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Category:E-Mail
MONTHYEARML24271A0282024-09-26026 September 2024 E-Mail - Dresden Nuclear Power Station, Unit 1 - Site Visit Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations ML24250A1062024-09-0606 September 2024 NRR E-mail Capture - Final RAI - Constellation Energy Generation, LLC - Fleet Request - Proposed Alternative to Utilize Code Case OMN-32 (L-2024-LLR-0030) ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 ML24233A2472024-08-20020 August 2024 Acceptance of Requested Licensing Action Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations ML24176A0232024-06-21021 June 2024 NRR E-mail Capture - Dresden Nuclear Power Station, Units 2 and 3 - Acceptance Review of the Amendment Request to Adopt 10 CFR 50.69 ML24159A0122024-06-0606 June 2024 NRR E-mail Capture - Dresden Nuclear Power Station, Units 2 and 3 - Acceptance of Licensing Amendment to Adopt TSTF-505 and TSTF-591 ML24131A0612024-05-10010 May 2024 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request - Acceptance of Proposed Alternative to Utilize Code Case OMN-32 (L-2024-LLR-0030) ML24066A0802024-04-0101 April 2024 Email to Christian Williams Decision on the Exemption Request for Dresden Nuclear Power Station Unit 2 and Unit 3 Independent Spent Fuel Storage Installation in Morris, Illinois ML24065A4892024-03-28028 March 2024 Email to Christian Williams Availability of Environmental Assessment for the Exemption Request for Dresden Nuclear Power Station Unit 2 and Unit 3 Independent Spent Fuel Storage Installation in Morris, Illinois ML24078A3772024-03-15015 March 2024 Email to the State of Illinois Requesting Review of the Dresden Exemption Request Environmental Assessment ML24066A0872024-03-0404 March 2024 NRR E-mail Capture - Dresden 2 and 3 - Request for Additional Information for Alternative Request I5R-22 ML24067A1242024-03-0101 March 2024 Email to Christian Williams: Request for Additional Information Regarding Dresden Relief Request Dated February 23, 2024 ML24065A2922024-02-28028 February 2024 2/28/24 Email from Constellation: Clarifying Information Regarding Dresden Relief Request Dated February 23, 2024 ML23339A0882023-12-0404 December 2023 NRR E-mail Capture - NRC Acceptance Review Re Dresden, Units 2 and 3 Request for Relief I5R-22 ML23328A0092023-11-22022 November 2023 Supplement - Dresden Security Rule Exemption Request ISFSI Docket No. Reference (EPID L-2023-LLE-0031) (Email) ML23304A0172023-10-30030 October 2023 NRR E-mail Capture - Final RCI - Constellation Energy Generation, LLC - Dresden 1, 2 & 3 - Exemption from Security Rule (L-2023-LLE-0031) ML23268A0022023-09-22022 September 2023 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request - Acceptance of License Amendment Request to Adopt TSTF-264-A, Revision 0 ML23264A7992023-09-21021 September 2023 NRR E-mail Capture - Final RAI - Constellation Energy Generation, LLC Fleet Request License Amendment Request to Adopt TSTF-580, Revision 1 ML23263A9932023-09-20020 September 2023 NRR E-mail Capture - Dresden Nuclear Power Station, Units 2 and 3 - Acceptance of Licensing Action Submittal Re Amendment to Adopt TSTF-564 ML23163A2292023-06-12012 June 2023 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request - Acceptance of License Amendment Request to Adopt TSTF-580, Revision 1 ML23052A0652023-02-21021 February 2023 NRR E-mail Capture - Dresden Units 2 and 3 - Request for Additional Information for Alternative Request RV-23H ML23026A0172023-01-23023 January 2023 NRR E-mail Capture - (External_Sender) IEMA Response Action - Request for Comments on the Proposed Issuance of Amendment to Technical Specification 4.3.1 for Dresden Nuclear Power Station, Units 2 and 3 ML23019A0132023-01-12012 January 2023 NRR E-mail Capture - Final RAI Dresden 2 and 3 - License Amendment Pertaining to GNF3 Fuel Transition ML22354A2622022-12-20020 December 2022 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request - Acceptance of Request to Use Certain Provisions of the 2019 Edition of the ASME BPV Code, Section XI ML22325A1212022-11-21021 November 2022 NRR E-mail Capture - NRC Acceptance Review Re Dresden, Units 2 and 3 Request for Relief RV-02D (EPID L-2022-LLR-0075), RV-03 (EPID L-2022-LLR-0076), and RV-23H ML22301A0902022-10-28028 October 2022 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request - Acceptance of License Amendment Request to Adopt TSTF-301, Revision 2 ML22290A0842022-10-13013 October 2022 NRR E-mail Capture - Dresden 2 and 3 - RAI License Amendment Request Regarding New Fuel Storage Vault and Spent Fuel Storage Pool Criticality Methodologies ML22258A1882022-09-15015 September 2022 NRR E-mail Capture - Acceptance Review: Dresden 2 and 3 License Amendment Request to Revise Technical Specification 3.1.4, ML22258A1872022-09-13013 September 2022 NRR E-mail Capture - NRC Acceptance Review Dresden, Units 2 and 3, Amendment Request - Transition to GNF3 Fuel ML22229A0752022-08-16016 August 2022 NRR E-mail Capture - NRC Acceptance Review Dresden, Units 2 and 3 Request for Relief 16R-09 ML22229A0762022-08-16016 August 2022 NRR E-mail Capture - NRC Acceptance Review Dresden, Units 2 and 3 Request for Relief 16R-10 ML22203A0442022-07-21021 July 2022 Request for Additional Information (RAI) ML22200A0782022-07-19019 July 2022 NRR E-mail Capture - Constellation Energy Generation, LLC - Fleet Request to Use Honeywell Mururoa V4F1 R Supplied Air Suits ML22199A2412022-07-18018 July 2022 NRR E-mail Capture - Acceptance Review: Dresden Units 2 and 3 - License Amendment Request New Fuel Vault Storage and SFP Criticality Safety Analysis Methodology ML22199A2422022-07-13013 July 2022 NRR E-mail Capture - Draft RAI Dresden 2 and 3 Proposed Alternative Related to Sblc Nozzle Inspection for the Sixth Inservice Inspection Interval ML22103A2112022-04-12012 April 2022 NRR E-mail Capture - NRC Acceptance Review Dresden, Units 2 and 3 Request for Relief (16R-01) - EPID L-2022-LLR-0037 ML22103A2132022-04-12012 April 2022 NRR E-mail Capture - NRC Acceptance Review Dresden, Units 2 and 3 Request for Relief (16R-02) - EPID L-2022-LLR-0038 ML22041B5362022-02-10010 February 2022 NRR E-mail Capture - Constellation Energy Generation, LLC - Request for Additional Information Regarding Fleet License Amendment Request to Adopt TSTF-541 ML22039A2042022-02-0808 February 2022 NRR E-mail Capture - Public Meeting Dresden/Quad Cities - Proposed Alternative to Use ASME Code Case N-921 ML22027A3592022-01-26026 January 2022 U1: CY2022 Inspection Plan, Docket No. 05000010, License No. DPR-2 ML22020A0642022-01-13013 January 2022 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding Proposed Fleet Alternative for Repair of Water Level Instrumentation Partial Penetration Nozzles ML21321A3802021-11-17017 November 2021 NRR E-mail Capture - NRC Acceptance Review of Dresden Nuclear Power Station, Units 2 and 3, Request for Exemption from 10 CFR 2.109(b) ML21301A0672021-10-28028 October 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Acceptance of License Amendment Request to Adopt TSTF-541 ML21256A1902021-09-10010 September 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Request for Additional Information Regarding License Transfer Application ML21252A0482021-09-0707 September 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Fleet Alternative Request for Repair of Water Level Instrumentation Partial Penetration Nozzles ML21244A4012021-08-10010 August 2021 (Final) Request for Information (RAI) Dresden, Units 1, 2, 3, and ISFSI Request for Exemptions from Portions of 10 CFR 50.47 and 10 CFR 50 Appendix E ML21215A3502021-08-0303 August 2021 NRR E-mail Capture - Exelon Generation Company, LLC - Acceptance of License Amendment Request to Adopt TSTF-554 ML21190A0192021-07-0808 July 2021 NRR E-mail Capture - Exelon Fleet - Request for Additional Information Regarding Adoption of TSTF-582 and TSTF-583-T ML21154A0112021-05-28028 May 2021 NRR E-mail Capture - Extension of Comment Period for the Exelon Generation Company, LLC License Transfer Application ML21154A0142021-05-28028 May 2021 NRR E-mail Capture - Extension of Comment Period for the Exelon Generation Company, LLC License Transfer Application 2024-09-06
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I Steven Orth -Fwd: Tritium Timeline Page 1 1 From: Mark Ring To: -Orth, Steven Date: Fri. Mar 3, 2006 9:50 AM
Subject:
Fwd: Tritium Timeline Steve, Rough timeline for 2004 and 2006 tritium leakage at Dresden is attached to support the Green ticket response.
Please let us know if you need anything additional.-Mark CC: Slawinski, Wayne Gin I Steven Orth -Tritium Timeline Paae 1 1___------From: To: Date:
Subject:
Desiree Smith Ring, Mark Fri, Mar 3, 2006 9:42 AM Tritium Timeline Mark, Here's the information you requested from us.Desiree Steven Orth -TritiumLeakTimeline2004.w d Page 1 i Tritium Leak Timeline 2004 Tritium Leak August 26, tritium sampling result indicated 6.13E+6 pCi/L.August 26, the licensee began increased sampling.Beginning of September, the licensee began excavating area to locate and repair leak.October 14, pressurized suspect piping. However, did not locate leak. Therefore, the licensee decided to replace approximately 75 feet of the HPCI suction piping.November 29, HPCI realigned back to CST.December 8, 2004, an ACE determined that the primary cause for the failure of the HPCI suction piping was due to the degradation of the moisture barrier wrapping.
Deficiencies with the cathodic protection system was also identified as a contributing factor.Per the licensee's business plan, the remaining old piping, approximately 100 feet) was scheduled for replacement in June 2006.2006 Tritium Leak January 3, 2006, well E-3 showed tritium level of 5000 pCi/L.The licensee resampled on January 19, well E-3 increased to 89, 000 pCi/L. As a result, the licensee went to increased sampling.January 31, well E-3 indicated 90,000 pCi/L.February 10, well E-3 indicated tritium levels of 476,000 and 486,000 pCVL. As a result, the licensee increased sampling, to a daily basis, for seven wells in the vicinity of the suspect piping plus an additional 5 -9 wells.February 16, the licensee began excavating in the vicinity of well E-3.February 16, the inspectors observed the licensee's well sampling activity.March 3, the licensee completed shoring of the excavation site.March. 3 or 4, the licensee will pressurize the HPCI suction piping to determine the location of the leak. The licensee plans to replace all the HPCI suction, HPCI return, and CST cross-tie piping regardless if the leak location Is definitively identified by the testing.The licensee conducted G-Scan testing on approximately 70 feet of the LPCI (which is located in I Steven Orth -TritiumLeakTimeline2004.wDd Paae 2 1---- .............
the same areas as the HPCI suction and return) piping did not indicate any signs of piping wall reduction.
The licensee is still considering the remaining 100 feef of piping for testing.