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Issue date | Title | Topic | |
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ML19354C437 | 18 July 1974 | AO 50-219/74/36:on 740710,RE03D Reactor High Pressure Sensor Failed to Trip at Point Less than or Equal to 1,060 Psig. Caused by Lack of Allowance for Setpoint Tolerances in Tech Specs.Sensor Recalibr & Returned to Svc | |
ML20003C379 | 26 April 1974 | AO 50-219/74/29:on 740423,electromatic Relief Valve Pressure Switches 1A83B & 1A83D Tripped at Pressures in Excess of Max Allowable Value of 1,070 Psig.Caused by Instrument Drift. Switches Reset | |
ML20003C380 | 26 April 1974 | AO 50-219/74-27:on 740417,insp Revealed Bergen-Paterson Hydraulic Shock & Sway Arrestors in Drywell Inoperable.Cause Undetermined.Units Will Be Replaced During Present Refueling Outage | |
ML20003C381 | 22 April 1974 | AO 50-219/74/26:on 740412,emergency Svc Water Pump 52C Failed to Start.Caused by Thermal Overload Relay Coupled W/ Excess Current Relay.Feasibility Study Re Thermal Overload Relay Removal from Trip Circuits to Be Made | |
ML20003C382 | 19 April 1974 | AO 50-219/74/24:on 740409,stack Gas Particulate Filter in Svc from 740328-31 Not Analyzed for Gross Beta,Gross Alpha & Gross Gamma as Required.Caused by Technician Error. Administrative Control to Be Tightened | |
ML20003C383 | 19 April 1974 | AO 50-219/74/28:on 740419,suction Valve V-20-4 to Core Spray Pump B Stuck in Closed Position for 15 Minutes,Causing Loss of Core Spray Redundancy in Sys 2.Cause Undetermined.Valve Manually Opened & Circuit Breaker Tagged Open | |
ML20003C384 | 19 April 1974 | AO 50-219/74/25:on 740409,butterfly Valve V-26-16 Found Open & Primary Containment Integrity Lost W/Reactor Critical & Water Temp Greater than 212F.Caused by Component Failure. Valve Manually Forced to Seat Properly & Shutdown Commenced | |
ML20003C385 | 18 April 1974 | AO 50-219/74/27:on 740417,insp Revealed Bergen-Paterson Hydraulic Shock & Sway Arrestors in Drywell Inoperable.Cause Undetermined.Units Will Be Replaced During Present Refueling Outage | |
ML20003C387 | 10 April 1974 | AO 50-219/74/25:on 740409,butterfly Valve V-26-16 Found Open & Primary Containment Integrity Lost W/Reactor Critical & Water Temp Greater than 212F.Cause of Component Failure Not Known.Valve Manually Forced to Seat Properly | |
ML20003C388 | 10 April 1974 | AO 50-219/74-24:on 740409,stack Gas Particulate Filter in Svc from 740328-31 Not Analyzed for Gross Beta,Gross Alpha & Gross Gamma as Required.Cause Being Investigated | |
ML20003C389 | 25 March 1974 | AO 50-219/74/23:on 740315,isolation Condenser Condensate High Flow Sensors Actuated at Setpoints Above Tech Specs Limits.Caused by Lack of Sensor Repeatability.Procedures Being Revised to Reflect Setpoint Changes | |
ML20003C390 | 22 March 1974 | AO 50-219/74/21:on 740313,bypass Valve RE22D Opened,Causing Main Steam High Flow Sensor RE22D to Be Inoperable.Caused by Incorrect Valve Positioning.Instrument Technicians to Be Advised Re Critical Importance of Valve Lineup Checks | |
ML20003C391 | 22 March 1974 | AO 50-219/74/22:on 740315,low Pressure Main Steam Line Pressure Switch RE23D Tripped at Pressure Less than Min Required Value of 860 Psig.Caused by Switch Repeatability & Design.Basis for Steam Line Low Pressure Setting Studied | Fuel cladding |
ML20003C392 | 18 March 1974 | AO 50-219/74/20:on 740310,MSIVs NS04A & NS04B Failed to Meet Allowable Leakage Requirements.Caused by Faulty Lower Packing Rings Around Valve Shaft.Valves Closed Until 1974 Refueling Outage | |
ML20003C393 | 13 March 1974 | AO-50-219/74/21:on 740313,bypass Valve RE22D Opened,Causing Main Steam High Flow Sensor RE22D to Be Inoperable.Cause Under Investigation.Instrument Technicians to Be Advised Re Critical Importance of Valve Lineup Checks | |
ML20003C394 | 8 March 1974 | AO 50-219/74/17:on 740307,power Operation Continued W/Sb Startup Transformer Unavailable for Svc for Time Period Greater than Tech Specs Limits.Caused by Failure of Cam Switch Contacts.Corrective Action to Be Determined | |
ML20003C395 | 7 March 1974 | AO 50-219/74/15:on 740228,torus to Drywell Breaker Failed to Demonstrate Operability During Weekly Testing.Caused by Design Error Resulting in Excess Friction in Valve Hinge Pins.Valve Locked in Closed Position Pending Solution | |
ML20003C397 | 1 March 1974 | AO 50-219/74/14:on 740222,two Torus to Drywell Breakers Failed to Demonstrate Operability During Weekly Surveillance Testing.Caused by Excess Friction in Valve Hinge Pins.Valves Freed Immediately W/Repetitive Opening & Closing Movements | |
ML20003C399 | 27 February 1974 | AO 50-219/74/13:on 740218,cleanup Sys Ac Isolation Valve V-16-1 Inoperable W/Reactor Critical & Coolant Temp Above 212F.Caused by Inadvertent Opening of Valve V-16-1 Breaker. Breaker re-energized & Painting Contractor Personnel Warned | |
ML20003C400 | 25 February 1974 | AO 50-219/74/12:on 740215,low Pressure Main Steam Line Pressure Switches RE23A & B Tripped at Pressures Less than Min Required Value of 860 Psig.Caused by Design Error. Investigation in Progress & Tech Specs Change May Follow | Fuel cladding |
ML20003C401 | 25 February 1974 | AO 50-219/74/11:on 740215,four Torus to Drywell Vacuum Breakers Failed to Demonstrate Operability During Weekly Surveillance Testing.Caused by Excess Friction in Valve Hinge Pines.Valves Freed W/Opening & Closing Movements | |
ML20003C402 | 14 February 1974 | AO 50-219/74/10:on 740208,low Pressure Main Steam Line Pressure Switches RE23A,C & D Tripped at Pressure Less than Min Required Value of 860 Psig.Caused by Design Error & Sensor Drift.Investigation of Setpoint Drift in Progress | Fuel cladding |
ML20003C403 | 6 February 1974 | AO 50-219/74/9:on 740131,low Pressure Main Steam Line Pressure Switches RE23A & D Tripped at Pressures Less than Specified Value.Caused by Design Error & Unusual Svc Conditions.Study Re Basis for Specified Setting in Progress | Fuel cladding |
ML20003C721 | 18 March 1974 | Ao:On 740309,during Shutdown to Perform Maint on Six Torus to Drywell Vacuum Breaker Valves,Recirculation Loop Temp Recorder Indicated 160 F,Then Jumped to 250 F When Bumped. Caused by Equipment Malfunction & Operator Error | |
ML20003C722 | 18 March 1974 | AO 50-219/74/18:on 740308,w/plant Shutdown,Insp of Drywell Snubbers Located Three Inoperable & Four Leaking.Caused by Loss of Hydraulic Fluid.Units Replaced W/Identical Snubbers Rebuilt W/Ethylene Propylene Seals | Design basis earthquake |
ML20003C723 | 15 March 1974 | AO 50-219/74/17:on 740307,during Routine Plant Shutdown, While Transferring Power from 1B Auxiliary Transformer to SB Startup Transformer,Closing Switch for S1B Breaker Failed. Caused by Component Failure.Switchgears Will Be Checked | |
ML20003C724 | 15 March 1974 | AO 50-219/74/16:on 740307,while at Steady State Power,During Weekly Surveillance Testing on 14 Torus to Drywell Vacuum Breakers,Four Breakers Failed to Demonstrate Operability. Caused by Excess Friction in Valve Hinge Pins | |
ML20083Q021 | 27 February 1973 | Ao:On 730212,low Sample Flow Identified in Stack Monitor Sys.Caused by Moisture Freezing in Sample Line at 262-ft Elevation.Line Thawed Out | |
ML20083Q039 | 17 January 1973 | Ao:On 721229,electromatic Relief Valve Failed to Reset Causing Primary Sys Blowdown Following Reactor Scram.As Result,Three Different Valves Failed to Operate in Intended Manner.Manufacturers & Valve Users Will Be Consulted | Breakaway torque |
ML20083R190 | 24 May 1972 | Ao:On 711031,fuel Assembly Jc 359 Found Misoriented,As Result of Investigation of 720506 Incident Where Operator Unable to Position Sipper Head on Control Head 26-07.Visual Insp of Assembly Conducted | |
ML20084A090 | 29 October 1973 | Ao:On 730915,following Investigation of Excess Letdown Line Leak,Valve 1MOV-1299 Downstream Seat Protruded from Valve Body & Crack Discovered in Upper Portion of Downstream Seat Ring.Cause Unknown.Vendor Notified of Valve Problem | |
ML20084B712 | 26 June 1972 | Ao:On 720524,essential Svc Motor Generator Set Failed Resulting in Feedwater Control Sys Failure & Reactor Scram. Caused by Dirty Contacts on 2K Relay.Hfa Relay Replaced | |
ML20084C394 | 21 October 1974 | AO 50-219/74-52:on 741012,main Steam Line Low Pressure Switch RE23A Found to Trip at Pressure Less than Min of 860 Psig.Caused by Switch Repeatability.Ge Supplied Info to Reduce Setpoint | |
ML20084C419 | 15 October 1974 | Preliminary AO 50-219/74/52:on 741012,main Steam Low Pressure Switch RE23A Found to Trip at Pressure Less than Min of 860 Psig.Caused by Switch Repeatability.Ge Supplied Info to Enable Reduction in Setpoint | |
ML20084C435 | 24 October 1974 | AO 50-219/74-53:on 741015,stack Gas Sample Sys Discovered Not Functioning Properly While Reactor Not in Isolated Condition.Caused by Excessive Air Flow to Pump Thereby Reducing Vacuum of Filter.Loose Fitting Tightened | |
ML20084C478 | 15 October 1974 | Preliminary AO 50-219/74-53:on 741014,stack Gas Sample Sys Discovered Not Functioning Properly While Reactor Not in Isolated Condition.Caused by Excessive Air Flow to Pump Reducing Vacuum at Filter.Loose Fitting Replaced | |
ML20084C505 | 11 October 1974 | AO 50-219/74-51:on 741007,main Steam Line Low Pressure Switches RE23B & C Found to Trip at Pressure Less than Min of 860 Psig.Caused by Switch Repeatability.Ge Supplied Info Re Reduction of Setpoint.Info Being Evaluated | Fuel cladding |
ML20084C526 | 11 October 1974 | AO 50-219/74-50:on 741004,cleanup Sys Dc Isolation Valve V-16-14 Failed to Close Electrically.Caused Undetermined. Arc Horn on Contactor 2Bc Replaced | |
ML20084C545 | 4 October 1974 | AO 50-219/74-49:on 740927,main Steam Line Low Pressure Switch RE23A Found to Trip at Pressure Less than Min of 860 Psig.Caused by Switch Repeatability.Ge Supplied Info to Reduce Setpoint | Fuel cladding |
ML20084C557 | 4 October 1974 | AO 50-219/74-48:on 740925,isolation Condensers a & B Inoperable Due to High Flow as Sensed by Condensate Line Break Sensors.Caused by Tripping of Line Break Sensors Due to Effects of Rated Recirculation Flow | |
ML20084C580 | 30 September 1974 | Preliminary AO 50-219/74-48:on 740927,main Steam Line Low Pressure Switch RE23A Found to Trip at Pressure Less than Min of 860 Psig.Caused by Switch Repeatability.Ge Submitted Info to Reduce Setpoint | Fuel cladding |
ML20084C638 | 26 September 1974 | Preliminary AO 50-219/74-48:on 740925,isolation Condensers a & B Isolated Due to False High Flow Indication on Condensate Line Break Sensors.Cause Under Investigaion.Surveillance Testing Performed on All Condensate Line Break Sensors | |
ML20084C651 | 23 September 1974 | AO 50-219/74-47:on 740912,two Bergen-Paterson Hydraulic Shock & Sway Arrestors on South Core Spray Sys Found Inoperable.Caused by Component Failure.Two Snubbers Replaced W/Units Rebuilt W/Ethylene Propylene Seals | High Radiation Area Earthquake |
ML20084C712 | 16 September 1974 | Preliminary AO 50-219/74/47:on 740912,two Bergen-Paterson Hydraulic Shock & Sway Arrestor on South Core Spray Sys Found Inoperable.Caused by Component Failure.Two Snubbers Replaced W/Units Rebuilt W/Ep Seals | Design basis earthquake |
ML20084C734 | 3 September 1974 | AO 50-219/74-46:on 740826,one Torus to Drywell Vacuum Breaker Failed to Demonstrate Operability.Caused by Excessive Friction in Valve Hinge Pins.Burring Difficulty Discussed W/Atwood & Morrill Co,Valve Manufacturer | |
ML20084C751 | 27 August 1974 | Preliminary AO 50-219/74/46:on 740826,one Torus Drywell Vacuum Breaker Failed to Demonstrate Operability.Caused by Excessive Friction in Valve Hinge Pins.Bushing Difficulty Discussed W/Atwood & Morrill Co,Valve Manufacturer | |
ML20084C786 | 26 August 1974 | Preliminary AO 50-219/74/45:on 740824,commitment to Follow MAPLHGR Limits Violated.Caused by Insufficient Guidance. Reactor Power Reduced by Recirculation Flow to Point Where No MAPLHGR Limits Violated | |
ML20084C803 | 19 August 1974 | AO 50-219/74-44:on 740809,main Steam Line Low Pressure Switches RE22A,B,C & D Found to Trip at Pressures Less than Min of 860 Psig.Caused by Switch Repeatability | Fuel cladding |
ML20084C848 | 9 August 1974 | Preliminary AO 50-219/74/44:on 740809,main Steam Line Low Pressure Switches RE23A,B,C & D Found to Trip at Pressure Less than Min of 860 Psig.Caused by Switch Repeatability. Setpoint Accuracy Being Investigated | Fuel cladding |
ML20084C913 | 2 August 1974 | Preliminary AO 50-219/74/43:on 740802,main Steam Line Low Pressure Switch RE23B Found to Trip at Pressure Less than Min of 860 Psig.Caused by Switch Repeatability.Set Point Accuracy & Tolerance Being Investigated by GE | Fuel cladding |