ENS 40537
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ENS Event | |
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20:10 Feb 22, 2004 | |
Title | Manual Scram at Peach Bottom 2 Due to Decreasing Condenser Vacuum |
Event Description | Peach Bottom Unit 2 reactor was manually scrammed due to degrading main condenser vacuum. The reactor was manually scrammed prior to reaching the automatic scram setpoint. All plant systems responded as expected with no significant issues noted. A Group II and Group III Primary Containment Isolation was received due to reactor water level passing through 1 inch. All isolation systems responded as required and repositioned to their expected positions.
The licensee also indicated that all control rods properly inserted into the core. The method of decay heat removal was using the main condenser. The licensee initiated a post scram review to identify and correct the source of degrading vacuum. The licensee also indicated the manual scram was initiated at 25 inches and lowering of condenser vacuum. The licensee notified the NRC Resident Inspector. |
Where | |
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Peach Bottom Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-1.47 h-0.0613 days <br />-0.00875 weeks <br />-0.00201 months <br />) | |
Opened: | Barry Hedrick 18:42 Feb 22, 2004 |
NRC Officer: | Rich Laura |
Last Updated: | Feb 22, 2004 |
40537 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (100 %) |
After | Hot Shutdown (0 %) |
Peach Bottom with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 572212024-07-10T11:28:00010 July 2024 11:28:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Manual Turbine Trip ENS 569362024-01-29T17:02:00029 January 2024 17:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram ENS 558992022-05-16T19:52:00016 May 2022 19:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Scram Due to Electrical Transients ENS 555752021-11-14T10:25:00014 November 2021 10:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Trip Due to Lowering Main Condenser Vacuum ENS 536302018-09-30T04:00:00030 September 2018 04:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Scram Due to a Loss of Two Condensate Pumps ENS 472862011-09-21T14:20:00021 September 2011 14:20:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Relay Malfunction Resulted in a Valid Undervoltage Signal ENS 453482009-09-14T02:44:00014 September 2009 02:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to Short Period During Plant Shutdown ENS 428892006-10-07T21:50:0007 October 2006 21:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded, 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Technical Specification Required Shutdown Due to Loss of Primary Containment Integrity ENS 418322005-07-10T07:18:00010 July 2005 07:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip Resulting in Rps Actuation and Automatic Reactor Scram ENS 412772004-12-22T09:55:00022 December 2004 09:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Reactor Scram and Eccs Injection Following Opening of Turbine Bypass Valves ENS 405372004-02-22T20:10:00022 February 2004 20:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Scram at Peach Bottom 2 Due to Decreasing Condenser Vacuum ENS 401982003-09-25T04:00:00025 September 2003 04:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.73(a)(1), Submit an LER Initiation of a Technical Specification Required Shutdown at Peach Bottom 2 2024-07-10T11:28:00 | |
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