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05000272/LER-1976-002, Supplemental LER 76-002/01T:on 760822,Conde Milking Machine Co Model MX-16A (Containment Air Sample Pump for Air Particulate & Gaseous Radiation Monitors R11A,R12A & R12B) Failed.Caused by Bearing or Shaft Seal Seizure7 October 1976Supplemental LER 76-002/01T:on 760822,Conde Milking Machine Co Model MX-16A (Containment Air Sample Pump for Air Particulate & Gaseous Radiation Monitors R11A,R12A & R12B) Failed.Caused by Bearing or Shaft Seal Seizure
05000272/LER-1976-004, Supplemental LER 76-004/03L:on 760902,during Transfer of 1A Vital Instrument Bus to Alternate Power source,1RH2 Closed,Resulting in Loss of RHR Flow to Rcs.Caused by tagged-open Supply Breakers28 January 1977Supplemental LER 76-004/03L:on 760902,during Transfer of 1A Vital Instrument Bus to Alternate Power source,1RH2 Closed,Resulting in Loss of RHR Flow to Rcs.Caused by tagged-open Supply Breakers
05000272/LER-1976-022, Updated LER 76-022/03L:on 761211,steam Generator 13 Level Transmitter LT-538 Failed.Cause Undetermined.Vendor Failed to Analyze Transmitter Before Repairs Made4 April 1978Updated LER 76-022/03L:on 761211,steam Generator 13 Level Transmitter LT-538 Failed.Cause Undetermined.Vendor Failed to Analyze Transmitter Before Repairs Made
05000272/LER-1976-030, Updated LER 76-030/03L:on 761228,during Sample Analysis of Boric Acid Storage Tanks 11 & 12,boron Concentration Noted Low.Cause Unknown.Chemical Analysis After Batching Confirmed Findings4 April 1978Updated LER 76-030/03L:on 761228,during Sample Analysis of Boric Acid Storage Tanks 11 & 12,boron Concentration Noted Low.Cause Unknown.Chemical Analysis After Batching Confirmed FindingsBoric Acid
Shutdown Margin
05000272/LER-1979-068, Supplemental LER 79-068/03X-1:on 791018,safety Injection Pump Motor 12 Tripped on Overcurrent.Caused by Impeller Locknuts Improperly Secured at Mfg Facility.Pumps Reassembled Using Locktite Compound24 February 1984Supplemental LER 79-068/03X-1:on 791018,safety Injection Pump Motor 12 Tripped on Overcurrent.Caused by Impeller Locknuts Improperly Secured at Mfg Facility.Pumps Reassembled Using Locktite CompoundLocktite
05000272/LER-1981-059, Supplemental LER 81-059/01X-01:on 810616,during Initial Testing,Auxiliary Feedwater Pump 23 Turbine Steam Supply Check Valves 21MS46 & 23MS46 Found Damaged Internally.Caused by Steam Flow Sys Oscillations24 February 1984Supplemental LER 81-059/01X-01:on 810616,during Initial Testing,Auxiliary Feedwater Pump 23 Turbine Steam Supply Check Valves 21MS46 & 23MS46 Found Damaged Internally.Caused by Steam Flow Sys Oscillations
05000272/LER-1981-0922 November 1981LER 81-092/01T-0:on 811020,during Routine Containment Insp, Operator Discovered Svc Water Leaking from Third from Top Secondary Coil on Containment Fan Coil Unit 15.Caused by Secondary Coil Failure.Leaking Coil Blank Flanged Off
05000272/LER-1981-121, Supplemental LER 81-121/03X-1:on 811228,svc Water Leak in Spool Piece Discovered Between Valves 12SW57 & 58.Design Change Package 1EC-0504 Implemented to Replace Piece W/Stainless Steel for Improved Corrosion Resistance30 March 1983Supplemental LER 81-121/03X-1:on 811228,svc Water Leak in Spool Piece Discovered Between Valves 12SW57 & 58.Design Change Package 1EC-0504 Implemented to Replace Piece W/Stainless Steel for Improved Corrosion Resistance
05000272/LER-1982-002, Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing29 December 1982Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing
05000272/LER-1982-00326 May 1982LER 82-03L/031-0:on 820502,while Testing Valve 11SW122, Safeguards Equipment Control Cabinet Actuation Occurred. Caused by Locked Out Supply Breaker to Safety Injection Pump 11,due to Spurious Nature of Actuation
05000272/LER-1982-004, Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration20 October 1982Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration
05000272/LER-1982-008, Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added29 December 1982Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid AddedBoric Acid
05000272/LER-1982-009, Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage20 October 1982Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint OutageContinuous fire watch
05000272/LER-1982-01431 March 1982LER 82-014/03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable
05000272/LER-1982-024, Supplemental LER 82-024/03X-1:on 820410,svc Water Flow to Containment Fan Coil Unit 12 Discovered to Be Less than Required 700 Gpm.Caused by Valve 12SW223 Being Stuck in Closed Position.Valve Exercised17 November 1983Supplemental LER 82-024/03X-1:on 820410,svc Water Flow to Containment Fan Coil Unit 12 Discovered to Be Less than Required 700 Gpm.Caused by Valve 12SW223 Being Stuck in Closed Position.Valve Exercised
05000272/LER-1982-028, Corrected LER 82-028/03L-0:on 820425,both Channels of Refueling Water Storage Tank (RWST) Level Indication Showed Less than Min Vol.Caused by Refilling Spent Fuel Pool. Makeup to RWST Initiated21 May 1982Corrected LER 82-028/03L-0:on 820425,both Channels of Refueling Water Storage Tank (RWST) Level Indication Showed Less than Min Vol.Caused by Refilling Spent Fuel Pool. Makeup to RWST Initiated
05000272/LER-1982-029, Supplemental LER 82-029/03X-1:on 820501,during Surveillance Testing,Svc Water Flow to Containment Fan Coil Unit 12 Discovered Less than Required 2,500 Gallons Per Minute for Low Speed.Caused by Stuck Flow Control Valve17 November 1983Supplemental LER 82-029/03X-1:on 820501,during Surveillance Testing,Svc Water Flow to Containment Fan Coil Unit 12 Discovered Less than Required 2,500 Gallons Per Minute for Low Speed.Caused by Stuck Flow Control Valve
05000272/LER-1982-035, Supplemental LER 82-035/99X-1:on 820526,fire Pump 2 Failed to Start.Caused by Damaged Fire Pump Electrical Sys Voltage Regulator/Alternator,Due to Faulty Wiring Harness.Damaged Components Replaced1 June 1983Supplemental LER 82-035/99X-1:on 820526,fire Pump 2 Failed to Start.Caused by Damaged Fire Pump Electrical Sys Voltage Regulator/Alternator,Due to Faulty Wiring Harness.Damaged Components Replaced
05000272/LER-1982-042, Supplemental LER 82-042/03X-1:on 820628,valves 12AF10 & 12AF86 Discovered Open.Caused by Personnel Negligence in Failure to Notice That Chains on Valves Improperly Installed.Valve Operation & Tagging Lesson Plans Revised20 October 1982Supplemental LER 82-042/03X-1:on 820628,valves 12AF10 & 12AF86 Discovered Open.Caused by Personnel Negligence in Failure to Notice That Chains on Valves Improperly Installed.Valve Operation & Tagging Lesson Plans Revised
05000272/LER-1982-081, Supplemental LER 82-081/01X-1:on 821104,16 1,000-kip Steam Generator Snubbers Found Out of Spec on Bleed Test & Six Snubbers Failed Acceleration Test.Caused by Flattened Piston Seal Rubber Matl Due to Aging.Seals Rebuilt3 March 1983Supplemental LER 82-081/01X-1:on 821104,16 1,000-kip Steam Generator Snubbers Found Out of Spec on Bleed Test & Six Snubbers Failed Acceleration Test.Caused by Flattened Piston Seal Rubber Matl Due to Aging.Seals Rebuilt
05000272/LER-1982-083, Supplemental LER 82-083/03X-1:on 821102,control Room Operator Observed Temp Recorder for Air temp-delta T Channels Not Printing.Caused by Failure of Pinion Gear on Chart Drive Motor.Motor Replaced1 June 1983Supplemental LER 82-083/03X-1:on 821102,control Room Operator Observed Temp Recorder for Air temp-delta T Channels Not Printing.Caused by Failure of Pinion Gear on Chart Drive Motor.Motor Replaced
05000272/LER-1982-090, Supplemental LER 82-090/01X-1:on 821121,video Insp of Removed Fuel Assemblies Revealed Cladding Ruptures on Element 13 in Fuel Assembly D-20.Caused by Isolated Instance of Secondary Hydriding29 June 1983Supplemental LER 82-090/01X-1:on 821121,video Insp of Removed Fuel Assemblies Revealed Cladding Ruptures on Element 13 in Fuel Assembly D-20.Caused by Isolated Instance of Secondary HydridingFuel cladding
05000272/LER-1982-091, Supplemental LER 82-091/01X-1:on 821130,operator Discovered Leakage from Weld of Svc Water Piping to Component Cooling HX 12.Caused by Extensive Biofouling & Corrosion of Circumferential Welds8 June 1983Supplemental LER 82-091/01X-1:on 821130,operator Discovered Leakage from Weld of Svc Water Piping to Component Cooling HX 12.Caused by Extensive Biofouling & Corrosion of Circumferential WeldsHydrostatic
Biofouling
05000272/LER-1983-008, Supplemental LER 83-008/03X-1:on 830311,pressurizer Code Safety Valves 1PR3,1PR4 & 1PR5 Exceeded Lift Set Pressure Range & Had Heavy Seat Leakage.Partly Caused by Difference in Test Vs Actual Operating Conditions13 July 1983Supplemental LER 83-008/03X-1:on 830311,pressurizer Code Safety Valves 1PR3,1PR4 & 1PR5 Exceeded Lift Set Pressure Range & Had Heavy Seat Leakage.Partly Caused by Difference in Test Vs Actual Operating ConditionsLoop seal
Power Operated Valves
05000272/LER-1983-012, Telecopy Message of LER 83-012/01P-0:on 830222,both Reactor Trip Breakers Failed to Open.Cause Not Yet Determined. Investigation Underway28 February 1983Telecopy Message of LER 83-012/01P-0:on 830222,both Reactor Trip Breakers Failed to Open.Cause Not Yet Determined. Investigation Underway
05000272/LER-1983-023, Supplemental LER 83-023/01X-1:on 830602,notification Received from Westinghouse of Potential Unreviewed Safety Question Re Operation at Full Power Following Extended Reduced Power Operation.Procedures Implemented13 December 1983Supplemental LER 83-023/01X-1:on 830602,notification Received from Westinghouse of Potential Unreviewed Safety Question Re Operation at Full Power Following Extended Reduced Power Operation.Procedures Implemented
05000272/LER-1983-062, Supplemental LER 83-062/99X-1:on 831122,during Testing on Seismic Instrumentation,Triaxial Time History Accelograph Did Not Respond as Required.Caused by Detector Failure. Accelerometer Replaced24 February 1984Supplemental LER 83-062/99X-1:on 831122,during Testing on Seismic Instrumentation,Triaxial Time History Accelograph Did Not Respond as Required.Caused by Detector Failure. Accelerometer Replaced
05000311/LER-1981-0366 July 1981LER 81-036/03L-0:on 810606,pressurizer Pressure Channel 1 Indicated Greater than Max Allowable Tolerance.Caused by Pressure Transmitter 2PT455 Out of Spec.Unit Calibr & Returned to Svc
05000311/LER-1981-089, Supplemental LER 81-089/03X-1:on 810817,during Routine Wear & Alignment Check,Auxiliary Feedwater Pump 23 Linkage Between Trip Mechanism & Valve Found Loose.Caused by Loose Bolts.Bolts Tightened3 November 1982Supplemental LER 81-089/03X-1:on 810817,during Routine Wear & Alignment Check,Auxiliary Feedwater Pump 23 Linkage Between Trip Mechanism & Valve Found Loose.Caused by Loose Bolts.Bolts Tightened
05000311/LER-1982-001, Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed11 November 1983Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed
05000311/LER-1982-002, Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Vo20 October 1982Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Voltage
05000311/LER-1982-015, Supplemental LER 82-015/03X-1:on 820221,discovered That Reactor Coolant Leak Rate Surveillance 4.4.7.2.d Due 820220 Not Performed Because Plant Had Not Been in steady-state Condition Due to 820219 Reactor Trip8 December 1982Supplemental LER 82-015/03X-1:on 820221,discovered That Reactor Coolant Leak Rate Surveillance 4.4.7.2.d Due 820220 Not Performed Because Plant Had Not Been in steady-state Condition Due to 820219 Reactor TripMissed surveillance
05000311/LER-1982-017, Supplemental LER 82-017/03X-1:on 820228,svc Water Flow Indicated Zero Upon Starting Containment Fan Coil Unit 22 (Cfcu).On 820301,svc Water Flow to Cfcu 23 Less than Required 2,500 Gpm.Caused by Stuck Valve17 November 1983Supplemental LER 82-017/03X-1:on 820228,svc Water Flow Indicated Zero Upon Starting Containment Fan Coil Unit 22 (Cfcu).On 820301,svc Water Flow to Cfcu 23 Less than Required 2,500 Gpm.Caused by Stuck Valve
05000311/LER-1982-01831 March 1982LER 82-018/03L-0:on 820304,steam Generator 24 Feedwater Channel 2 Flow Indicator Failed.Caused by Failure of Force Motor in Flow Transmitter.Transmitter Properly Repaired, Calibr & Returned to Svc
05000311/LER-1982-01931 March 1982LER 82-019/03L-0:on 820307,undervoltage Condition in Safeguards Equipment Control Cabinet Caused Mod 1 2A Sec Actuation.Caused by Failure of Card File Assembly.Card File Assembly Replaced & Loads Secured.Sys Returned to Svc
05000311/LER-1982-024, Supplemental LER 82-024/03X-1:on 820328,sample Results from Boric Acid Storage Tank 21 & Boron Injection Tank 22 Indicated Concentrations Below Tech Spec Limit.Cause Unknown.Boric Acid Added29 June 1983Supplemental LER 82-024/03X-1:on 820328,sample Results from Boric Acid Storage Tank 21 & Boron Injection Tank 22 Indicated Concentrations Below Tech Spec Limit.Cause Unknown.Boric Acid AddedBoric Acid
Shutdown Margin
05000311/LER-1982-027, Supplemental LER 82-027/03X-1:on 820418,RCS Water Inventory SP(o)4.4.7.2.d Not Performed within Required Time Interval. License Change Request 82-14 Submitted to Eliminate RCS Water Inventory Requirement During Nonsteady State20 October 1982Supplemental LER 82-027/03X-1:on 820418,RCS Water Inventory SP(o)4.4.7.2.d Not Performed within Required Time Interval. License Change Request 82-14 Submitted to Eliminate RCS Water Inventory Requirement During Nonsteady State
05000311/LER-1982-070, Supplemental LER 82-070/01X-1:on 830809,0.5 Gpm Svc Water Leak Observed on Containment Fan Coil 24.Caused by Failed Cooling Coil Resulting from Silt Erosion by Particles in Svc Water29 June 1983Supplemental LER 82-070/01X-1:on 830809,0.5 Gpm Svc Water Leak Observed on Containment Fan Coil 24.Caused by Failed Cooling Coil Resulting from Silt Erosion by Particles in Svc WaterPacking leak
05000311/LER-1982-072, Supplemental LER 82-072/03X-1:on 820820,during Surveillance Testing,Discovered That Reactor Trip Breaker B Would Not Trip.Caused by Binding of Undervoltage Coil Solenoid.Coil Replaced & Breaker Reinstalled20 October 1982Supplemental LER 82-072/03X-1:on 820820,during Surveillance Testing,Discovered That Reactor Trip Breaker B Would Not Trip.Caused by Binding of Undervoltage Coil Solenoid.Coil Replaced & Breaker Reinstalled
05000311/LER-1982-074, Corrected LER 82-074/01T-0:on 820813,control Operator Discovered Increased Leakage to Containment Sump.Caused by Coil Failures Due to Silt Particles in Svc Water.Leak Repaired by Blanking Flanges18 August 1982Corrected LER 82-074/01T-0:on 820813,control Operator Discovered Increased Leakage to Containment Sump.Caused by Coil Failures Due to Silt Particles in Svc Water.Leak Repaired by Blanking Flanges
05000311/LER-1982-077, Supplemental LER 82-077/01X-1:on 820818,leakage Discovered from Containment Fan Coil 21.Caused by Erosion of Copper Nickel Piping.Cooling Coils Replaced w/erosion-resistant Matl29 June 1983Supplemental LER 82-077/01X-1:on 820818,leakage Discovered from Containment Fan Coil 21.Caused by Erosion of Copper Nickel Piping.Cooling Coils Replaced w/erosion-resistant Matl
05000311/LER-1982-083, Supplemental LER 82-083/03X-1:on 820812,during Routine Surveillance,Control Room Operator Received Low Svc Water Flow Indication on Containment Fan Coil Unit (Cfcu) 25. Caused by Oysters or Silt Restricting Cfcu Flow20 April 1983Supplemental LER 82-083/03X-1:on 820812,during Routine Surveillance,Control Room Operator Received Low Svc Water Flow Indication on Containment Fan Coil Unit (Cfcu) 25. Caused by Oysters or Silt Restricting Cfcu Flow
05000311/LER-1982-084, Telecopy Message of LER 82-084/01P:on 820829,svc Water Leak on Containment Fan Coil Unit 23 Discovered.Leak Isolated.No Cause Stated.Investigation in Progress30 August 1982Telecopy Message of LER 82-084/01P:on 820829,svc Water Leak on Containment Fan Coil Unit 23 Discovered.Leak Isolated.No Cause Stated.Investigation in Progress
05000311/LER-1982-092, Supplemental LER 82-092/01X-1:on 820908,svc Water Leak Discovered on Containment Fan Coil Unit 21,rendering Unit Inoperable.Caused by Motor Cooler Erosion Due to Silt in Svc Water.Cooler Replaced29 June 1983Supplemental LER 82-092/01X-1:on 820908,svc Water Leak Discovered on Containment Fan Coil Unit 21,rendering Unit Inoperable.Caused by Motor Cooler Erosion Due to Silt in Svc Water.Cooler Replaced
05000311/LER-1982-111, Telecopy Message of LER 82-111/01P:on 821002,during Routine Power Operation,Svc Water Leak Discovered Inside Containment Bldg on Containment Fan Coil Unit 23.Cause Undetermined.Rept Will Be Submitted Per IE Bulletin 80-244 October 1982Telecopy Message of LER 82-111/01P:on 821002,during Routine Power Operation,Svc Water Leak Discovered Inside Containment Bldg on Containment Fan Coil Unit 23.Cause Undetermined.Rept Will Be Submitted Per IE Bulletin 80-24
05000311/LER-1982-141, Updated LER 82-141/03X-1:on 821121 & 1204,P-250 Computer Inoperable Due to Parity Error.Caused by Periodic Increases in Ambient Temp Due to Insufficient Ventilation.Computer Reprogrammed & Action Statement Terminated16 December 1983Updated LER 82-141/03X-1:on 821121 & 1204,P-250 Computer Inoperable Due to Parity Error.Caused by Periodic Increases in Ambient Temp Due to Insufficient Ventilation.Computer Reprogrammed & Action Statement Terminated
05000311/LER-1983-007, Telecopy Message of LER 83-007/01P:on 830218,two 1,000-kip Steam Generator Snubbers Failed to Meet Lockup & Bleed Rate Velocity Requirements.Cause Not Stated.Investigation Continuing.Detailed Rept to Be Submitted in 14 Days18 February 1983Telecopy Message of LER 83-007/01P:on 830218,two 1,000-kip Steam Generator Snubbers Failed to Meet Lockup & Bleed Rate Velocity Requirements.Cause Not Stated.Investigation Continuing.Detailed Rept to Be Submitted in 14 Days
05000311/LER-1983-017, Supplemental LER 83-017/03X-1:on 810515,during Startup & Cycle 1 Operations,Leakage Past Pressurizer PORVs & Pressurizer Overpressure Protection Sys Values Observed. Cause Not Stated.Porvs Modified16 September 1983Supplemental LER 83-017/03X-1:on 810515,during Startup & Cycle 1 Operations,Leakage Past Pressurizer PORVs & Pressurizer Overpressure Protection Sys Values Observed. Cause Not Stated.Porvs Modified
05000311/LER-1983-023, Corrected LER 83-023/03L-0:on 830117-0418,seven Containment Isolation Valves Experienced Leakage Rates Greater than Max Range of Test Equipment.Total Containment Type B & C Leakage Could Not Be Demonstrated.Valves Repaired8 June 1983Corrected LER 83-023/03L-0:on 830117-0418,seven Containment Isolation Valves Experienced Leakage Rates Greater than Max Range of Test Equipment.Total Containment Type B & C Leakage Could Not Be Demonstrated.Valves Repaired
05000311/LER-1984-010, Corrected LER 84-010-00:on 840423,during Startup Operations, Turbine Trip & Reactor Trip Occurred.Caused by hi-hi Level in Steam Generator 23.Feedwater Flow Nozzle Replaced & All Sys Performed as Designed23 May 1984Corrected LER 84-010-00:on 840423,during Startup Operations, Turbine Trip & Reactor Trip Occurred.Caused by hi-hi Level in Steam Generator 23.Feedwater Flow Nozzle Replaced & All Sys Performed as Designed