ENS 40362
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ENS Event | |
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04:02 Nov 29, 2003 | |
Title | Automatic Scram Due To Low Reactor Water Level |
Event Description | At 2202 CST, a low Reactor Water Level Scram (Level 3) occurred due to lowering feedwater flow. All control rods inserted on the Scram. The Scram resulted in actuation of HPCI and RCIC on low Reactor Water level (Level 2), and the low level ATWS Recirculation Pump Trip (RPT). HPCI and RCIC initiated and both Reactor Recirculation pumps tripped. It is estimated that RCIC injected approximately 500 to 600 gallons, and HPCI injected less than 100 gallons. HPCI was secured early in the transient, and RCIC operated for approximately 2 minutes. Reactor Water level was recovered and maintained with the operating feedwater pump.
The Reactor Water low level (Level 3) also resulted in Group 2 (Primary Containment), Group 3 (Reactor Water Cleanup), and Group 6 isolations (Secondary Containment Isolation and Control Room Ventilation system start). All isolations functioned as designed. Initial indications are that Feedwater Pump B speed lowered unexpectedly, causing Reactor Water level to lower. Reactor Water level reached -44 inches (wide range instruments) [120 inches above top of active fuel]. The setpoints for HPCI, RCIC, and ATWS-RPT are -33 inches. Plans are to take the unit to Mode 4. The licensee notified the NRC Resident Inspector. |
Where | |
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Cooper Nebraska (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-1.25 h-0.0521 days <br />-0.00744 weeks <br />-0.00171 months <br />) | |
Opened: | John Myers 02:47 Nov 29, 2003 |
NRC Officer: | Mike Ripley |
Last Updated: | Nov 29, 2003 |
40362 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Shutdown (0 %) |
Cooper with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge | |
WEEKMONTHYEARENS 562782022-12-17T05:51:00017 December 2022 05:51:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram ENS 562202022-11-13T04:19:00013 November 2022 04:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram ENS 561742022-10-22T17:58:00022 October 2022 17:58:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge ECCS Injection While Shutdown ENS 549762020-11-01T10:34:0001 November 2020 10:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to an Un-Isolable Leak on the Turbine High Pressure Fluid System ENS 522612016-09-25T06:03:00025 September 2016 06:03:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of Group 1 Isolation Signal ENS 454892009-11-11T23:43:00011 November 2009 23:43:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram After a Turbine Hydraulic Fluid Leak ENS 454822009-11-07T01:30:0007 November 2009 01:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to an Unisolable Leak on the Turbine High Pressure Fluid System ENS 444022008-08-09T07:04:0009 August 2008 07:04:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Failure of Reheat Stop Valve to Open During Turbine Valve Testing ENS 433752007-05-19T07:12:00019 May 2007 07:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Control Rod Hcu Valve Bonnet Leak Into Reactor Building ENS 425942006-05-22T12:01:00022 May 2006 12:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram as a Mitigating Action Due to Lowering Service Air Pressure ENS 423752006-02-26T08:50:00026 February 2006 08:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Msr High Level ENS 420102005-09-23T05:40:00023 September 2005 05:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Degrading Main Condenser Vacuum ENS 416012005-04-15T09:36:00015 April 2005 09:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Reactor Scram and Specified System Actuations ENS 403622003-11-29T04:02:00029 November 2003 04:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Scram Due to Low Reactor Water Level 2022-12-17T05:51:00 | |
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