05000271/FIN-2010008-01
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Finding | |
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Title | Fire Scenario Resulting in Loss of Reactor Core Isolation Cooling System |
Description | The team identified a Green, Non-Cited Violation of the Vermont Yankee Nuclear Power Station Facility Operating License, Condition 3.F, in that Entergy failed to implement and maintain in effect all provisions of the approved Fire Protection Program as described in the Final Safety Analysis Report. Specifically, Entergy failed to assure that reactor vessel water level would remain below the reactor core isolation cooling (RCIC) system steam line for postulated alternate shutdown fire scenarios that spuriously started a reactor feedwater pump (RFP). Entergy initiated condition report CR-VTY-2010-04682 and promptly revised the alternate shutdown procedure to additionally trip all running condensate pumps. The additional action prevented a single spurious operation from restarting or precluding a trip of the RFPs. This finding was more than minor because it was associated with the External Factors attribute (fire) of the Mitigating Systems Cornerstone and adversely affects the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the availability of the RCIC system was not ensured for postulated fires in alternate shutdown areas. The team used Phase 1 of IMC 0609, Appendix F, Fire Protection Significance Determination Process, to determine that this finding was of very low safety significance (Green) because the Vermont Yankee Nuclear Power Station alternate shutdown system also includes safety relief valves and a residual heat removal train that can be utilized for reactor pressure and water level control. This finding did not have a cross-cutting aspect because the m9st significant contributor of the performance deficiency was not reflective of current licensee performance. |
Site: | Vermont Yankee File:NorthStar Vermont Yankee icon.png |
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Report | IR 05000271/2010008 Section 1R05 |
Date counted | Dec 31, 2010 (2010Q4) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.05 |
Inspectors (proximate) | J Lilliendahl M Patel W Cook D Orr J Rogge |
INPO aspect | |
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Finding - Vermont Yankee - IR 05000271/2010008 | |||||||||||||||||||||||||||||||||||||||||||
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Finding List (Vermont Yankee) @ 2010Q4
Self-Identified List (Vermont Yankee)
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