4 Sep-03 Sch-40 PVC 2 36.0 26.0- 36.0 Shallow 3 99.07 9.15 230,603 199,541 Well AB 4 Oct-03 Sch-40 PVC 2 42.0 32.0- 42.0 Shallow 3 98.93 9.01 230,623 199,677 Well AC 4 Sep-03 Sch-40 PVC 2 24.0 14.0 -24.0 Cofferdam2 98.77 8.85 230,724 199,725 Well AD 4 Oct-03 Sch-40 PVC 6 43.0 33.0-43.0 Shallow 3 98.99 9.07 230,684 199,607 Well AE Oct-03 Sch-40 PVC 2 37.5 27.5-37.5 Cofferdam2 101.54 11.62 230,829 199,845 Notes: MP Measuring Point bgs Below ground surface RPD Relative to plant datum amsl Relative to mean sea level (NAVD 1988)1 Monitoring well is screened in the Vincentown Formation.

2 Monitoring well is screened in the shallow, water-bearing unit at a location within the limits of the cofferdam.

3 Monitoring well is screened in the shallow, water-bearing unit at a location outside the limits of the cofferdam.

4 The surface completions of Monitoring Wells S, U, V, W, AA, AB, AC, and AD were converted from above-grade to flush-grade in February 2004.

a 2 of 2 Table 01.Well Construction Details, PSEG Nuclear, LLC, Salem Generating Station, Hancock's Bridge, New Jersey.Installation Construction Diameter Total Depth Monitoring Monitored MP MP Northing Easting Well ID Date Details (inches) (feet bgs) Interval Hydrogeologic Elevation Elevation (NAD 83) (NAD 83)(feet bgs) Unit (feet RPD) (feet amsl)Well AF Oct-03 Sch-40 PVC 2 45.0 35.0 -45.0 Shallow 3 101.61 11.69 230,491 199,702 Well AG-Shallow Feb-04 Sch-40 PVC 1 24.2 14.2 -24.2 Shallow 3 99.29 9.37 230,496 199,508 Well AG-Deep Feb-04 Sch-40 PVC 1 40.0 30.0 -40.0 Shallow 3 99.20 9.28 230,496 199,508 Well AH-Shallow Feb-04 Sch-40 PVC 1 24.5 14.5 -24.5 Shallow 3 102.58 12.66 230,450 199,596 Well AH-Deep Feb-04 Sch-40 PVC 1 40.0 30.0 -40.0 Shallow 3 102.70 12.78 230,450 199,596 Well Al Jan-04 Sch-40 PVC 4 22.0 12.0 -22.0 Cofferdam 2 98.79 8.87 230,798 199,521 Well AJ Jan-04 Sch-40 PVC 4 35.3 15.3 -35.3 Shallow 3 98.85 8.93 230,670 199,665 Well AL Jan-04 Sch-40 PVC 2 25.3 15.3 -25.3 Shallow 3 99.13 9.21 230,594 199,806 Well AM Jan-04 Sch-40 PVC 4 20.9 10.9 -20.9 Cofferdam 2 98.55 8.63 230,762 199,680 Well AN Jun-04 Sch-40 PVC 4 25.0 10.0-25.0 Cofferdam2 98.76 8.84 230,727 199,735 Well AO Jun-04 Sch-40 PVC 4 21.0 11.0 -21.0 Cofferdam2 98.82 8.90 230,765 199,556 Well AP Jun-04 Sch-40 PVC 4 40.0 15.0 -40.0 Shallow3 98.65 8.73 230,694 199,464 Well AQ Jun-04 Sch-40 PVC 41 45.0 20.0-45.0 Shallow3 99.05 9.13 230,526 199,540 Well AR Jun-04 Sch-40 PVC 4 43.0 18.0-43.0 Shallow3 99.22 9.30 230,622 199,626 Well AS Jun-04 Sch-40 PVC 4 41.5 16.5-41.5 Shallow3 99.44 9.52 230,566 199,604 Well AT Jun-04 Sch-40 PVC 4 44.0 19.0 -44.0 Shallow3 99.25 9.33 230,546 199,566 Well BW Dec-06 Sch-40 PVC 1 10 5-10 Shallow1 98.72 8.80 231563.00 199,864 Well BX Dec-06 Sch-40 PVC 1 10 5-10 Shallow1 98.72 8.80 231582.00 199,876 Well CA Dec-06 Sch-40 PVC 4 38 28.0 -38.0 Shallow 2 98.87 8.95 231318.00.

199,791 Well CB Dec-06 Sch-40 PVC 2 80 70.0 -80.0 Vincentown 3 98.98 9.06 231328.00 199,787 Notes: MP Measuring Point, bgs Below ground surface RPD Relative to plant datum amsl Relative to mean sea level (NAVD 1988)1 Monitoring well is screened in the Vincentown Formation.

2 Monitoring well is screened in the shallow, water-bearing unit at a location within the limits of the cofferdam.

3 Monitoring well is screened in the shallow, water-bearing unit at a location outside the limits of the cofferdam.

4 The surface completions of Monitoring Wells S, U, V, W, AA, AB, AC, and AD were converted from above-grade to flush-grade in February 2004.

Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium I Major Cations and Anions Identification Date Note Result (pCi/L)I LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K Well- K 01/29/03 02/03/03 02/05/03 02/12/03 02/27/03 03/14/03 03/18/03 03/26/03 03/31/03 04/09/03 04/17/03 04/21/03 04/29/03 05/05/03 05/20/03 05/28/03 06/04/03 06/10/03 06/17/03 06/24/03 06/30/03 07/16/03 07/29/03 08/12/03 08/27/03 09/09/03 09/25/03 10/06/03 11/09/03 02/04/04-153ý153 1,120 506 1,170 937 875 822 677 1,010 1,170 911 833 948 878 859 921 897 894 783 914 870 950 845 852 653 713 880 891 762 153 153 147 148 145 144 144 140 155 140 141 140 142 135 145 141 141 138 141 141 142 140 140 142 141 147 139 143 141 139 90 91 104 96 104 100 99 97 103 99 102 98 97 96 100 97 98 97 98 96 99 97 98 98 97 98 94 99 98 95 0.74 0.8 1.38 1.19 1,060 1,210 1,200 1,060 1,190 1,220 1,170 1,280 1,250 1,330 1.13 1.02 1.16 0.82 1.15 0.92 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.( Constituent was detected above its New Jersey Groundwater Quality Criteria.Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page I of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- K 06/10/04 777 143 97 --Well- K 08/02/04 720 144 97 0.67 1,160 Well- K 10/04/04 485 156 100 --Well- K 11/03/04 598 148 98 1.60 1,270 Well- K 12/06/04 1 -4,520 4,520 1,370 -- -Well- K 01/10/05 480 152 98 2.12 1,200 Well- K 02/01/05 602 139 93 --Well- K 03/03/05 711 146 98 ....Well- K 04/05/05 740 143 97 --Well- K 05/09/05 473 155 100 -- -Well- K 07/05/05 721 150 101 ---Well- K 01/09/06 511 155 100 --Well- K 07/10/06 404 153 97 --Well- K 01/23/07 468 152 98 ---Well- K 07/12/07 294 144 90 --Well- L 01/22/03 ,147 147 87 0.76 1,020 Well- L 01/23/03 '146 146 86 0.67 1,890 Well- L 01/24/03 -147 147 87 0.59 2,000 Well- L 01/27/03 -151 151 89 0.53 1,900 Well- L 03/14/03 ,143 143 85 ....Well- L 03/18/03 -143 143 86 -- -Well- L 04/02/03 '153 153 91 --Well- L 04/08/03 ,142 142 86 --Well- L 04/15/03 '141 141 84 --Well- L 04/24/03 -139 139 82 --Well- L 04/29/03 '141 141 83 -- -Well- L 05/05/03 '134 134 82 ....Well- L 05/15/03 '144 144 85 -- -Well- L 05/20/03 -144 144' 86 --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.-Constituent was detected above its New Jersey Groundwater Quality Criteria.Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 2 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium T Major Cations and Anions Identification Date' Note Result (pCi/L)I LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L Well- L 05/28/03 06/04/03 06/10/03 06/17/03 06/24/03 06/30/03 07/29/03 08/27/03 09/25/03 12/16/03 03/23/04 05/04/04 05/10/04 05/19/04 05/24/04 06/10/04 07/07/04 08/02/04 10/04/04 11/03/04 12/06/04 01/10/05 02/01/05 03/07/05 04/06/05 05/17/05 07/06/05 01/09/06 07/10/06 01/22/07'141-140 ,137-141'141 140'141-142 ,140-146 3,870 ,138-138-148-147 140 753 ,147-159'142'4,520-158'148-158-152-150'152'160'156-154 141 140 137 141 141 140 141 142 140 146 147 138 138 148 147 140 140 147 159 142 4,520 158 148 158 152 150 152 160 156 154 84 84 82 84 84 83 86 84 84 86 137 82 84 88 88 85 96 88 92 84 1,280 93 87 94 90 88 90 95 92 92 1.95 1.62 1.56 0.81 0.832 2,330 2,490 2,180 1,140 2,400 I Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.[i--i]Constituent was detected above its New Jersey Groundwater Quality Criteria.L- 'N ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM 0 Page 3 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample I Tritium Major Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- L 07/19/07 1 145 1145 87 -- -Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M 02/12/03 02/28/03 03/03/03 03/10/03 03/17/03 03/24/03 03/31/03 04/07/03 04/14/03 04/21/03 04/30/03 07/09/03 07/23/03 08/06/03 08/06/03 08/20/03 09/04/03 09/16/03 10/03/03 10/20/03 10/30/03 12/04/03 01/06/04 01/22/04 02/17/04 03/05/04 04/29/04 05/11/04 18,700 14,400 9,420 15,000 10,600 10,100 11,000 9,260 9,600 8,880 8,800 16,380 11,200 8,900 7,340 11,300 7,170 6,510 2,350 170 146 140 144 142 144 154 136 135 140 143 138 141 141 144 141 143 141 146 NA NA 146 145 140 NA 146 141 141 270 219 181 223 192 189 203 181 183 180 180 602 573 466 462 430 346 320 289 NA NA 198 183 164 NA 168 159 117 0.25 0.17 0.16 0.21 23 28 27 22 1 1 0.24 0.27 0.22 0.32 0.27 0.15 0.12 22 23 23 25 25 22 21 Notes: LLD mg/L pCi/L Lower Limit of Detection Milligrams per liter Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.InooConstituent was detected above its New Jersey Groundwater Quality Criteria.NA Not Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 4 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification IDate NoteResult (pCi/L) I LLD Deviation I Boron(mg/L)

ISodium(mg/L)

Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M Well- M 06/10/04 07/08/04 08/17/04 09/08/04 10/04/04 11/03/04 12/06/04 01/19/05 01/19/05 02/09/05 03/02/05 04/11/05 05/03/05 06/06/05 07/12/05 08/15/05 09/06/05 10/10/05 11/14/05 12/13/05 01/17/06 02/21/06 02/22/06 03/20/06 04/11/06 05/16/06 06/19/06 07/18/06 08/08/06 09/18/06 3,610 5,090 3,857 3,745 3,036 2,818'4,520 10,031 15,169 17,049 12,528 8,257 6,932 7,371 7,510 4,200 4,067 4,592 4,712 5,553 4,912 4,132 141 144 143 146 144 143 4,520 3,950 2,650 4,660 3,360 4,220 147 146 3,750 3,905 4,940 148 158 148 152 153 3,550 3,730 155 152 155 157 161 161 133 150 136 137 126 125 1,390 2,890 2,830 3,240 3,400 2,550 192 225 4,070 4,114 4,037 240 219 178 170 174 1,750 1,530 144 148 150 161 157 148 3.33 24 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.5 Constituent was detected above its New Jersey Groundwater Quality Criteria.N Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 5 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- M 10/10/06 3,565 157 139 --Well- M 11/01/06 4,077 170 154 --Well- M 12/18/06 3,887 162 147 ....Well- M 01/13/07 4,517 150 148 --well- M 02/23/07 4,796 168 161 ....Well- M 03/08/07 5,085 158 160 ....Well- M 04/20/07 11,617 170 225 -- -Well- M 05/15/07 10,479 181 219 -- -Well- M 06/18/07 8,426 147 177 ....Well- M 07/18/07 7,443 146 168 -- -Well- M 08/15/07 6,066 140 154 --Well- M 09/20/07 5,271 150 153 --Well- M 10/03/07 5,612 160 164 --Well- M 11/14/07 4,505 124 133 --Well- M 12/12/07 4,617 151 146 --Well- N 01/30/03 -5S4004 141 412 0.37 14 Well- N 01/30/03 6 187 505 0.34 14 Well- N 02/10/03 15,600 149 229 0.28 11 Well- N 03/04/03 2,770 144 123 0.2 34 Well- N 03/14/03 2,670 143 121 0.41 24 Well- N 03/17/03 3,830 142 134 0.36 21 Well- N 03/25/03 3,480 139 129 --Well- N 04/04/03 3,560 152 137 ....Well- N 04/11/03 3,730 137 131 ---Well- N 04/16/03 3,910 142 134 --Well- N 04/25/03 4,600 138 140 ....Well- N 04/30/03 9,370 144 185 --Well- N 05/06/03 9,830 137 186 -- -Well- N 05/21/03 7,480 144 169 --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.FVo ]Constituent was detected above its New Jersey Groundwater Quality Criteria.NA ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 6 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample I Tritium I Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N 05/27/03 06/04/03 06/11/03 06/19/03 06/25/03 07/10/03 07/25/03 08/07/03 08/20/03 09/04/03 09/17/03 10/03/03 10/03/03 11/03/03 12/12/03 01/20/04 02/11/04 02/11/04 03/18/04 04/08/04 05/12/04 06/03/04 07/20/04 08/17/04 09/14/04 10/25/04 11/23/04 12/27/04 01/12/05 02/22/05 7,130 5,480 4,990 5,680 5,060 5,020 5,220 5,110 5,850 5,660 6,160 5,740 6,460 5,560 6,010 6,050 5,950 7,360 6,550 7,180 8,210 9,890 5,220 14,303 11,642 10,619 9,150 7,660 9,550 9,442 141 141 137 142 142 137 141 145 140 145 141 145 NA NA NA 143 139 NA 145 137 147 152 141 161 148 157 149 4,060 154 146 165 150 144 153 146 144 148 148 153 154 157 157 NA NA NA 155 154 NA 162 164 178 196 148 235 207 206 187 1,720 195 186 0.21 0.25 0.33 0.27 0.24 24 20 23 22 24 2.30E-01 17 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.1Constituent was detected above its New Jersey Groundwater Quality Criteria.~Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 7 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification I Date I Nte Result (pCi/L) LLD Deviation I Boron(mg/L)

I Sodium(mg/L)

Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N Well- N 03/15/05 04/19/05 05/17/05 06/21/05 07/12/05 08/15/05 09/20/05 10/10/05 11/14/05 12/20/05 01/23/06 02/23/06 03/21/06 04/11/06 05/16/06 06/20/06 07/18/06 08/21/06 09/07/06 09/19/06 10/09/06 11/01/06 11/15/06 12/07/06 12/18/06 01/13/07 01/22/07 02/06/07 02/23/07 03/08/07 9,712 9,781 9,060 9,302 8,147 8,152 7,502 8,280 8,210 5,896 7,400 8,410 13,500 8,393 8,588 15,289 6,660 13,776 14,486 11,023 10,407 9,280 10,163 6,325 6,812 11,587 12,517 13,252 153 147 147 145 147 157 151 149 151 157 149 3,920 3,730 164 152 150 159 154 155 160 159 165 197 211 154 148 157 189 167 146 195 193 185 183 177 184 174 180 180 162 171 1,810 2,130 189 185 232 170 224 277 232 310 213 232 233 199 165 173 234 227 218 0.11 18 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.Constituent was detected above its New Jersey Groundwater Quality Criteria.N-'Not Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 8 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- N 04/20/07 6,332 160 172 -- -Well- N 05/15/07 8,139 150 177 ---Well- N 06/19/07 7,554 145 169 ---Well- N 07/18/07 8,865 99 168 -- -Well- N 08/15/07 9,045 148 182 ---Well- N 09/21/07 9,711 147 188 --Well- N 10/03/07 L239O 145 267 ---Well- N 10/17/07 2 2.01 153 279 ---Well- N 11/14/07 18,607 124 237 --Well- N 12/12/07 12,763 145 207 --Well- 0 01/29/03 1,400 143 106 0.17 40 Well- 0 01/29/03 1,220 156 110 0.16 41 Well- 0 02/10/03 10,300 149 193 0.1 13 Well- 0 02/21/03 7,370 149 170 0.09 15 Well- 0 02/28/03 11,700 147 201 0.09 17 Well- 0 03/04/03 8,800 142 178 0.07 21 Well- 0 03/13/03 12,300 143 204 0.11 16 Well- 0 03/17/03 11,000 155 206 0.08 12 Well- 0 03/25/03 8,660 141 178 --Well- 0 03/31/03 8,010 155 180 ---Well- 0 04/07/03 7,290 137 165 --Well- 0 04/15/03 12,400 141 204 ---Well- 0 04/21/03 11,800 139 201 --Well- 0 04/29/03 10,500 140 191 --Well- 0 05/06/03 10,200 134 187 --Well- 0 05/21/03 11,100 143 197 --Well- 0 05/28/03 12,700 140 207 --Well- 0 06/03/03 12,200 140 202 ---Well- 0 06/10/03 12,800 137 206 ....Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.F Constituent was detected above its New Jersey Groundwater Quality Criteria.NA-Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 9 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Nte Result (pCi/L) LLD Deviation Boron(mg/L)

I Sodium(mg/L)

Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 06/17/03 06/24/03 07/09/03 07/25/03 08/06/03 08/20/03 09/03/03 09/15/03 10/03/03 10/20/03 11/17/03 12/18/03 01/14/04 02/09/04 02/09/04 03/03/04 03/23/04 04/06/04 05/03/04 05/11/04 06/10/04 06/24/04 07/13/04 07/29/04 08/31/04 09/22/04 10/04/04 10/18/04 11/22/04 12/16/04 10,300 13,400 9,100 7,710 8,300 7,440 6,400 7,730 6,980 6,700 5,320 3,750 19,300 14,174 9,510 6,739 7,307 6,637 5,543 5,874 14,027 15,000 141 141 139 139 148 142 143 141 145 141 NA 145 141 NA NA NA NA 136 140 140 4,974 141 141 146 159 146 140 150 144 190 212 182 169 178 168 159 170 168 161 NA 150 132 NA NA NA NA 247 253 254 2,855 218 185 163 179 167 151 161 218 1,950 0.24 0.31 0.28 0.27 0.23 0.2 14 14 14 13 23 47 2.81E-01 120 3,230 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.[11()0) Constituent was detected above its New Jersey Groundwater Quality Criteria.A Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 10 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)I LLD Deviation I Boron(mg/L)

[Sodium(mg/L)

Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 Well- 0 01/18/05 02/08/05 03/08/05 04/11/05 05/10/05 06/07/05 07/06/05 07/19/05 08/02/05 09/07/05 10/04/05 11/02/05 12/09/05 01/16/06 02/07/06 03/07/06 04/04/06 05/02/06 06/19/06 07/17/06 08/21/06 09/18/06 10/05/06 11/02/06 12/07/06 01/13/07 02/24/07 03/07/07 04/20/07 05/16/07 18,840 10,911 7,096 6,722 5,803 3,827 4,999 4,295 5,400 4,326 14,530 15,734 18,595 8,560 7,340 9,369 9,417 9,533 4,760 4,237 12,747 19,760 9,060 15,782 152 4,660 139 148 148 147 145 156 148 146 153 151 152 3,550 157 3,310 161 152 155 151 152 158 157 169 162 147 153 155 163 180 257 2,640 195 170 166 156 136 154 143 152 146 224 235 2,460 254 1,720 178 191 194 188 150 147 219 275 197 306 292 393 393 257 0.297 22 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.F[i -C onstituent was detected above its New Jersey Groundwater Quality Criteria.N ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page I11 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- 0 06/18/07 15,749 148 229 --Well- 0 07/19/07 8,610 145 177 ---Well- 0 08/15/07 9,155 142 178 ---Well- 0 09/19/07 1,525 146 109 -- -Well- O 10/04/07 2,619 183 146 --Well- O 11/19/07 6,211 149 167 ---Well- 0 12/12/07 1713l'9 142 340 Well- P 02/05/03 0.18 1,600 Well- P 02/06/03 -153 153 91 --Well- P 02/21/03 -148 148 91 --Well- P 03/13/03 303 143 90 0.2 --Well- P 03/18/03 465 143 92 ---Well- P 03/26/03 '143 143 87 ---Well- P 04/03/03 '154 154 9 --Well- P 04/24/03 '139 139 82 --Well- P 04/29/03 '144 144 85 --Well- P 05/05/03 '134 134 82 --Well- P 05/20/03 '145 145 85 -- -Well- P 05/30/03 '142 142 85 --Well- P 06/04/03 141 141 84 -- -Well- P 06/10/03 '138 138 84 --Well- P 06/17/03 '141 141 85 ---Well- P 06/24/03 '141 141 85 -- -Well- P 07/16/03 '141 141 85 --Well- P 08/13/03 ' 140 140 84 0.48 1,570 Well- P 09/08/03 -147 147 87 0.65 1,560 Well- P 09/09/03 1 '7,430 7,430 NA --Well- P 10/06/03 '143 143 86 0.48 1,610 Well- P 01/22/04 ' 144 144 86 -- --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.qoConstituent was detected above its New Jersey Groundwater Quality Criteria.Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 12 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- P 04/28/04 '139 139 83 0.441 1,550 Well- P 08/03/04 '157 157 92 0.292 1,540 Well- P 10/05/04 -149 149 87 -- -Well- P 11/03/04 ' 147 147 87 0.955 1,690 Well- P 12/14/04 1 '3,230 3,230 1,010 ....Well- P 01/11/05 ,162 162 95 1.02 1,580 Well- P 02/09/05 '148 148 88 --Well- P 03/03/05 '158 158 92 -- -Well- P 04/12/05 ,149 149 89 -- -Well- P 05/10/05 ,148 148 87 --Well- P 07/11/05 -151 151 89 -- -Well- P 01/23/06 ,150 150 89 -- -Well- P 07/24/06 '155 155 93 --Well- P 01/14/07 '154 154 92 --Well- P 07/19/07 '146 146 86 -- -Well- Q 02/06/03 '147 147 88 ---Well- Q 03/11/03 -142 142 85 --Well- Q 03/12/03 -141 141 84 --Well- Q 03/14/03 '143 143 85 --Well- Q 03/19/03 '143 143 85 ....Well- Q 03/24/03 ' 143 143 85 ---Well- Q 04/23/03 '139 139 82 -- -Well- Q 04/30/03 '142 142 84 --Well- Q 05/06/03 ' 135 135 81 --Well- Q 05/12/03 '144 144 84 --Well- Q 05/19/03 '144 144 84 -- -Well- Q 05/30/03 -140 140 84 ....Well- Q 06/05/03 '139 139 83 -- -Well- Q 06/11/03 '138 138 83 ---Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.[;o4ýConstituent was detected above its New Jersey Groundwater Quality Criteria.NA Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 13 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mgIL)

Sodium(mgIL)

Well- Q 06/16/03 -141 141 84 --Well- Q 06/23/03 '143 143 85 --Well- Q 07/17/03 '141 141 85 -- -Well- Q 08/13/03 142 142 85 0.32 1,830 Well- Q 09/10/03 -148 148 89 0.25 1,790 Well- Q 10/07/03 ' 144 144 85 0.33 1,920 Well- Q 11/09/03 '142 142 86 0.32 1,930 Well- Q 01/08/04 '142 142 83 0.3 1,850 Well- Q 02/04/04 -139 139 84 ---Well- Q 03/22/04 ' 144 144 85 0.285 1,720 Well- Q 06/04/04 -156 156 91 -- -Well- Q 08/02/04 '146 146 88 0.28 1,630 Well- Q 10/04/04 '153 153 87 --Well- Q 11/03/04 '150 150 88 0.312 1,960 Well- Q 12/29/04 1 '4,020 4,020 1,420 --Well- Q 01/31/05 213 142 89 --Well- Q 02/15/05 1 '3,910 3,910 1,130 -- --Well- Q 03/14/05 <151 151 91 0.30 1,730 Well- Q 03/15/05 151 151 91 -1,730 Well- Q 04/18/05 '145 145 85 --Well- Q 05/16/05 '151 151 88 -- -Well- Q 07/19/05 ,150 150 89 -- -Well- Q 01/23/06 -150 150 90 --Well- Q 07/10/06 -159 159 93 --Well- Q 01/08/07 '157 157 92 --Well- Q 07/24/07 '146 146 86 --Well- R 02/26/03 13,900 145 218 0.29 3 Well- R 03/03/03 7,490 140 166 0.23 Well- R 03/10/03 6,170 145 158 0.27 29 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.J Constituent was detected above its New Jersey Groundwater Quality Criteria.W0 Cot Available

-Deviation and/or LLD were not reported.Constituent not analyzed.03/05/2008 5:52 PM Page 14 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R 03/17/03 03/25/03 04/01/03 04/08/03 04/14/03 04/22/03 04/30/03 07/09/03 07/25/03 08/06/03 08/20/03 09/04/03 09/17/03 10/03/03 10/21/03 12/05/03 01/22/04 02/09/04 02/09/04 03/05/04 04/28/04 05/24/04 06/10/04 07/08/04 08/17/04 09/29/04'10/11/04 11/08/04 12/27/04 01/19/05 7,270 6,810 6,740 5,940 5,890 5,800 5,260 3,270 2,940 2,860 2,860 2,990 2,800 2,740 2,650 2,550 2,210 2,230<5,390 2,200-5,780 2,420 2,390 2,050 2,124 2,000 1,708 1,696 ,4,053 2,420 144 140 153 135 142 139 141 136 141 144 142 153 141 146 140 147 143 140 5,390 146 5,780 144 148 147 159 156 143 151 4,053 159 168 162 169 152 154 153 148 125 124 124 124 132 122 125 120 122 116 115 NA 117 1,649 120 123 118 126 122 110 115 1,290 129 0.27 33 0.46 0.51 0.57 0.47 0.4 0.37 0.265 0.30 0.24 54 48 46 50 52 50 42 41 42 I Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.2 Constituent was detected above its New Jersey Groundwater Quality Criteria.Nl Not Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 15 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample I Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

I Sodium(mgIL)

Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R Well- R 02/09/05 03/15/05 04/11/05 05/03/05 06/22/05 07/20/05 08/16/05 09/20/05 10/10/05 11/14/05 12/13/05 01/17/06 02/21/06 03/20/06 04/11/06 05/16/06 06/19/06 07/18/06 08/08/06 09/18/06 10/10/06 11/15/06 12/18/06 01/13/07 02/23/07 03/08/07 04/20/07 05/15/07 06/18/07 07/18/07 I 2,450 2,704 2,742 2,755 2,736 2,486 2,752 2,673 2,435 2,149 ,4,370 2,131 2,262 4,350 2,192 2,010 2,067 2,090 1,940 2,138 1,943 2,395 3,092 3,208 3,563 3,487 3,180 2,567 2,844 2,862 150 147 157 151 151 147 155 159 149 148 4,370 151 153 3,730 160 150 160 156 148 162 157 164 154 154 167 161 157 138 142 145 123 125 132 128 127 122 130 131 123 119 NA 120 122 1,560 125 118 124 123 116 126 121 132 134 135 146 143 138 118 122 124 0.122 45 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.Constituent was detected above its New Jersey Groundwater Quality Criteria.NA Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 16 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- R 08/15/07 3,000 143 125 --Well- R 09/20/07 3,104 144 127 --Well- R 10/03/07 2,799 149 129 --Well- R 11/14/07 3,029 141 124 ---Well- R 12/12/07 2,951 145 125 ---Well- S 07/09/03 1, 5 1 134 3,120 Well- S 08/07/03 1 "92(00H NA NA --Well- S 08/21/03 1 2-70, 00 NA NA --Well- S 09/03/03 1 2390,000 NA NA --Well- S 09/15/03 1 2,340,000 NA NA ---Well- S 10/04/03 1 2,180,000 NA NA --Well- S 10/13/03 1 2,130,000 NA NA -- -Well- S 10/20/03 1 2,060,000 NA NA --Well- S 10/20/03 1 210,000 NA NA ---Well- S 11/09/03 1 T1 960,000 NA NA --Well- S 11/09/03 1 1,71)(),0()

NA NA -- -Well- S 11/09/03 1 .O4(u.000 NA NA ....Well- S 11/26/03 1 >2,60MOO NA NA --Well- S 01/20/04 1 1 _0 0 NA NA --Well- S 02/17/04 1 1,.20,000 NA NA ---Well- S 03/18/04 1 .220AMO NA NA --Well- S 04/06/04 1 11J00000 4,706 15,206 -- -Well- S 05/04/04 1 1.100,00 5,589 15,212 44.5 35 Well- S 05/19/04 1 884.000 5,780 13,380 --Well- S 06/25/04 1 1.(20,(()1) 5,270 14,500 ....Well- S 07/13/04 1 3,620 13,800 --Well- S 08/09/04 1 S 4,850 13,000 -45 Well- S 09/13/04 1 845.00 4,560 13,000 --Well- S 11/08/04 1 82u000O 3,230 12,800 --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.,Zioo7Constituent was detected above its New Jersey Groundwater Quality Criteria.NWN ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 17 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- S 12/28/04 1 (ZIA00o 4,060 11,300 Well- S 01/11/05 1 "530011 3,910 12,100 Well- S 02/15/0S 1 012'H1 3,910 11,900 Well-S 03/07/05 1 3__MOO 3,490 8,570 -- -Well- S 03/14/05 1 175MOO 4,320 6,110 Well-S 03/23/05 1 12,001 3,790 6,190 -_Well- S 03/28/05 1 40ý50o 6,280 3,540 Well- S 04/18/05 1 320A)00 4,420 8,380 --Well-S 10/17/05 1 91200 3,790 4,570 --Well- S 11/15/05 1 64 ý7.00 3,430 3,840 -Well-S 12/12/05 1 49O4 155 446 Well- T 07/10/03 5147 147 88 Well- T 07/15/03 140 140 82 Well- T 07/30/03 -141 141 86 Well- T 08/12/03 5140 140 83 0.64 931 Well-T 08/28/03 5141 141 83 0.66 896 Well- T 09/09/03 '147 147 88 0.63 899 Well- T 09/25/03 ,142 142 84 0.63 912 Well- T 10/06/03 '146 146 86 0.65 966 Well- T 12/12/03 '149 149 88 06 93 Well- T 03/22/04 '142 142 84 0.649 986 Well- T 04/12/04 -141 141 84 0.762 920 Well- T 07/07/04 148 148 87 06 9 Well- T 08/02/04 '152 152 91 0.622 894 Well- T 08/31/04 147 147 87 -...Well- T 09/22/04 '146 146 87 --Well- T 10/11/04 -155 155 91 --Well- T 11/09/04 '148 148 87 --Well- T 12/21/04 1 '3,910 3,910 1,340 ....Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.oooConstituent was detected above its New Jersey Groundwater Quality Criteria.N ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 18 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- T 01/10/05 '165 165 96 -- --Well- T 02/01/05 137 135 83 0.638 945 Well- T 03/03/05 -152 152 90 --Well- T 04/05/05 '148 148 90 -- -Well- T 05/09/05 -144 144 86 -- -Well- T 07/05/05 -145 145 86 --Well- T 10/03/05 -149 149 90 ---Well- T 01/09/06 '154 154 90 -- -Well- T 04/03/06 ' 162 162 96 --Well- T 07/10/06 -161 161 95 --Well- T 10/05/06 '161 161 95 -- -Well- T 10/06/06 1 -6,270 6,270 NA --Well- T 01/23/07 193 152 94 --Well- T 04/11/07 -168 168 101 --Well- T 07/12/07 ' 147 147 86 --Well- T 10/09/07 '152 152 91 -- -Well- U 07/10/03 '136 136 83 Well- U 07/16/03 146 NA 86 Well- U 07/29/03 '141 141 96 --Well- U 08/12/03 '139 139 84 0.34 139 Well- U 08/27/03 '143 143 87 0.35 144 Well- U 09/09/03 148 147 90 0.38 139 Well- U 09/25/03 '139 139 83 0.34 155 Well- U 10/06/03 203 145 90 0.35 140 Well- U 12/12/03 '148 148 86 --Well- U 03/22/04 '144 144 88 0.38 168 Well- U 04/12/04 182 136 84 0.392 146 Well- U 07/07/04 162 150 92 --Well- U 08/02/04 '152 152 91 0.346 143 Notes: LLD Lower Limit of Detection mg/L. Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.o Constituent was detected above its New Jersey Groundwater Quality Criteria.~-'Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 19 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- U 08/31/04 '148 148 90 --Well- U 09/22/04 167 152 93 --Well- U 10/04/04 -146 146 87 -- -Well- U 11/03/04 165 148 91 --Well- U 12/06/04 1 '4,520 4,520 1,160 ....Well- U 01/10/05 -157 157 93 ---Well- U 02/08/05 -149 149 91 0.377 156 Well- U 03/03/05 '147 147 88 --Well- U 04/05/05 '142 142 86 --Well- U 05/09/05 -148 148 90 --Well- U 07/05/05 '143 143 87 --Well- U 10/03/05 284 150 94 --Well- U 01/09/06 '157 157 94 --Well- U 04/03/06 -154 154 93 ....Well- U 04/06/06 1 '5,000 5,000 NA -- -Well- U 07/10/06 '157 157 95 --Well- U 10/05/06 '160 160 98 --Well- U 10/06/06 1 -6,270 6,270 NA --Well- U 01/22/07 163 152 93 ---Well- U 04/11/07 '167 167 102 ---Well- U 07/12/07 < 150 150 91 -- -Well- U 10/09/07 ' 153 153 92 ....Well- V 07/21/03 334 140 89 Well- V 07/29/03 285 142 89 --Well- V 08/12/03 278 142 89 0.5 568 Well- V 08/27/03 338 141 90 0.61 584 Well- V 09/09/03 337 150 95 0.57 582 Well- V 09/25/03 261 140 -87 0.47 670 Well- V 10/06/03 185 144 89 0.46 543 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.[j7]o nstituent was detected above its New Jersey Groundwater Quality Criteria.NA Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 20 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mgfL)

Well- V 11/19/03 1 -3,300 3,300 NA --Well- V 12/12/03 207 147 91 --Well- V 03/22/04 290 144 90 0.46 556 Well- V 04/12/04 316 137 87 0.529 567 Well- V 07/07/04 228 145 90 -- -Well- V 08/02/04 309 154 97 0.433 504 Well- V 08/31/04 395 151 96 --Well- V 09/22/04 402 141 91 --Well- V 10/04/04 340 146 92 --Well- V 11/03/04 224 143 89 -- -Well- V 12/06/04 1 -4,170 4,170 1,360 --Well- V 01/10/05 394 151 96 --Well- V 02/08/05 307 152 95 -- -Well- V 03/03/05 157 156 95 0.436 431 Well- V 04/05/05 294 141 89 --Well- V 05/09/05 244 155 96 -Well- V 07/05/05 197 144 89 -- -Well- V 10/03/05 346 147 93 --Well- V 01/09/06 264 157 98 --Well- V 04/03/06 -152 152 93 --Well- V 07/10/06 181 157 96 --Well- V 10/05/06 '159 159 95 ---Well- V 01/22/07 199 157 97 ....Well- V 04/11/07 154 149 92 -- -Well- V 07/12/07 163 153 94 --Well- V 10/09/07 170 153 94 ....Well- W 07/07/03 10,500 135 189 --Well- W 07/21/03 11,100 140 196 --Well- W 08/06/03 11,500 141 200 0.46 211 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.jIii& Constituent was detected above its New Jersey Groundwater Quality Criteria.NA Not Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 21 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample I Tritium T Major Cations and Anions Identification Date Note Result (pCi[L) LLD F Deviation I Boron(mg/L) jSodium(mgIL)

Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W 08/07/03 08/19/03 09/03/03 09/15/03 10/03/03 10/21/03 11/17/03 11/19/03 12/16/03 12/16/03 01/14/04 02/02/04 03/03/04 04/29/04 05/10/04 05/24/04 06/24/04 07/28/04 08/02/04 08/31/04 09/22/04 10/11/04 11/08/04 12/14/04 01/10/05 02/01/05 03/02/05 04/05/05 05/02/05 06/06/05 I 6,010 10,700 10,500 10,900 11,100 10,600 12,200 13,200 15,500 15,200 17,100 19,600 5,320 4,570 2,350 4,080 5,300 11,691 11,910 11,091 9,571 9,947 8,920 5,560 6,292 7,340 5,756 8,826 12,339 11,480 NA 142 143 140 147 147 NA NA NA 147 144 144 146 140 141 146 141 154 148 160 138 147 150 3,230 150 159 150 155 147 154 NA 194 192 195 202 195 NA NA NA 226 232 251 151 140 117 139 149 208 204 211 186 194 186 1,390 165 178 158 192 209 207 0.59 0.53 0.57 0.46 215 222 237 240 0.28 0.14 273 212 0.487 0.681 3.33 309 273 27 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.I Constitisent was detected above its New Jersey Groundwater Quality Criteria.NA Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 22 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Identification I Date Tritium Major Cations and Anions LLD Deviation Boron(mg/L)

Sodium(mgfL)

Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W Well- W 07/06/05 08/01/05 09/06/05 10/03/05 11/14/05 12/20/05 01/17/06 02/07/06 02/21/06 03/07/06 03/20/06 04/03/06 04/17/06 05/02/06 05/15/06 06/06/06 06/19/06 07/10/06 07/24/06 08/07/06 08/21/06 09/07/06 09/18/06 10/09/06 10/24/06 11/01/06 11/15/06 12/07/06 12/19/06 01/13/07 149 149 154 149 3,430 3,430 3,550 3,090 3,920 3,310 3,730 5,000 5,510 5,000 5,000 155 4,890 161 152 158 162 158 166 166 155 170 171 184 139 152 239 227 247 211 2,460 2,830 3,380 3,470 3,620 3,750 3,850 3,880 4,240 3,800 3,870 374 3,500 144 109 139 162 220 242 266 194 231 245 220 221 259 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.F Constituent was detected above its New Jersey Groundwater Quality Criteria.NNot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 23 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-W 02/05/07 24 .147 278 Well- W 03/08/07 5,838 165 169 -- -Well- W 04/20/07 1,616 159 120 --Well- W 06/18/07 1,530 142 107 --Well- W 07/18/07 2,462 147 121 --Well- W 08/15/07 3,000 147 127 --Well- W 09/20/07 6,562 149 164 ....Well- W 10/03/07 12,492 165 229 --Well- W 11/14/07 13,071 123 202 --Well- W 12/12/07 13,940 147 216 --Well- X 08/20/03 1i '4,820 j 4,820 NA -Well- X 107/20/05 1,500 NA NA -- -Well- Y 10/27/03 '142 142 85 ---Well- Y 11/09/03 '143 143 85 --Well- Y 11/19/03 1 '3,750 3,750 NA --Well- Y 11/25/03 '141 141 85 0.82 1,070 Well- Y 12/12/03 '148 148 87 --Well- Y 12/22/03 '147 147 87 --Well- Y 01/06/04 '142 142 85 -- -Well- Y 02/02/04 <145 145 84 --Well- Y 02/02/04 1 '5,390 5,390 NA --Well- Y 03/23/04 145 145 86 --Well- Y 04/07/04 '136 136 82 0.83 1,080 Well- Y 05/10/04 143 143 85 ---Well- Y 06/24/04 141 141 86 0.82 1,060 Well- Y 07/28/04 '156 156 90 ---Well- Y 08/02/04 '157 157 94 -- -Well- Y 08/31/04 '145 145 87 ---Well- Y 09/08/04 -158 158 94 ....Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.2[yjtp'Constituent was detected above its New Jersey Groundwater Quality Criteria.Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 24 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium" Major Cations and Anions Identification I Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

[,Sodium(mg/L)

Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y Well- Y 10/11/04 11/08/04 12/13/04 01/10/05 02/01/05 03/07/05 04/06/05 05/25/05 06/07/05 07/20/05 08/01/05 09/07/05 10/04/05 11/01/05 12/13/05 01/17/06 02/07/06 03/07/06 04/04/06 05/02/06 05/16/06 06/06/06 06/19/06 07/11/06 07/24/06 08/07/06 08/22/06 09/07/06 09/19/06 10/09/06-162'151-3,230-162'154'149'144'155'155-159'149' 149-151'155-151'157'161-158'173'156'152'159-165'160'155'155-157'157'161'171 162 151 3,230 162 154 149 144 155 155 159 149 149 151 155 151 157 161 158 173 156 152 159 165 160 155 155 157 157 161 171 96 88 1,150 94 92 89 84 92 92 93 89 89 91 93 91 94 94 93 101 91 90 93 97 96 92 93 96 94 95 102 0.801 0.761 1,160 1,190 1,230 1,270 1,290 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.2o Constituent was detected above its New Jersey Groundwater Quality Criteria.NA ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 25 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- Y 10/24/06 '171 171 100 --Well- Y 11/01/06 ,166 166 100 -- -Well- Y 11/15/06 -166 166 98 ---Well- Y 12/07/06 '193 193 109 -- -Well- Y 12/18/06 '157 157 92 ---Well- Y 01/14/07 -155 155 93 ---Well- Y 02/20/07 -165 165 97 ---Well- Y 03/14/07 -162 162 94 --Well- Y 04/19/07 -163 163 97 ---Well- Y 05/16/07 -180 180 101 --Well- Y 06/19/07 ' 149 149 87 --Well- Y 07/12/07 -155 155 91 -- -Well- Y 08/16/07 -146 146 87 --Well- Y 09/20/07 '146 146 88 --Well- Y 10/04/07 ' 154 154 91 ---Well- Y 11/20/07 -149 149 90 ....Well- V 12/20/07 ' 140 140 82 ---Well- Z 10/27/03 573 142 94 ---Well- Z 11/09/03 '140 140 92 --Well- Z 11/19/03 1 -3,500 3,500 NA --Well- Z 11/24/03 583 141 93 0.5 519 Well- Z 12/12/03 621 141 94 -- -Well- Z 12/22/03 659 140 94 --Well- Z 01/06/04 648 142 95 ---Well- Z 02/02/04 538 145 95 ....Well- Z 03/23/04 412 144 92 --Well- Z 04/07/04 580 137 91 0.5 531 Well- Z 05/10/04 561 142 93 ---Well- Z 06/24/04 474 147 95 0.51 510 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.[o' 6C onstituent was detected above its New Jersey Groundwater Quality Criteria.NA-Not Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 26 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample I Tritium Major Cations and Anions Identification

[ Date INote Result (pCi/L) I LLD Deviation I Boron(mg/L)

I Sodium(mg/L)

Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z 07/28/04 07/29/04 08/02/04 08/31/04 09/08/04 10/11/04 11/08/04 12/13/04 01/10/05 02/01/05 03/07/05 04/06/05 05/25/05 06/07/05 07/20/05 08/01/05 08/16/05 08/29/05 09/07/05 09/19/05 10/04/05 10/18/05 11/01/05 12/13/05 01/17/06 02/07/06 02/21/06 03/07/06 03/20/06 04/04/06 519 519 706 585 444 268 339-3,230 249 228 192 274-149 182 177 202 ,160 186 201'156 271 ,153-158 ,157-153 240 238 ,3,310-3,730-177 150 150 159 152 141 144 155 3,230 159 153 153 165 149 149 158 147 160 149 149 156 148 153 158 157 153 149 152 3,310 3,730 177 97 97 106 100 91 90 98 1,060 99 95 94 103 91 91 97 91 98 91 92 94 93 93 94 96 93 93 94 NA NA 108 0.491 0.535 0.506 548 688 716 635 702 696 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.Fi0,0OConstituent was detected above its New Jersey Groundwater Quality Criteria.N N ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed, 03/05/2008 5:52 PM Page 27 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample I Tritium I Major Cations and Anions Identification I Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z Well- Z 04/17/06 05/02/06 05/16/06 06/06/06 06/19/06 07/11/06 07/24/06 08/07/06 08/22/06 09/07/06 09/19/06 10/09/06 10/24/06 11/01/06 11/15/06 12/07/06 12/18/06 01/14/07 02/20/07 03/14/07 04/19/07 05/16/07 06/19/07 07/12/07 08/16/07 09/20/07 10/04/07 11/20/07 12/20/07-160'153'151-163-155 194 211'157 217-160-163'160-160-162 248'203'175'155-152'164 217-143 154-150-146 156 173'147-138 160 153 151 163 155 159 151 157 161 160 163 160 160 162 155 203 175 155 152 164 160 143 148 150 146 145 153 147 138 96 93 93 99 94 98 93 96 99 97 99 95 97 97 96 120 107 94 91 98 99 85 90 90 88 89 94 90 83 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.2oob Constituent was detected above its New Jersey Groundwater Quality Criteria.* ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 28 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium I Major Cations and Anions Identification Date Note Result (pCi/L)I LLD I Deviation I Boron(mg/L)

I Sodium(mg/L)

Well-AA Well-AA Well-AA Well-AA Well-AA WeIl-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA We1l-AA WelI-AA Well-AA Well-AA Well-AA 10/27/03 11/10/03 11/19/03 11/24/03 12/10/03 12/22/03 01/06/04 02/09/04 02/19/04 03/18/04 04/12/04 05/03/04 05/19/04 06/23/04 07/29/04 08/02/04 08/31/04 09/08/04 10/11/04 11/08/04 12/14/04 01/11/05 02/02/05 02/02/05 03/07/05 04/06/05 05/02/05 06/06/05 07/06/05 08/01/05 613 645 3,750 639 785 682 713 1,130 ,5,390 2,610 3,140-5,590ý3,320 4,376 1,650 1,580 1,543 1,512 1,529 1,927ý3,230 6,640 11,100 11,150 16,136 14,547 13,174 141 141 NA 145 141 142 141 139 5,390 140 140 5,590 3,320 142 156 148 159 152 146 152 3,230 151 154 155 142 4,220 3,320 150 150 155 93 94 NA 96 96 95 95 100 NA 120 126 1,770 1,198 141 118 112 118 113 110 118 1,130 168 205 205 260 2,970 2,310 235 226 220 0.25 2.40E-01<3.3<3.33 0.59 253 169 168 138 147 0.036 152 Notes.LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.2 1 ýoii( Constituent was detected above its New Jersey Groundwater Quality Criteria.ot Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM 0 Page 29 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date INoteJResult (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA Well-AA 09/06/05 09/07/05 10/03/05 11/01/05 12/08/05 01/10/06 02/06/06 03/06/06 04/04/06 05/01/06 06/06/06 07/17/06 08/08/06 09/06/06 10/09/06 11/02/06 12/08/06 01/13/07 02/05/07 03/07/07 04/19/07 05/15/07 06/18/07 07/13/07 08/15/07 09/19/07 10/03/07 11/14/07 12/12/07 I 15,887 13,500 10,930 8,911 5,255 6,416 5,683 4,251 3,483 3,625 2,813 2,745 2,647 2,651 2,302 2,413 1,847 2,236 1,518 1,871 1,805 1,422 1,336 1,569 1,423 1,238 1,460 1,166 1,521 150 4,940 148 159 147 159 182 157 158 149 168 162 157 158 158 167 179 161 147 155 158 167 144 148 144 150 161 141 137 234 2,271 199 189 151 168 177 146 140 137 138 133 129 130 126 133 134 128 110 120 121 120 105 110 106 107 119 103 104 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.f C onstituent was detected above its New Jersey Groundwater Quality Criteria.Tt Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 30 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sampl Identification Date Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB 10/28/03 11/02/03 11/19/03 12/04/03 12/16/03 12/16/03 01/14/04 02/17/04 03/03/04 04/06/04 05/04/04 05/11/04 05/19/04 05/24/04 06/03/04 06/17/04 07/07/04 07/12/04 07/19/04 07/28/04 08/02/04 08/09/04 08/16/04 08/25/04 09/01/04 09/08/04 09/13/04 09/22/04 10/04/04 10/12/04 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.rlO;O Constituent was detected above its New Jersey Groundwater Quality Criteria.NA Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM 0 Page 31 of67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification I Date Note Result (pCiJL) LLD Deviation I Boron(mgIL)

I Sodium(mgfL)

Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB Well-AB 10/18/04 11/03/04 11/08/04 11/15/04 11/29/04 12/13/04 01/11/05 01/27/05 01/31/05 02/01/05 02/08/05 03/02/05 03/07/05 03/14/05 03/23/05 03/28/05 04/18/05 05/18/05 06/22/05 08/15/05 10/17/05 11/15/05 12/12/05 01/24/06 02/23/06 03/21/06 04/17/06 05/15/06 06/20/06 07/24/06 112,ooo 1 (,7jý00 101,0011 163 MOO 14oý000 I 42"Ool)I t10,000ý1'ý 6. 0 1) 1)155,000 141,000 1 1 ý 3 ý 6 1611,000 163.000 224M00 97..j(j(j 71 ý000 5.900 49,201)18.900 48ýý()O 2,3 0 0 39.800 43,101)3,230 2,720 3,230 3,910 2,650 3,230 3,910 2,470 4,560 2,650 4,660 144 3,490 4,320 3,790 6,280 4,420 3,490 3,750 3,905 3,790 3,430 4,370 3,550 3,920 3,730 5,510 5,000 4,890 5,470 5,340 5,850 5,650 5,800 5,730 5,410 5,330 5,650 5,770 5,630 5,560 664 5,770 5,760 5,830 5,920 5,470 7,050 4,460 3,950 3,730 3,740 3,600 3,480 3,200 3,580 3,990 3,590 3,680 3,540 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.1,00Constituent was detected above its New Jersey Groundwater Quality Criteria.NNot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 32 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AB 09/21/06 1 '4 2 7,550 3,700 --Well-AB 01/23/07 ;'014 159 158 Well-AB 02/06/07 4S.ý, , 172 387 -- -Well-AB 06/19/07 331.11 145 316 -- -Well-AB 08/23/07 24.1,; 141 283 ---Well-AB 09/20/07 25MSI 148 283 --Well-AB 10/17/07 _ 23,16 151 286 ....Well-AC 10/28/03 1 101901 NA NA 253 31 Well-AC 11/03/03 332 -Well-AC 11/03/03 1 14,20.009 NA NA 332 30 Well-AC 11/18/03 1 14200,0 NA NA -- -Well-AC 11/18/03 1 NA NA ---Well-AC 12/18/03 1 1 NA NA ---Well-AC 01/20/04 1 11170.160 NA NA --Well-AC 02/18/04 1 9110/000 NA NA --Well-AC 03/18/04 1 6 60I000 NA NA --Well-AC 04/08/04 1 5,822 36,309 --Well-AC 06/04/04 1 3,400011) 6,283 26,713 <3.3 12 Well-AC 07/07/04 1 2,770,001 3,360 23,200 -- --Well-AC 07/28/04 1 3,200,000 4,280 25,100 --Well-AC 08/02/04 1 2.840,.00 3,320 23,400 --Well-AC 08/09/04 1 2,230 4,850 20,900 17.90 71 Well-AC 08/16/04 1 2,15(omo 3,320 20,400 --Well-AC 08/25/04 1 2 3,030 19,900 -- -Well-AC 09/01/04 1 1,940000 4,520 19,400 ---Well-AC 01/11/05 1 h94000 3,910 11,600 ....Well-AC 01/17/05 1 3,360 11,600 -- -Well-AC 02/09/05 1 ()(H 4,660 11,200 ---Well-AC 04/29/05 1 2'4tm 3,320 2,650 ---Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.o Constituent was detected above its New Jersey Groundwater Quality Criteria.N ot Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 33 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Identification Date Well-AC 05/24/05 Well-AC 06/16/05 Well-AC 07/29/05 Well-AC 08/18/05 Well-AC 09/26/05 Well-AC 11/21/05 Well-AC 12/12/05 Well-AC 01/12/06 Well-AC 02/28/06 Well-AC 03/23/06 Well-AC 06/16/06 Well-AC 07/14/06 Well-AC 08/23/06 Well-AC 09/27/06 Well-AC 11/17/06 Well-AC 12/28/06 Well-AC 01/22/07 Well-AC 02/12/07 Well-AC 03/27/07 Well-AC 04/23/07 Well-AC 05/10/07 Well-AC 06/19/07 Well-AC 07/30/07 Well-AC 08/28/07 Well-AC 10/30/07 Well-AC 11/27/07 Well-AC 12/29/07 I Well-AD 110/27/03 1 1 244000 NA NA -I Well-AD 11/02/03 1 42,000 NA NA -Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.L[ 0IConstituent was detected above its New Jersey Groundwater Quality Criteria.IN ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 34 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Identification Date Tritium Major Cations and Anions LLD Deviation Boron(mg/L)

I Sodium(mg/L)

-4. 4.Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD Well-AD 11/17/03 12/04/03 12/04/03 12/16/03 12/16/03 01/14/04 02/17/04 03/03/04 04/06/04 05/04/04 05/11/04 05/19/04 06/03/04 06/17/04 07/07/04 07/12/04 07/19/04 07/28/04 08/02/04 08/09/04 08/16/04 12/28/04 03/02/05 03/07/05 03/14/05 03/23/05 03/28/05 04/18/05 05/18/05 06/22/05 NA NA NA NA NA NA NA NA 4,706 5,589 5,392 5,780 4,563 5,666 3,360 3,620 2,870 4,280 3,030 4,850 3,320 4,060 3,670 3,490 4,320 3,790 6,280 4,420 3,490 3,750 NA NA NA NA NA NA NA NA 10,418 11,649 11,469 11,152 12,461 12,887 11,900 12,300 12,100 12,500 12,600 1,230 13,000 1,130 11,700 11,300 12,100 10,700 3,640 10,000 9,320 8,160 5.8<3.3<3.3 12.00 12.80 65 109 71 81 90 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.-o----]Constituent was detected above its New Jersey Groundwater Quality Criteria.IXN ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 35 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AD 07/19/05 1 296MOO 3,750 7,610 --Well-AD 08/15/05 1 213.000 3,905 6,575 --Well-AD 10/17/05 1 224.000 3,790 7,010 ....Well-AD 11/15/05 1 2070)0 3,430 6,700 --Well-AD 12/12/05 1 15LOO11 4,370 5,860 --Well-AD 01/24/06 1 1 f1000 3,550 5,710 --Well-AD 02/23/06 1 1 35000 3,920 5,640 ---Well-AD 03/21/06 1 115,000 3,730 5,330 --Well-AD 04/17/06 1 106000 5,510 5,460 --Well-AD 05/15/06 1 17.000 5,000 5,780 --Well-AD 06/20/06 1 82.700 4,890 4,870 --Well-AD 07/24/06 1 81130 5,470 4,650 ....Well-AD 08/22/06 1 81,2111 2,520 2,100 -- -Well-AD 09/21/06 1 6t900 7,550 4,240 ---Well-AD 10/06/06 1 '73,6001 6,270 4,430 --Well-AD 11/16/06 6,4 168 517 --W,ell-AD 12/15/06 72.300 147 471 --Well-AD 01/23/07 1.873 155 481 --Well-AD 02/06/07 1 01901) 4,370 4,130 --Well-AD 03/14/07 1 50 4,020 3,770 -- -Well-AD 06/19/07 1 _0 3,430 4,300 --Well-AD 07/19/07 1 0 .700 4,530 4,200 --Well-AD 08/23/07 1 71.300 4,280 4,520 --Well-AD 09/20/07 0 146 431 --Well-AD 10/17/07 4.284' 167 416 ....Well-AD 11/15/07 '43.o2 123 351 ---Well-AD 12/13/07 47,643 148 376 --Well-AE 110/27/03 5,9910 145 156 0.23 14 Well-AE 11/02/03 1 5,710 NA NA --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.4 Constituent was detected above its New Jersey Groundwater Quality Criteria.N ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 36 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)I LLD I Deviation Boron(mg/L)

I Sodium(mg/L)

Well-AE WeIl-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE Well-AE 11/19/03 12/04/03 12/18/03 12/18/03 01/14/04 02/09/04 02/09/04 03/03/04 03/18/04 04/28/04 05/03/04 06/17/04 07/13/04 08/16/04 09/22/04 10/18/04 11/22/04 12/16/04 01/18/05 02/08/05 03/08/05 04/11/05 05/10/05 06/07/05 07/06/05 08/02/05 09/07/05 10/04/05 11/02/05 12/09/05 I 6,910 10,200 15,800 16,100 16,100 16,600 19,200 17,000 19,000 14,900 14,000 7,810 7,820 7,238 5,939 5,375 4,636-3,230 7,530 10,100 13,026 8,832 9,305 7,741 6,336 4,947 3,384 3,305 3,592 5,123 NA 146 147 NA 144 139 NA 147 145 140 5,589 5,666 149 151 140 150 152 3,230 164 147 142 157 147 147 148 148 150 152 151 153 NA 190 229 NA 229 232 NA 237 248 220 2,409 2,152 175 173 156 156 149 1,200 185 192 212 192 187 173 162 149 134 135 136 154 0.17 10 0.09<3.33 8 11 0.099 11 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.[ Constituent was detected above its New Jersey Groundwater Quality Criteria.N ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 37 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AE 01/16/06 1 2f 00 3,550 2,390 Well-AE 02/07/06 9,966 149 193 ....Well-AE 03/07/06 1 13,400 3,310 2,000 --Well-AE 04/04/06 9,924 161 200 --Well-AE 05/02/06 7,075 150 171 -- -WelU-AE 06/19/06 3,945 151 141 ---Well-AE 07/17/06 4,379 160 150 --Well-AE 08/21/06 3,822 152 140 --Well-AE 09/18/06 11,860 167 219 --Well-AE 10/05/06 4,300 161 151 -- -Well-AE 11/02/06 5,226 161 160 --Well-AE 12/07/06 5,000 172 167 --Well-AE 01/13/07 4,289 156 150 -- -Well-AE 02/24/07 5,721 170 171 --Well-AE 03/07/07 4,749 143 146 --Well-AE 04/20/07 5,233 156 159 --Well-AE 05/16/07 8,428 153 182 ....Well-AE 06/18/07 6,863 146 164 --Well-AE 07/19/07 5,663 146 153 --Well-AE 08/15/07 5,174 147 149 ---Well-AE 09/19/07 4,064 144 137 ....Well-AE 10/04/07 4,065 158 149 --Well-AE 11/19/07 4,673 151 153 --Well-AE 12/12/07 4,998 148 148 --Well-AF 10/07/03 142 142 86 0.38 227 Well-AF 10/27/03 242 145 90 --WeIl-AF 10/27/03 I -2,430 2,430 NA -- -Well-AF 11/10/03 330 144 91 -- --Well-AF 11/24/03 245 146 91 0.43 545 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.L 20104 Constituent was detected above its New Jersey Groundwater Quality Criteria.-N---Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 3 8 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification I Date Note Result (pCi/L) I LLD Deviation I Boron(mg/L)

I Sodium(mg/L)

Well-AF Well-AF Well-AF'Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF Well-AF 12/10/03 12/22/03 01/06/04 01/20/04 02/02/04 03/18/04 04/20/04 05/03/04 06/25/04 07/13/04 08/16/04 09/23/04 10/12/04 11/16/04 12/21/04 01/11/05 02/08/05 03/14/05 04/11/05 05/09/05 07/11/05 10/17/05 01/16/06 04/10/06 07/17/06 10/09/06 01/22/07 04/19/07 07/13/07 10/09/07 343 302 366 262 295 150 247 308 301 270 177 241-151 168'3,910-3,910'154-4,320 363 245 193 182 264 244 372 249 347 223 210-173 140 141 142 143 144 144 141 141 144 145 156 147 151 153 3,910 3,910 154 4,320 148 143 152 157 152 156 154 162 158 165 146 173 89 89 90 89 91 88 88 89 90 91 96 92 90 94 1,130 1,180 94 1,240 94 89 93 96 95 97 97 100 99 102 90 101 4.80E-01 0.523 0.644 654 766 843 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.F2,0[Q7 Constituent was detected above its New Jersey Groundwater Quality Criteria.NA Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 39 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for, Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium I Major Cations and Anion/Identification Date INote lResult (pCiIL) ILLD IDeviation IBoron(mg/L)

ISodiummgL Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D WelI-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D WelI-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D WelI-AG-D Well-AG-D Well-AG-D 02/23/04 03/09/04 03/29/04 04/12/04 04/19/04 04/28/04 05/03/04 05/10/04 05/24/04 05/28/04 06/03/04 06/08/04 06/16/04 06/25/04 07/07/04 07/14/04 07/19/04 07/28/04 08/09/04 08/23/04 09/13/04 09/29/04 10/05/04 10/18/04 11/04/04 11/09/04 11/15/04 11/22/04 11/29/04 6,100 3,280 2,540 4,990 2,920 896<5,590 1,490 1,290"4,560 4,040 13,625 566 1,865 2,698 3,426 2,718 2,939 4,217 6,538 7,191 13,241 8,613 12,456 7,424 11,993 3,813 8,860 140 149 151 141 141 135 5,590 140 152 4,560 145 142 154 141 141 142 152 145 148 156 149 148 156 144 139 3,230 150 148 2,650 156 132 125 145 124 95 NA 106 109 1,551 139 214 101 111 121 130 128 127 143 171 172 218 190 209 167 2,690 209 138 1,580 0.34 5.10E-01 0.5 0.38 5.60E-01 0.18 0.539 0.506 0.518 0.533 849 765 868 866 885 239 862 798 826 883 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.I oooj Constituent was detected above its New Jersey Groundwater Quality Criteria.-'Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 40 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium I Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D Well-AG-D WelI-AG-D Well-AG-D Well-AG-D Well-AG-D 12/07/04 12/14/04 12/21/04 12/28/04 01/07/05 01/11/05 01/18/05 01/26/05 02/02/05 02/09/05 02/14/05 02/22/05 03/03/05 03/07/05 03/14/05 03/23/05 03/28/05 04/05/05 04/18/05 05/03/05 05/16/05 06/06/05 07/11/05 08/01/05 09/06/05 10/11/05 11/01/05 12/08/05 01/09/06 02/06/06 ,4,170 6,910'3,910 5,710 6,300 8,700 4,880 4,040 6,455 6,310 5,995 958 1,099 937 1,026 1,203 1,217 764 938 1,380 798 883 884 762 1,170 901 995 712 525 575 4,170 3,230 3,910 4,060 150 143 154 141 155 149 146 155 148 155 143 149 141 169 162 149 144 148 149 144 149 147 150 146 156 177 1,510 1,500 1,370 1,570 166 180 153 139 168 162 159 107 105 106 101 107 102 113 111 109 98 102 102 97 106 101 104 98 101 114 0.823 0.39 0.344 836 1,060 971 958 876 929 858 865 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.F jConstituent was detected above its New Jersey Groundwater Quality Criteria.NA Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 41 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AG-D 03/06/06 620 159 104 --Well-AG-D 04/03/06 270 156 97 ---Well-AG-D 05/01/06 486 152 99 ....Well-AG-D 06/05/06 685 155 102 --Well-AG-D 07/11/06 763 162 108 --Well-AG-D 08/07/06 720 153 102 --Well-AG-D 09/18/06 663 158 104 ....Well-AG-D 10/06/06 413 160 101 ---Well-AG-D 11/15/06 671 160 106 --Well-AG-D 12/08/06 496 198 126 --Well-AG-D 01/14/07 543 159 103 ....Well-AG-D 02/20/07 204 158 97 -- -Well-AG-D 03/14/07 201 179 110 --Well-AG-D 04/19/07 391 175 111 --Well-AG-D 05/03/07 633 141 94 -- -Well-AG-D 06/18/07 716 142 95 ....Well-AG-D 07/12/07 490 151 97 --Well-AG-D 08/16/07 702 147 98 --Well-AG-D 09/20/07 608 144 95 -- -Well-AG-D 10/17/07 2,172 149 118 -- -Well-AG-D 11/20/07 1,491 150 113 --Well-AG-D 12/20/07 905 137 96 --Well-AG-S 02/23/04 2,320 138 115 0.04 348 Well-AG-S 03/09/04 3,000 146 126 ---Well-AG-S 03/29/04 4,810 153 150 --Well-AG-S 04/12/04 6,620 143 161 0.26 319 Well-AG-S 04/20/04 8,060 142 173 0.23 338 Well-AG-S 04/28/04 10,300 136 188 0.19 312 Well-AG-S 05/10/04 9,580 139 184 -Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.F Constituent was detected above its New Jersey Groundwater Quality Criteria.N ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 42 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)I LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S 05/24/04 05/26/04 05/27/04 05/28/04 06/03/04 06/08/04 06/16/04 06/25/04 07/07/04 07/14/04 07/19/04 07/26/04 07/28/04 07/30/04 08/09/04 08/23/04 09/13/04 09/29/04 10/05/04 10/18/04 11/04/04 11/09/04 11/15/04 11/22/04 11/29/04 12/07/04 12/14/04 12/21/04 12/28/04 01/07/05 9,390 11,300 18,300 14,400 17,329 13,226 17,244 13,528 17,361 12,601 15,617 10,430 7,074 11,088 16,353 15,313 1 .300'147 5,780 4,563 4,563 150 154 145 152 147 149 149 3,230 147 4,850 144 3,025 151 160 154 143 150 3,230 3,910 4,220 2,650 4,170 3,230 4,020 4,060 3,910 189 2,281 2,383 2,193 242 220 237 263 217 241 210 2,230 232 2,700 263 2,176 200 179 207 233 231 2,320 2,390 2,350 2,220 2,480 2,330 2,700 2,380 2,610 0.247 0.271 0.243 0.231 0.241 286 300 323 341 315 365 321 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.j (I]Constituent was detected above its New Jersey Groundwater Quality Criteria.N ot Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 43 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification I Date Not Result (pCi/L) I LLD I Deviation I Boron(mg/L)

Sodium(mg/L)

Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S Well-AG-S 01/11/05 01/18/05 01/26/05 02/02/05 02/02/05 02/09/05 02/14/05 02/22/05 03/03/05 03/07/05 03/14/05 03/23/05 03/28/05 04/05/05 04/18/05 05/03/05 05/16/05 06/06/05 07/11/05 08/01/05 09/06/05 10/11/05 11/01/05 12/08/05 01/09/06 02/06/06 03/06/06 04/03/06 05/01/06 06/05/06 11,929 6,944 7,239 7,693 9,248 9,399 9,357 3,472 6,858 2,493 1,007 2,022 3,537 4,295 6,309 4,043 349 744 1,551 1,926 1,616 1,150 639 3,910 3,950 149 2,650 4,660 4,660 3,910 154 158 136 143 147 141 143 152 151 146 148 150 151 151 146 149 150 159 165 157 159 149 158 2,770 2,630 267 2,660 2,810 2,710 2,480 211 174 164 171 187 183 187 138 169 121 103 119 136 144 160 139 95 106 121 120 118 106 103 0.175 0.144 240 426 236 192 567 582 606 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.[ Constituent was detected above its New Jersey Groundwater Quality Criteria.~Not Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 44 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mgfL)

Well-AG-S 07/11/06 499 162 104 --Well-AG-S 08/07/06 453 158 101 --Well-AG-S 09/18/06 403 159 101 --Well-AG-S 10/06/06 339 165 103 ---Well-AG-S 11/15/06 602 158 104 -- -Well-AG-S 12/08/06 487 194 123 -- -Well-AG-S 01/14/07 513 157 102 ---Well-AG-S 01/22/07 1 4,610 4,610 NA --Well-AG-S 02/20/07 406 152 97 --Well-AG-S 03/14/07 336 190 118 -- -Well-AG-S 04/19/07 363 160 101 ---Well-AG-S 05/03/07 201 142 88 ---Well-AG-S 06/18/07 888 141 97 --Well-AG-S 07/12/07 645 150 99 --Well-AG-S 08/16/07 1,101 144 102 --Well-AG-S 09/20/07 671 146 97 --Well-AG-S 11/20/07 304 142 90 --Well-AG-S 12/20/07 343 137 87 ....Well-AH-D 02/23/04 548 142 93 0.21 309 Well-AH-D 03/08/04 620 142 95 --Well-AH-D 03/29/04 522 142 93 0.31 290 Well-AH-D 04/19/04 563 140 93 0.19 241 Well-AH-D 05/03/04 637 142 95 --Well-AH-D 06/03/04 619 157 103 --Well-AH-D 06/16/04 1 <5,670 5,670 1,571 --Well-AH-D 07/19/04 552 147 97 0.191 260 Well-AH-D 08/23/04 586 140 93 -- --Well-AH-D 09/13/04 557 151 99 --Well-AH-D 09/29/04 517 155 101 --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.b oI Constituent was detected above its New Jersey Groundwater Quality Criteria.N-Z Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 45 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample I Tritium I Major Cations and Anions Identification I Date Note Result (pCi/L)I LLD Deviation Boron(mg/L)

I Sodium(mg/L)

Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D WeIl-AH-D Well-AH-D Well-AH-D WelI-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D Well-AH-D WeU-AH-D Well-AH-D Well-AH-D WeIl-AH-D Well-AH-D 10/18/04 11/15/04 12/20/04 01/11/05 02/15/05 03/08/05 04/18/05 05/16/05 06/07/05 07/11/05 08/02/05 09/07/05 10/17/05 11/02/05 12/09/05 01/10/06 02/06/06 03/06/06 04/10/06 05/01/06 06/05/06 07/17/06 08/08/06 09/06/06 10/06/06 11/02/06 12/19/06 01/22/07 02/20/07 03/14/07 308-3,910'3,910 487 493 529 407 492 610 665 599 522 361 403 257 260 264 318 303 439 297 321 330 322 278 430 209 333-177-155 144 3,910 3,910 154 147 146 150 146 148 143 145 151 156 152 151 151 165 156 155 152 157 160 157 161'162 152 159 159 177 155 90 1,328 1,130 100 96 96 96 95 98 96 96 98 99 97 94 94 102 98 97 98 98 100 98 101 101 97 98 100 108 94 0.235 0.298 250 673 654 1,020 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.PROConstituent was detected above its New Jersey Groundwater Quality Criteria.NA Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 46 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AH-D 04/19/07 270 168 104 ---Well-AH-D 05/15/07 ,142 142 86 .....Well-AH-D 06/18/07 343 141 89 --Well-AH-D 07/13/07 221 149 92 ---Well-AH-D 08/15/07 1,089 148 104 ....Well-AH-D 09/19/07 376 145 92 -- -Well-AH-D 10/03/07 1,311 151 109 ---Well-AH-D 11/19/07 920 177 119 -- -Well-AH-D 12/12/07 973 138 97 ---Well-AH-S 02/23/04 899 143 99 0.14 135 Well-AH-S 03/08/04 894 142 98 --Well-AH-S 03/29/04 878 141 97 0.27 56 Well-AH-S 04/20/04 932 141 98 0.25 67 Well-AH-S 05/03/04 908 141 98 ---Well-AH-S 06/03/04 759 149 100 --Well-AH-S 06/16/04 835 142 97 0.263 48 Well-AH-S 07/19/04 816 151 103 0.204 38 Well-AH-S 08/23/04 752 155 105 --Well-AH-S 09/13/04 512 144 94 ---Well-AH-S 09/29/04 533 149 97 ....Well-AH-S 10/18/04 420 159 101 --Well-AH-S 11/15/04 1 43,910 3,910 1,235 --Well-AH-S 12/20/04 1 -3,910 3,910 1,130 --Well-AH-S 01/11/05 658 163 107 0.446 61 Well-AH-S 02/15/05 633 146 97 -- --Well-AH-S 03/08/05 614 147 97 --Well-AH-S 04/18/05 319 146 92 0.138 216 Well-AH-S 05/16/05 249 150 93 -- 277 Well-AH-S 06/07/05 238 147 91 -151 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.Constituent was detected above its New Jersey Groundwater Quality Criteria.Not Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 47 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium I Major Cations and Anions Identification Date Note Result (pCi/L)I LLD Deviation I Boron(mg/L)

I Sodium(mg/L)

Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S Well-AH-S 07/11/05 08/02/05 09/07/05 10/17/05 11/02/05 12/09/05 01/10/06 02/06/06 03/06/06 04/10/06 05/01/06 06/05/06 07/17/06 08/08/06 09/06/06 10/06/06 11/02/06 12/19/06 01/22/07 02/20/07 03/14/07 04/19/07 05/15/07 06/18/07 07/13/07 08/15/07 09/19/07 10/03/07 11/19/07 12/12/07 293 241 162-153 298 218 251 213-158-155 163 190'171 178 211 238 366 252 384 242 248'162 154 236 1,193-145'144 195 2,790 5,579 144 147 149 153 151 148 153 170 158 155 151 156 171 160 157 159 154 163 155 151 149 162 137 142 147 145 144 164 190 142 91 92 91 92 94 91 95 105 94 92 92 96 104 98 97 99 97 101 98 93 93 98 84 88 105 88 88 101 152 150 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.2 0 Constituent was detected above its New Jersey Groundwater Quality Criteria.N9 Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 48 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Wel Sample I Tritium I Major Cations and Anions Identification Date Note Result (pCi/L) I LLD I Deviation Boron(mg/L)

I Sodium(mg/L)

Well-Al Well-Al Well-Al Well-Al Well-AI Well-AI Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-AI Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al 02/02/04 02/26/04 03/11/04 03/30/04 05/04/04 05/11/04 05/19/04 06/03/04 07/19/04 07/28/04 08/02/04 08/09/04 08/16/04 08/25/04 12/27/04 04/19/05 05/10/05 06/21/05 07/12/05 08/15/05 09/06/05 10/10/05 11/14/05 12/20/05 01/17/06 02/21/06 03/20/06 04/10/06 04/11/06ý5,780 4,360 4,370 3,550 11,800 13,120 13,120 14,060 7,683 6,669 5,081 4,535 3,602 2,755 2,730 4,200-4,720 5,194 5,780 140 145 143 140 5,392 5,780 4,563 2,870 3,790 3,320 4,850 3,320 3,030 153 153 3,620 3,750 155 147 150 148 152 156 150 149 3,730 4,720 157 NA 138 141 131 200 3,466 3,439 3,360 2,550 2,650 2,670 3,030 3,000 3,050 222 222 2,640 2,820 226 172 166 151 148 139 127 126 1,530 NA 156 0.05 0.17<3.3 8 16 47 28 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.ýijij'O 1 Constituent was detected above its New Jersey Groundwater Quality Criteria.-N7Not Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 49 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-Al 05/16/06 2,354 149 122 --Well-A] 06/19/06 2,082 162 126 -- -Well-AL 07/18/06 1,572 150 112 ...Well-Al 07/19/06 1 -4,890 4,890 NA --Well-Al 08/08/06 1,621 160 118 ---Well-Al 09/18/06 1,782 157 119 -- -Well-Al 10/10/06 2,110 159 124 ---Well-Al 11/01/06 1,543 157 116 -- -Well-Al 12/18/06 2,495 178 142 --Well-Al 12/19/06 1 -4,840 4,840 NA --Well-Al 01/13/07 2,784 149 127 --Well-Al 02/06/07 2,393 157 127 ....Well-Al 03/08/07 2,100 149 119 -- -Well-Al 04/20/07 2,677 161 134 --Well-Al 05/15/07 2,556 140 119 --Well-Al 06/18/07 2,867 142 123 --Well-Al 07/18/07 2,784 145 123 -- -Well-Al 08/15/07 3,204 143 128 --Well-Al 09/20/07 3,137 150 131 -- -Well-Al 10/03/07 3,360 149 132 ....Well-Al 11/14/07 3,173 154 138 --Well-Al 12/12/07 2,902 138 121 --Well-AJ 02/25/04 1,150 142 102 0.62 616 Well-Al 03/09/04 1,040 140 99 0.68 650 Well-Al 03/30/04 1,080 146 103 0.62 642 Well-AJ 04/19/04 1,190 139 101 0.67 621 Well-AJ 05/10/04 1,240 142 103 --Well-Al 05/24/04 1,270 158 113 --Well-Al 06/16/04 1,495 148 111 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.[ C onstituent was detected above its New Jersey Groundwater Quality Criteria.NANot Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 50 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L)I LLD Deviation I Boron(mg/L)

I Sodium(mg/L)

Well-AJ Well-AJ Well-AJ Well-AJ Well-AJ Well-Al Well-Al Well-AJ Well-AJ Well-Al Well-Al Well-Al Well-Al Well-Al Well-AJ Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-Al Well-AJ Well-Al Well-Al Well-Al 07/13/04 07/20/04 08/16/04 09/08/04 10/18/04 11/16/04 12/28/04 01/12/05 02/14/05 03/02/05 03/07/05 03/14/05 03/23/05 03/28/05 04/18/05 05/18/05 08/15/05 10/17/05 11/15/05 12/12/05 01/24/06 02/23/06 03/21/06 04/17/06 05/15/06 07/24/06 08/22/06 06/19/07 2,193 1,525 1,677 4,254 343,000 218,00 142 152 141 152 3,230 3,910 2,820 3,910 3,910 3,670 3,490 4,320 3,790 6,280 4,420 3,490 3,905 3,790 3,430 4,370 3,550 3,920 3,730 5,510 5,000 5,470 2,520 150 116 113 110 146 3,560 6,440 5,450 8,540 8,260 6,710 5,670 6,120 3,720 5,880 5,490 4,900 3,877 6,330 3,770 5,750 3,520 3,280 4,120 4,030 3,780 3,500 1,340 329~~-a-0 0aaa Well-AL 02/25/04 -141 141 83 0.21 60 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.[wiConstituent was detected above its New Jersey Groundwater Quality Criteria.N Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 51 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample I Tritium _Major Cations and Anions Identification Date Note Result (pCi/L)I LLD I Deviation Boron(mg/L)

Sodium(mg/L)

Well-AL WelI-AL WellAL WelI-AL WelI-AL WeI1-AL WelI-AL WelI-AL WelI-AL Well-AL WeI1-AL Well-AL WeI1-AL WeI1-AL WelI-AL WelI-AL WeI1-AL WelI-AL WeI1-AL WelI-AL WelI-AL WeI1-AL WeI1-AL Well-AL Well-AL Well-AL WeI1-AL 03/09/04 03/30/04 04/19/04 05/19/04 06/16/04 07/13/04 07/28/04 08/16/04 09/08/04 10/12/04 11/16/04 12/21/04 01/11/05 02/08/05 03/14/05 04/11/05 05/09/05 07/11/05 10/10/05 01/23/06 04/10/06 07/17/06 10/09/06 01/13/07 04/19/07 07/19/07 10/09/07 1 1-147 ,146 ,141 ,151 ,141ý 141-147 , 150 ,153 , 146 ,3,910-3,910-157 ,157 ,146<158-150< 154-148-153<,165-154< 162-153 243 203-175 147 146 141 151 141 141 147 150 153 146 3,910 3,910 157 157 146 158 150 154 148 153 165 154 162 153 158 146 175 86 86 85 89 85 85 88 91 91 85 1,126 1,130 92 92 87 93 88 90 89.91 99 92 97 91 98 90 103 0.20 0.22 0.3 55 63 62 0.23 74 Well-AL 10/09/07 '175 175 103 Well-AM 02/02/04 425 0 NA N I A Well-AM 02/26/04 1 NA NA -Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.IEOOODConstituent was detected above its New Jersey Groundwater Quality Criteria."Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 52 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium I Major Cations and Anions Identification I Date Note Result (pCi/L)I LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM 02/26/04 03/11/04 03/11/04 04/08/04 04/08/04 05/06/04 05/06/04 05/20/04 06/10/04 07/20/04 08/17/04 09/14/04 10/25/04 11/23/04 12/27/04 01/12/05 02/22/05 03/15/05 04/19/05 05/17/05 06/21/05 07/11/05 08/15/05 09/20/05 10/10/05 11/14/05 12/20/05 01/23/06 02/23/06 03/21/06 273Jb00 1A96M00O 1~28,000 139MOO ~NA NA NA 5,822 5,822 5,589 5,589 4,563 4,974 2,870 3,320 4,560 3,030 4,220 4,060 3,910 3,550 4,320 4,420 3,490 3,750 3,750 3,905 4,563 3,790 3,430 3,430 3,550 3,920 3,730 NA NA NA 6,425 6,425 5,807 5,807 5,651 5,832 5,020 5,270 5,380 5,080 4,940 4,590 4,660 4,340 4,100 3,570 3,480 3,420 3,110 2,979 4,478 2,930 3,210 2,580 2,750 4,200 10,100<3.3<3.33 6 6 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.~,)Constituent was detected above its New Jersey Groundwater Quality Criteria.'Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM 0 Page 53 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium I Major Cations and Anions Identification Date I Note Result (pCi/L)I LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM Well-AM 04/11/06 05/16/06 06/20/06 07/17/06 07/21/06 08/08/06 08/21/06 09/07/06 09/13/06 09/19/06 10/09/06 11/01/06 11/15/06 12/07/06 12/18/06 01/13/07 01/22/07 02/06/07 02/23/07 03/08/07 04/20/07 05/15/07 06/19/07 07/18/07 07/30/07 08/15/07 09/21/07 09/25/07 10/03/07 10/17/07 1 1 1 1 17,003 18,191 19,530~39050'5U1&004 4,720 5,000 4,890 4,670 NA NA 2,520 151 NA 161 156 162 162 153 148 148 155 162 157 149 160 174 3,430 146 139 148 3,830 3,730 3,830 4,370 13,700 15,100 12,100 5,130 NA NA 3,590 241 NA 257 261 275 290 330 352 266 294 311 407 266 275 363 3,730 335 321 342 7,330 7,950 7,550 5,690 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter I Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.0(0,o2Constituent was detected above its New Jersey Groundwater Quality Criteria.NKNot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM 0 Page 54 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AM 11/14/07 1 1 4,110 5,210 --Well-AM 11/28/07 1 14U1ýO0<q 3,630 5,330 ....Well-AM 12/12/07 2 150 272.Well-AM 12/27/07 19,329 149 250 --Well-AN 08/10/04 .2l1579 143 263 0.685 32 Well-AN 08/24/04 19,632 155 263 --Well-AN 09/14/04 9,150 141 182 0.567 23 Well-AN 10/25/04 8,950 147 185 -- -Well-AN 11/23/04 6,245 144 158 --Well-AN 12/29/04 1 -4,020 4,020 1,210 --Well-AN 01/12/05 6,180 159 169 --Well-AN 03/02/05 1 192,000 3,670 6,300 -- -Well-AN 03/07/05 1 171,0011 3,490 5,940 -- -Well-AN 03/14/05 1 1 ;1.000 4,320 5,700 --Well-AN 03/23/05 1 3,790 6,030 Well-AN 03/28/05 1 9 9,00 6,280 4,900 -- -Well-AN 04/18/05 1 1494000 4,420 5,650 --Well-AN 05/18/05 1 11.010 3,490 4,920 -- -Well-AN 06/22/05 1 48000 3,750 4,470 --Well-AN 07/19/05 148 479 -- -Well-AN 08/15/05 1 (9.000 3,905 3,879 Well-AN 10/17/05 1 7c1,]( ( 3,790 4,150 --Well-AN 11/15/05 1 6 -3,430 4,860 -- -Well-AN 12/12/05 1 7_.40 4,370 4,260 --Well-AN 01/24/06 1 '99J00 3,550 4,800 --Well-AN 02/22/06 "8'29 149 485 --Well-AN 02/23/06 1 65,600 3,920 4,030 ---Well-AN 03/21/06 1 3,730 4,630 ....Well-AN 04/17/06 1 5 5,510 4,070 --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.2 11()j -Constituent was detected above its New Jersey Groundwater Quality Criteria.NANot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 55 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AN 05/15/06 1 40300 5,000 4,870 --Well-AN 06/20/06 1 76400 4,890 4,730 Well-AN 07/24/06 1 S4.800 5,470 3,930 --Well-AN 08/22/06 1 1111 2,520 2,320 ..Well-AN 09/21/06 1 82401 7,550 4,720 Well-AN 10/06/06 3,169 161 138 --Well-AN 11/16/06 1 89AMO 3,630 4,680 ---Well-AN 12/15/06 Z 3 158 286 Well-AN 01/23/07 5,973 154 164 --Well-AN 02/06/07 43 181 404 Well-AN 08/23/07 27M7ý 143 289 Well-AN 09/20/07 79.768 151 492 Well-AN 10/17/07 4 1,105 158 381 Well-AN 11/15/07 1 54A00 4,110 3,930 Well-AN 12/13/07 1 f 4,030 4,300 --Well-AO 07/29/04 6,739 146 163 --Well-AO 08/10/04 2,399 153 125 0.24 27 Well-AO 08/16/04 5,420 146 155 --Well-AO 08/24/04 2,225 155 125 --Well-AO 09/14/04 2,417 149 123 --Well-AO 09/29/04 2,794 152 130 --Well-AO 10/25/04 2,706 158 132 --Well-AO 11/23/04 2,570 147 123 --Well-AO 12/27/04 1 '4,060 4,060 1,370 --Well-AO 01/12/05 1,780 166 125 --Well-AO 03/02/05 1 15,900 3,670 2,100 ....Well-AO 03/07/05 1 1 ;8,000 3,490 5,710 Well-AO 03/14/05 1 138,00 4,320 5,430 Well-AO 03/23/05 1 1 000 3,790 6,570 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit._001)Constituent was detected above its New Jersey Groundwater Quality Criteria.tot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 56 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AO 03/28/05 6,395 147 .162 --Well-AO 11/15/05 1 34.7()j) 3,430 2,900 ....Well-AO 12/12/05 1 58.000 4,370 3,750 Well-AO 07/24/06 1 38A00 5,470 3,410 --Well-AO 08/22/06 1 98J100 2,520 2,290 Well-AO 10/06/06 4,190 160 148 --Well-AO 11/16/06 .... ' 164 301 ---Well-AO 12/15/06 7,629 168 190 -- -Well-AO 01/23/07 5,136 154 154 Well-AP 07/19/04 2,078 148 118 0.06 59 Well-AP 08/09/04 1,455 150 112 0.126 105 WeIl-AP 08/23/04 1,006 151 106 --Well-AP 09/08/04 1,039 148 105 --Well-AP 09/22/04 1,679 156 119 ---Well-AP 10/11/04 777 151 102 -- -Well-AP 11/22/04 1,531 150 112 0.204 65 Well-AP 12/14/04 1 ,3,230 3,230 984 --Well-AP 01/27/05 1,200 138 102 0.16 134 Well-AP 02/01/05 2,680 153 128 -- -Well-AP 03/07/05 1 .03j 7 3,490 3,970 Well-AP 04/05/05 1 1011,000 4,220 4,730 Well-AP 05/02/05 1 '94,40 3,320 1,690 --Well-AP 06/06/05 1 106,00 3,460 4,630 -Well-AP 06/21/05 1 46j(10 3,750 3,220 -Well-AP 07/06/05 1,968 144 114 ---Well-AP 07/19/05 4,563 148 145 --Well-AP 08/01/05 1 6,190 3,320 3,640 -- -Well-AP 08/16/05 1 3,905 2,564 Well-AP 08/29/05 961 151 105 --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit."21'o constituent was detected above its New Jersey Groundwater Quality Criteria.NANot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 57 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium I Major Cations and Anions Identification Date Note Result (pCi/L) I LLD Deviation I Boron(mg/L)

Sodium(mglL)

Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP Well-AP 09/06/05 09/19/05 10/03/05 10/18/05 11/01/05 12/08/05 01/10/06 02/07/06 02/21/06 03/06/06 03/20/06 04/03/06 04/17/06 05/01/06 05/15/06 06/05/06 06/20/06 07/10/06 07/24/06 08/07/06 08/21/06 09/06/06 10/10/06 11/01/06 12/08/06 01/13/07 02/05/07 03/07/07 04/19/07 05/15/07 1,196 10,097 12,250 798 14,354 9,723 14,580 9,829 8,860 9,490 8,284 8,316 7,686 5,639 5,681 757 465 2,006 4,405 2,560 5,939 779 5,412 1,086 4,348 1,169 1,059 781 150 152 4,220 156 149 3,730 152 152 152 161 3,730 155 158 154 158 167 150 157 152 159 153 157 161 153 186 156 151 151 158 186 107 195 3,530 212 101 2,750 225 191 226 199 1,850 192 184 184 180 167 158 105 98 123 147 128 166 103 179 109 145 109 111 123 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.kq ]C onstituent was detected above its New Jersey Groundwater Quality Criteria.N ot Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 58 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AP 06/18/07 1,093 145 102 ....Well-AP 07/18/07 1,049 144 101 --Well-AP 08/15/07 2,730 144 122 --Well-AP 09/19/07 3,830 161 144 --Well-AP 10/03/07 3,442 150 133 ....Well-AP 11/14/07 4,025 124 128 ....Well-AP 12/12/07 3,806 137 130 --Well-AQ 07/08/04 1 '3,260 3,260 1,094 -- -Well-AQ 07/19/04 217 142 88 0.436 308 Well-AQ 08/09/04 309 152 95 0.57 1,090 Well-AQ 08/23/04 243 147 92 ---Well-AQ 09/08/04 273 150 94 -- -Well-AQ 09/22/04 213 138 86 --WeIl-AQ 10/26/04 201 144 89 -- -Well-AQ 11/16/04 218 147 91 --Well-AQ 12/21/04 1 '4,280 4,280 i,300 --Well-AQ 01/27/05 225 135 84 -Well-AQ 02/02/05 -148 148 90 0.448 1,100 Well-AQ 03/14/05 367 145 92 --Well-AQ 04/12/05 247 143 89 --Well-AQ 05/09/05 248 151 94 -- -Well-AR 07/14/04 1 324A& 3,620 7,980 ---Well-AR 07/19/04 1 39000 2,870 8,700 Well-AR 08/09/04 1 464.000 4,850 9,620 6.00 75 Well-AR 08/23/04 1 49(),100 3,670 10,000 --Well-AR 09/13/04 1 5;1.000 4,560 10,500 7.10 65 Well-AR 09/30/04 1 ý'00Ok 5,780 10,800 ---Well-AR 10/26/04 1 500 3,030 11,000 Well-AR 12/28/04 1 423 4,060 9,050 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.Fiýo Constituent was detected above its New Jersey Groundwater Quality Criteria.--ýNot Available

-Deviation and/or LLD were not reported.-- Constituent not analyzed.03/05/2008 5:52 PM Page 59 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date NotejResult (pCi/L)I LLD I Deviation Boron(mg/L)

Sodium(mg/L)

Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR ,Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR Well-AR 01/27/05 02/22/05 03/14/05 04/12/05 05/10/05 06/21/05 07/19/05 08/16/05 09/19/05 10/10/05 11/02/05 12/08/05 01/10/06 02/06/06 03/20/06 04/10/06 05/15/06 06/06/06 07/17/06 08/08/06 09/06/06 10/10/06 11/02/06 12/18/06 12/19/06 01/13/07 02/05/07 03/07/07 06/18/07 07/19/07!33U.00 206,570 12,5550 212,751 22A100 12,61901 2,470 3,550 4,320 4,220 3,620 3,750 2,820 3,905 4,563 3,790 3,030 3,730 4,370 3,090 3,730 155 156 162 4,670 4,440 157 158 169 155 4,840 3,730 4,370 3,630 3,430 4,370 8,140 8,220 6,510 7,010 6,420 6,670 6,310 6,592 6,272 5,540 6,560 6,090 6,250 4,810 3,510 240 215 221 5,000 4,330 273 216 506 447 4,060 4,700 4,350 4,110 4,620 4,780 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.IooW]Constituent was detected above its New Jersey Groundwater Quality Criteria.N ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 60 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AR 07/23/07 1 S2,3 0 1,840 2,180 ....Well-AR 08/08/07 1 8 4,110 4,390 ---Well-AR 08/15/07 1 84700: 3,830 4,760 -- -Well-AR 09/19/07 1 51'S00 3,830 3,760 -- -Well-AR 09/25/07 1 1_400 3,730 4,170 ....Well-AR 10/03/07 20i 157 267 --Well-AR 10/17/07 12,266 137 200 --Well-AR 11/14/07 1 5-.900. 4,110 3,940 --Well-AR 11/28/07 L;0'018 123 374 --Well-AR 12/12/07 47.105 146 373 --Well-AR 12/27/07 43.,89 149 360 ....Well-AS 07/08/04 1 ;,700 3,620 2,920 --Well-AS 07/19/04 1 27.600 2,870 2,460 ---Well-AS 08/09/04 1 7,510 4,850 1,920 --Well-AS 08/23/04 1 300 3,030 2,990 --Well-AS 09/13/04 145 259 0.727 199 Well-AS 09/29/04 18,171 146 248 --Well-AS 10/11/04 9,899 156 200 --Well-AS 11/16/04 1 14,400 3,910 2,090 --Well-AS 12/21/04 1 15,200 3,910 2,070 --Well-AS 01/27/05 14,000 143 224 0.459 186 Well-AS 03/02/05 1 '23.460 3,670 2,430 -- -Well-AS 03/07/05 1 3,490 3,020 ---Well-AS 03/14/05 1 12,600 4,320 2,080 -- -Well-AS 03/23/05 1 7 200 3,790 4,050 -- -Well-AS 03/28/05 1 (76 6,280 4,180 -- -Well-AS 04/18/05 1 7 0j 4,420 4,140 --Well-AS 05/18/05 1 5 3,490 3,520 --Well-AS 06/22/05 1 6 3,750 3,730 --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.F'O]Constituent was detected above its New Jersey Groundwater Quality Criteria.Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.0 03/05/2008 5:52 PM Page 61 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium I Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

I Sodium(mg/L)

Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS Well-AS 07/19/05 08/15/05 10/17/05 11/15/05 12/12/05 01/24/06 02/23/06 03/21/06 04/17/06 05/15/06 06/20/06 07/24/06 08/22/06 09/21/06 10/06/06 11/16/06 12/15/06 01/23/07 02/06/07 03/14/07 06/19/07 07/19/07 08/23/07 09/20/07 10/17/07 11/15/07 12/13/07 Well-AS~7 3,90 3,1 Well-AS 355064,15 Well-AS66 5,00 3,5 Well-AS4 2,52 1,85 Well-AS 7,5 4,350 Well-A 6,2744,26 Well-AS1158840 Well-AS7162733 2,820 3,905 3,790 3,430 4,370 3,550 3,920 3,730 5,510 5,000 4,890 5,470 2,520 7,550 6,270 163 151 158 162 165 147 146 141 149 168 124 150 3,530 3,334 3,010 3,910 3,870 4,150 4,190 3,640 3,820 3,850 3,970 3,640 1,850 4,350 4,260 584 394 403 334 383 298 146 218 214 204 220 296 We70204 1 1 3 °2,50 -I 3 Well-AT 07/08/04 4,288 142 139 0.275 309 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.[ Constituent was detected above its New Jersey Groundwater Quality Criteria.~Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 62 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification I Date INote Result (pCi/L)I LLD Deviation I Boron(mg/L)

Sodium(mg/L)

Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT Well-AT 07/12/04 07/22/04 08/03/04 08/11/04 08/12/04 08/13/04 08/21/04 08/31/04 12/28/04 01/19/05 03/02/05 03/07/05 03/14/05 03/23/05 03/28/05 04/18/05 05/18/05 06/22/05 07/19/05 08/15/05 10/17/05 11/15/05 12/12/05 01/24/06 02/22/06 02/23/06 03/21/06 04/17/06 05/15/06 06/20/06 17,124'4,060 1,991 10,039 7,973 4,974 3,451 1,777 1,687 1,578 2,224 1,451 1,722 2,139 2,375-3,920<3,730 1,396 1,517 1,911 3,620 2,870 3,320 3,030 3,030 3,030 3,030 157 4,060 159 3,670 3,490 4,320 150 148 151 151 145 146 150 157 151 153 153 152 3,920 3,730 159 156 151 2,750 2,200 2,580 2,320 2,620 2,220 2,460 250 1,260 124 3,030 2,330 3,660 195 176 153 136 112 112 112 124 112 116 121 123 NA NA 115 115 117 0.286 0.267 163 396 Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.-2-111Constituent was detected above its New Jersey Groundwater Quality Criteria.IN ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 63 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-AT 07/24/06 2,110 151 120 --Well-AT 08/22/06 3,715 152 139 ....Well-AT 09/21/06 4,002 158 145 --Well-AT 10/06/06 4,785 159 154 -- -Well-AT 11/16/06 6,235 170 178 --Well-AT 12/15/06 2,458 166 134 --Well-AT 01/23/07 2,103 146 118 --Well-AT 02/06/07 1,401 149 110 -- -Well-AT 03/14/07 2,359 197 152 ....Well-AT 04/24/07 4,046 160 149 --Well-AT 05/22/07 3,482 151 135 --Well-AT 06/19/07 1,892 143 112 -- -Well-AT 07/19/07 2,158 145 116 --Well-AT 08/22/07 1 -4,280 4,280 NA -- -Well-AT 08/23/07 2,182 148 118 -- -Well-AT 09/20/07 2,114 148 118 ....Well-AT 10/17/07 1,705 149 112 ---Well-AT 11/15/07 2,221 176 136 --Well-AT 12/13/07 4,326 140 137 -- -I Well-AV 07/20/05 3,060 NA NA --Well-AY 07/20/05 3,000 NA NA -- --Well-AZ 07/20/05 8,710 NA NA --Well-BA 10/16/06 '157 157 194I Well-BA 04/10/07 126 126 75 --Well-BA 05/07/07 172 172 105 -- -Well-BA 10/17/07 150 150 89 -- -Well-BB 10/1,6/061 289 162 101 -I -Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.I Constituent was detected above its New Jersey Groundwater Quality Criteria.N9(Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 64 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-BB 12/08/06 338 165 104 --Well-BB 04/10/07 161 161 97 Well-BB 10/17/07 149 149 89 Well-BC 10/16/06 -163 163 98 Well-BC 04/10/07 -162 162 94 Well-BC 10/17/07 150 ISO 89 WeI1-BD 10/16/06 1 325 157 99 Well-BD 04/10/071 256 152 95 Well-BD 10/10/07 264 156 97 Well-BE 10/16/06 '159 159 95 Well-BE 04/10/07 -168 168 98 Well-BE 10/10/07 -158 158 93 WeIl-BF 10/16/06 I 155 155 91 Well-BF 04/11/07 -'164 164 94 Well-BF 10/17/07 ,189 189 109 Wel1-BG 10/17/06 -'162 162 97 Well-BG 04/11/07 '152 152 92 Well-BG 11/01/07 '165 165 94 Well-BU 10/18/07 -153 153 90 Well-BW 02/24/07 2,556 162 132 --Well-BW 03/27/07 3,728 164 149 --Well-BW 04/20/07 3,054 159 138 --Well-BW 05/22/07 1,517 168 122 Well-BW 06/25/07 1 3,730 3,730 NA --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.2 j0joConstituent was detected above its New Jersey Groundwater Quality Criteria.Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 65 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-BW 07/12/07 1,593 146 110 --Well-BW 08/22/07 1,719 149 113 -- -Well-BW 09/21/07 1,917 149 115 ---Well-BW 10/09/07 2,056 150 117 ....Well-BW 11/20/07 1,729 179 132 ....Well-BW 12/19/07 1,641 147 111 ---Well-BX 02/24/07 1,958 155 120 --Well-BX 03/27/07 962 151 105 --Well-BX 04/20/07 883 161 110 --Well-BX 05/22/07 1,265 138 102 --Well-BX 06/25/07 1 -3,730 3,730 NA --Well-BX 07/12/07 1,556 144 108 --Well-BX 08/22/07 1,806 147 113 ....Well-BX 09/21/07 1,430 150 110 --Well-BX 10/09/07 996 151 104 --Well-BX 11/20/07 1,270 173 122 ---WelI-BX 12/19/07 1,378 146 107 -- -Well-CA 02/21/07 695 161 107 --Well-CA 03/15/07 932 165 113 --Well-CA 04/11/07 853 160 109 --Well-CA 05/22/07 665 170 111 --Well-CA 06/19/07 639 138 92 --Well-CA 07/12/07 710 144 96 --Well-CA 08/22/07 670 147 97 --Well-CA 09/20/07 599 150 98 -- -Well-CA 10/09/07 549 153 99 --Well-CA 11/19/07 437 177 112 -- -Well-CA 12/19/07 729 146 98 --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.F_2bjConstituent was detected above its New Jersey Groundwater Quality Criteria.WX Not Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 66 of 67 Table 02. Groundwater Analytical Results, PSEG Nuclear, LLC, Salem Generating Station.for Samples collected between 01/22/2003 and 12/29/2007 Well Sample Tritium Major Cations and Anions Identification Date Note Result (pCi/L) LLD Deviation Boron(mg/L)

Sodium(mg/L)

Well-CB 02/21/07 156 152 93 -- -Well-CB 03/27/07 ,158 158 95 -- -Well-CB 04/11/07 -162 162 97 ---Well-CB 05/22/07 -180 180 106 --Well-CB 06/19/07 -145 145 87 --Well-CB 07/12/07 -147 147 89 --Well-CB 08/22/07 '149 149 90 --Well-CB 09/20/07 '144 144 87 --Well-CB 10/09/07 '150 150 89 -- -Well-CB 11/19/07 '180 180 108 ---Well-CB 12/19/07 1 146 146 89 --Notes: LLD Lower Limit of Detection mg/L Milligrams per liter pCi/L Picocuries per liter 1 Reported analytical results are from Salem Chemistry.

< Constituent was not detected above the indicated laboratory detection limit.762 Constituent was detected above the laboratory method detection limit.Fnop-Constituent was detected above its New Jersey Groundwater Quality Criteria.ot Available

-Deviation and/or LLD were not reported.-Constituent not analyzed.03/05/2008 5:52 PM Page 67 of 67 Table 03. Groundwater Extraction System Operational Data and Tritium Analytical Results, PSEG Nuclear, LLC, Salem Generating Station Sample Number Release End Date Volume Discharged Tritium (pCi/L) Curies Removed Pilot Syatem ____________________0.93*

12/22/2005 137,810 36,200 0.0189 2 3/l/2005 84,566 109,000 0.0349 3 3/8/2005 2,687 66,500 0.0007 4 3/10/2005 459 30,300 0.0001 5 3/17/2005 178,372 53,900 0.0364 6 3/24/2005 173,513 65,800 0.0432 7 3/31/2005 143,437 72,800 0.0395 8 4/7/2005 140,279 58,300 0.03 10 9 4/15/2005 270,445 65,300 0.0669 10 4/20/2005 63,835 63,500 0.0153 11 4/28/2005 99,244 61,900 0.0233 12 4/28/2005 10,178 62,200 0.0024 13 5/5/2005 27,366 60,100 0.0062 14 5/12/2005 32,950 70,300 0.0088 15 5/19/2005 23,013 59,900 0.0052 16 5/26/2005 56,727 64,400 0.0138 17 6/2/2005 40,437 54,400 0.0083 18 6/9/2005 66,012 52,600 0.0131 19 6/16/2005 80,460 60,400 0.0184 20 6/24/2005 38,457 63,800 0.0093 21 6/30/2005 113,247 51,500 0.0221 22 7/7/2005 126,530 49,200 0.0236 23 7/14/2005 101,080 42,500 0.0163 24 7/21/2005 80,699 39,900 0.0122 25 7/28/2005 129,721 65,200 0.0320 26 8/4/2005 130,851 62,000 0.0307 27 8/11/2005 116,177 57,200 0.0252 28 8/18/2005 128,290 49,200 0.0239 29 8/25/2005 127,158 51,400 0.0247 30 9/22/2005 6,999 14,400 0.0004 31 11/3/2005 111,699 33,600 0.0142 32 11/10/2005 355,417 27,900 0.0375 33 11/24/2005 310,171 30,600 0.0359 34 12/8/2005 246,336 28,800 0.0269 35 12/15/2005 244,370 31,700 0.0293 36 12/22/2005 268,454 30,300 0.0308 37 12/29/2005 249,559 1 26,700 0.0252 38 1/5/200 99,502 1 19,100 0.0072 Notes: Pilot-Study Cycle 1 was initiated on April 26, 2004.Full scale system became operational February 16, 2005* Total curies removed from the Pilot System Total curies removed to date from the Full Scale System 1 of 3 Table 03. Groundwater Extraction System Operational Data and Tritium Analytical Results, PSEG Nucleari LLC, Salem Generating Station Sample Number Release End Date Volume Discharged Tritium (pCi/L) Curies Removed 39 1/12/2006 310,508 27,900 0.0328 40 2/2/2006 331,650 25,700 0.0323 41 2/9/2006 326,436 24,800 0.0306 42 2/23/2006 320,934 26,600 0.0323 43 3/2/2006 333,662 19,400 0.0245 44 3/9/2006 327,270 30,900 0.0383 45 3/16/2006 329,963 25,100 0.0314 46 3/23/2006 257,370 25,200 0.0246 47 3/30/2006 156,671 55,300 0.0328 48 4/6/2006 155,685 24,300 0.0143 49 4/13/2006 157,437 23,300 0.0139 50 4/20/2006 156,806 39,500 0.0234 51 4/27/2006 161,303 30,000 0.0234 52 5/4/2006 164,369 24,000 0.0149 53 5/11/2006 163,588 15,500 0.0096 54 5/18/2006 165,460 18,800 0.0118 55 5/25/2006 157,258 18,500 0.0110 56 6/1/2006 153,950 22,100 0.0129 57 6/8/2006 164,783 20,100 0.0125 58 6/15/2006 161,788 17,900 0.0110 59 6/22/2006 148,220 18,600 0.0104 60 6/29/2006 144,590 12,600 0.0069 61 7/6/2006 137,690 11,000 0.0057 62 7/13/2006 153,710 15,500 0.0090 63 7/20/2006 160,790 17,100 0.0104 64 7/27/2006 156,469 13,500 0.0080 65 8/3/2006 145,658 13,700 0.0076 66 8/10/2006 119,811 11,300 0.0051 67 8/17/2006 115,665 11,700 0.0051 68 8/24/2006 123,100 13,100 0.0061 69 8/31/2006 126,095 10,100 0.0048 70 9/7/2006 135,939 10,800 0.0056 71 9/14/2006 84,446 18,200 0.0058 72 9/21/2006 120,372 15,600 0.0071 73 9/28/2006 59,089 12,200 0.0027 74 10/5/2006 149,094 13,800 0.0078 75 10/12/2006 141,618 17,400 0.0093 76 10/19/2006 116,290 14,900 0.0066 77 10/26/2006 9,188 21,600 0.0008 78 11/2/2006 127,740 99,100 0.0479 79 11/9/2006 131,760 17,700 0.0088 80 11/16/2006 132,090 12,000 0.0060 81 11/23/2006 132,280 12,000 0.0060 82 11/30/2006 127,190 75,000 0.0361 83 12/7/2006 134,120 16,700 0.0085 84 12/14/2006 135,910 15,000 0.0077 85 12/21/2006 84,817 13,100 0.0042 86 12/28/2006 119,220 13,800 0.0062 Notes: Pilot-Study Cycle 1 was initiated on April 26, 2004.Full scale system became operational February 16, 2005* Total curies removed from the Pilot System** Total curies removed to date from the Full Scale System 2 of 3 Table 03. Groundwater Extraction System Operational Data and Tritium Analytical Results, PSEG Nuclear, LLC, Salem Generating Station Sam ple Number Release End Date Volume Discharged Tritium (pCi/L) Cories Removed 87 1/5/2007 55,000 10,100 0.0021 88 1/12/2007 89,078 17,900 0.0060 89 1/19/2007 77,670 13,100 0.0039 90 1/25/2007 121,070 14,900 0.0068 91 2/1/2007 146,400 27,600 0.0153 92 2/8/2007 141,504 21,000 0.0112 93 2/15/2007 138,900 15,300 0.0080 94 2/22/2007 136,630 45,300 0.0234 95 .3/1/2007 96,791 9,610 0.0035 96 .3/8/2007 94,849 7,060 0.0025 97 3/15/2007 94,000 8,110 0.0029 98 3/22/2007 101,124 5,710 0.0022 99 3/29/2007 112,065 .11,700 0.0050 100 4/5/2007 118,053 13,500 .0.0060 101 4/12/2007 116,658 8,860 0.0039 102 4/19/2007 100,138 9,460 0.0036 103 4/26/2007 350,699 11,100 0.0147 104 5/3/2007 84,705 9,010 0.0029 105 5/10/2007 72,867 14,400 0.0040 106 5/17/2007 72,488 12,500 0.0034 107 5/24/2007 71,531 11,600 0.0031 108 5/31/2007 71,152 14,900 0.0040 109 6/7/2007 81,726 11,700 0.0036 110 6/14/2007 115,446 26,400 0.0115 111 6/21/2007 109,665 22,800 0.0095 112 6/28/2007 67,435 69,100 0.0176 113 7/5/2007 70,000 10,700 0.0028 114 7/12/2007 68,461 11,600 0.0030 115 7/19/2007 69,845 12,900 0.0034 116 7/26/2007 70,300 66,100 0.0176 117 8/2/2007 74,555 29,400 0.0083 118 8/9/2007 79,888 93,100 0.0282 119 8/16/2007 132,588 18,500 0.0093 120 8/23/2007 150,343 18,000 0.0102 121 8/30/2007 152,945 16,700 0.0097 122 9/6/2007 122,833 17,000 0.0079 123 9/13/2007 68,290 43,500 0.0112 124 9/20/2007 155,780 14,400 0.0085 125 10/4/2007 14,580 12,600 0.0007 126 10/11/2007 151,815 11,100 0.0064 127 10/18/2007 151,693 12,500 0.0072 128 10/25/2007 151,400 11,700 0.0067 129 11/1/2007 152,219 13,200 0.0076 130 11/8/2007 140,180 28,400 0.0151 131 11/15/2007 105,120 7,060 0.0028 132 11/22/2007 93,700 1,990 0.0007 133 11/29/2007 99,787 9,310 0.0035 134 1 12/6/2007 92,245 7,210 0.0025 135 12/13/2007 91,607 11,300 0.0039 136 12/20/2007

.82,150 27,200 0.0085 138 12/31/2007 244,440 43,100 0.0399 Notes: Pilot-Study Cycle I was initiated on April 26, 2004.Full scale system became operational February 16, 2005* Total curies removed from tbe Pilot System** Total curies removed to date from tbe Full Scale System 3 of 3 1 .11 T61. 04. Gtoodtol Elo.oooo f0, 2007 d0 O=.ooq 28. 2008, PSEI3 S.I.t ftooo.g Slolio.8 1 0 1 I 7 t t S 8 5 S-tttd ItoA. 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NM 7.02 NM NM NM NM NM NM 00.36 0.44 Wel1 BP 99.06 9. 14 8.S4 8.34 8.6 69.92 0.00 90.52 0.60 90.72 0.80 90.46 0.54 WdiBQ 102.16 12.24 NM NM NM NM NM NM NM NM NM NM WAl B 104.28 14.36 12.64 12.76 12.8 91.33 1.41 91. 1.72 91.52 1.60 91.48 1.56 We.l BS 100.35 10.63 7.77 7. 7.4 NM NM 9238 2.84 9237 2m5 92.71 2.79 WA BT 09.60 9.68 6.99 7 0.84 92.13 2.21 93.01 3.09 92.60 2.68 92.76 2.84 WA) BU 100.16 10.24 7.32 7.65 7.89 91:70 1.78 92.84 2.92 9231 2.59 92.31 2.39 WAl CA 98.87 8.95 5.96 6,21 0.6 91.41 1.49 92.91 2.99 92.66 2.74 92.27 2.35 WAl K 102.00 12.08 11, 3 11.71 16.92 9.33 0.41 90.87 0.95 94.29 0.37 91.08 1.16 WAlL 16O.46 11.54 61.23 11.62 9.93 90.46 0.54 90.23 031 89.84 -6.08 91.53 1.61 W)P 101.13 11.21 9.85 10.27 9.99 81.30 4.38 91.28 130 90.8m 0.94 91.58 1.66 Wo Q 100.59 10.67 NM NM NM NM NM NM NM NM NM NM WAI1V 98.74 8.82 7.67 7.97 7.48 93.51 3.99 91.07 1.15 91.17 1.25 91.26 1.94 Well CB 98.98 9.06 7.9 9.97 7.73 90.0M 0.14 91.08 1.16 89.4) -0.5) 91.25 1.33 250.39 70 1. 00 N.-o NM ot bgs fItms It11 Mot1loi(.1g o00otlol0 t oo010001lll8018001 WOW 100 oo.o- oo 0 olood Foomtlolo Oooobd wdftO.01,0.00 (It foo) 1-l~v d...,O4000 F- 0A~0 ot.. 8o boo 1 (AVft 1908).M-~ ido 1-o) .1 A180001 14.1-d .0.11 1-O (40506 1988).

Table 05. Unit I Seismic Gap Drain Tritium Analytical Results, PSEG Nuclear, LLC, Salem Generating Station Date of Operation Tritium Results (pCi/L)October 5, 2004 2,590,000 October 13, 2004 74,600,000 October 21, 2004 75,600,000 October 27, 2004 1,920,000 November 3, 2004 66,300,000 November 8, 2004 103,000,000 November 15, 2004 61,900,000 November 23, 2004 46,800,000 December 1, 2004 40,400,000 December 8, 2004 63,400,000 December 14, 2004 44,800,000 December 21, 2004 89,900,000 January 4, 2005 13,600,000 January 11, 2005 40,900,000 January 19, 2005 17,700,000 January 24, 2005 57,900,000 February 2, 2005 46,700,000 February 9, 2005 53,800,000 February 25, 2005 26,800,000 February 28, 2005 59,400,000 March 9, 2005 31,800,000 March 18, 2005 44,200,000 April 1, 2005 39,300,000 April 13, 2005 34,600,000 April 21, 2005 29,900,000 May 11, 2005 25,600,000 May 19, 2005. 33,400,000 May 25, 2005 37,400,000 June 9, 2005 35,800,000 July 8, 2005 31,800,000 July 15, 2005 47,900,000 September 4, 2005 32,600,000 September 28, 2005 50,300,000 November 27, 2005 29,700,000 December 26, 2005 27,800,000 February 19, 2006 28,000,000 March 13, 2006 28,000,000 March 20, 2006 28,000,000 March 27, 2006 28,000,000 April 10, 2006 58,400,000 April 17, 2006 70,300,000 April 23,2006 70,300,000 May 1, 2006 74,600,000 May 7, 2006 88,000,000 May 14, 2006 85,800,000 May 20, 2006 83,800,000 May 27, 2006 6,970,000 May 29, 2006 ND June 5, 2006 ND June 12, 2006 73,100,000 June 18, 2006 58,400,000 June 25, 2006 72,400,000 June 29, 2006 63,200,000 July 2, 2006 30,000,000 July 15, 2006 30,000,000 July 22, 2006 63,200,000 July 29, 2006 36,300,000 August 5, 2006 45,800,000 August 12, 2006 68,600,000 August 20, 2006 68,600,000 September 17, 2006 123,000,000 September 30, 2006 118,000,000 October 7, 2006 128,000,000 October 14, 2006 133,000,000 October 21, 2006 116,000,000 October 28, 2006 84,000,000 November 4, 2006 113,000,000 November 11, 2006 100,000,000 Notes: ' concentration estimated based upon results of prior events ND = Data not availible Volume data after September 2005 estimated due to change in draining proceedurew 1 of 2 Table 05. Unit I Seismic Gap Drain Tritium Analytical Results, PSEG Nuclear, LLC, Salem Generating Station Date of Operation Tritium Results (pCi/L)November 19, 2006 97,200,000 November 25, 2006 116,000,000 December 2, 2006 122,000,000 December 9, 2006 110,000,000 December 17, 2006 100,000,000 December 23, 2006 115,000,000 December 31, 2006 134,000,000 January 8, 2007 131,000,000 January 14, 2007 105,000,000 January 21, 2007 102,000,000 January 27, 2007 77,900,000 February 3, 2007 71,800,000 February 11, 2007 67,700,000 February 17, 2007 67,400,000 February 24, 2007 66,400,000 March 3, 2007 76,000,000 March 7, 2007 40,800,000 March 25, 2007 75,800,000 April 15, 2007 69,900,000 April 20, 2007 1,770,000 May 1, 2007 58,600,000 May 6, 2007 79,100,000 May 11, 2007 80,900,000 May 13, 2007 77,100,000 May 15, 2007 82,300,000 May 16, 2007 82,600,000 May 18, 2007 82,900,000 June 1, 2007 65,700,000 June 10, 2007 66,600,000 June 17, 2007 63,200,000 June 21, 2007 70,200,000 June 24, 2007 73,900,000 June 26, 2007 81,400,000 July 6, 2007 39,000,000 July 8, 2007 1,970,000 July 11, 2007 66,200,000 July 19, 2007 60,400,000 July 24, 2007 57,300,000 July 29, 2007 12,800,000 August 5, 2007 61,500,000 August 12, 2007 66,600,000 August 15, 2007 71,400,000 August 21, 2007 76,400,000 August 26, 2007 66,300,000 September 6, 2007 88,200,000 September 9, 2007 87,000,000 September 16, 2007 89,000,000 September 26, 2007 100,000,000 October 7, 2007 94,600,000 October 14, 2007 98,200,000 October 21, 2007 190,000,000 October 24, 2007 107,000,000 November 1, 2007 100,000,000 November 4, 2007 97,400,000 November 11, 2007 102,000,000 November 19, 2007 4,800,000 November 30, 2007 99,000,000 December 9, 2007 124,000,000 December 16, 2007 107,000,000 December 23, 2007 40,500,000 January 6, 2008 107,000,000 January 13, 2008 70,900,000 Notes: ' concentration estimnated based upon results of prior events ND = Data not availible Volume data after September 2005 estimsated due to change in draining proceedures 2 of 2 THIS PAGE IS AN OVERSIZED DRAWING OR FIGURE, THAT CAN BE VIEWED AT THE RECORD TITLED: "FIGURE NO. 1 GROUNDWATER TRITIUM RESULTS"1 WITHIN THIS PACKAGE...

D-01 THIS PAGE IS AN OVERSIZED DRAWING OR FIGURE, THAT CAN BE VIEWED AT THE RECORD TITLED: "FIGURE NO. 2, WATER TABLE ELEVATION CONTOURS DURING OPERATION OF THE PERMANENT SYSTEM AUGUST 2007"9 WITHIN THIS PACKAGE.., D-02 FIGURE, THAT CAN BE VIEWED AT THE RECORD TITLED: "FIGURE NO. 3, WATER TABLE ELEVATION CONTOURS DURING OPERATION OF THE PERMANENT SYSTEM JANUARY 2008" WITHIN THIS PACKAGE...

D-03X

'lw PSEG Nuclear, LLC Salem Generating Station -Unit 1 Tritium Recovered Through Well Field Operation w 3.000 2.500 0 E ,-I-2.000 1.500 1.000 900,000 800,000 700,000 600,000 0 0 500,000 *0 300,000 200,000 N 100,000 0 0.500 0.000 DateMwwPSEG NUCLEAR, LLC fo "b R.GAN SALEM GENERATING STATION NP000571.0007

.TPMILIONIS errie HISTORIC TRITIUM RECOVERED THROUGH 13 ______c.6 TeqNve WELL FIELD OPERATION I TCS*HARwPE Suite 300 FEDCDDTtN e Newtown, Pa 18940 Tel: 267/685-1800 Fax: 267/685-1801 C. SHAFPE www.arcadis-us.com HANCOCK'S BRIDGE, NEW JERSEY w 1w PSEG Nuclear, LLC Salem Generating Station -Unit I Concentrations of Tritium in Water Recovered Through Seismic Gap Drain Operation w 0 E E k.6 200,000,000 180,000,000 160,000,000 140,000,000 120,000,000 100,000,000 80,000,000 60,000,000 40,000,000 20,000,000 0 Date AMM- PSEG NUCLEAR, LLC ,M-n A P. GMILOI K A SALEM GENERATING STATION NP000571 .0007 P.iO Nyuoe HISTORIC TRITIUMCONCENTRATIONS OBSERVED 13____,_M S Tas Mww 6 Terry Drve Fon c. ESufte 300 DURING SEISMIC GAP DRAIN OPERATION j o Newtown, Pa 1894& 5 TJ *Tel: 267/685-1800 Fax 267/685-1801 c.SHAPPE www.amadis-us.com HANCOCK'S BRIDGE, NEW JERSEY