ENS 46996
ENS Event | |
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05:05 Jun 28, 2011 | |
Title | Failure of #2 Fire Water Pump to Realign |
Event Description | At 0005 CDT, on 06-28-2011, the Plant Shift Superintendent was notified that the C-631 High Pressure Fire Water (HPFW) pumps #2 and #3 automatically started in response to low HPFW header pressure created by a line leak and rendered inoperable. Following isolation of the water leak the #2 and #3 pumps were shut down and were being configured for automatic start. The RCW operator observed the 'Auto Start' Indicator for the #2 pump was not illuminated. The pump was declared inoperable and power was removed from the #2 pump for troubleshooting and repair by electrical maintenance (EM). When power was removed from the pump the HPFWS could not perform its intended safety function of providing 4875 gpm. Two HPFW system pumps are required to be operable according to TSR LCO 2.4.4.8. EM reset a disconnect interlock switch which reenergized the 'Auto Start' controls and the pump was declared operable and returned to service.
This event is reportable under 10 CFR 76.120(c)(2) as an event in which equipment required by the TSR is disabled or fails to function as designed. The NRC Senior Resident Inspector has been notified of this event.
Due to the uncertain nature of the leak on the 16 inch underground High Pressure Fire Water (HPFW) distribution main, it is not known at this time if the two operable HPFW pumps would have been able to satisfy the maximum sprinkler system demand of 4875 gpm. Upon completion of excavating the area of the leak, Engineering will evaluate the failure mode to determine if system requirements were maintained. The licensee notified the NRC Resident Inspector. Notified R2DO (M. Franke) and NMSS (R. Johnson).
Upon further evaluation it was determined that the (High Pressure Fire Water System) HPFWS was capable of fulfilling its intended safety function at all times during the incident. The safety function of the High Pressure Fire Water System established in SAR 3.15.7.2 is to provide sufficient fire suppression capability for the cascade process buildings to minimize the likelihood of a large fire. Fire scenarios were evaluated to establish the system design basis. A lube oil spill fire on the operating floor resulted in the highest sprinkler flow rate demand of 3200 gpm. A 500 gpm hose stream demand is added to the sprinkler system flow rate to obtain a maximum fire water flow rate of 3700 gpm for the evaluation basis fire event. As stated in the TSR 2.4.4.8 Basis Statement, the requirements for HPFWS operability established in TSR 2.4.4.8 are conservative with respect to the system evaluation presented in SAR 3.15.7.2. TSR SR 2.4.4.8-4 requires an annual flow rate verification of each HPFW pump. The most recent flow rate tests performed in Nov. 2010 demonstrate the capacity of each pump exceeds the evaluation basis flow demands. During the short time where only HPFW pump #3 was operable, this pump could have supplied more than the 3700 gpm required to satisfy the evaluation basis flow demand. The HPFWS remained capable of fulfilling its intended safety function. In addition, when HPFW pumps #2 and #3 were running in response to the leak on the underground distribution system, system pressure was approximately 134 psig. Using the pump curves established by the annual TSR surveillance test discussed above, this equates to a flow rate of approximately 5900 gpm. Any sprinkler system activation on the HPFWS would drop the system pressure to around 125 psig, slightly lowering the flow rate through the leak. During the time frame the leak was active, the HPFWS remained capable of fulfilling its intended safety function. The combined pump capacity of pumps #2 and #3 (10,600 gpm) demonstrated by the annual surveillance test exceeds the combined demand from the leak (5900 gpm) and the evaluation basis flow requirements (3700 gpm). Therefore, the HPFWS remained operable throughout the incident of the underground piping leak and the following time period of only one pump operable. Thus, reporting per 10 CRF 76.120 was not required and the subject notification can be retracted. The NRC Senior Resident Inspector has been notified of this retraction by the licensee. Notified R2DO (Freeman) and NMSS (Rahimi). |
Where | |
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Paducah Gaseous Diffusion Plant Paducah, Kentucky (NRC Region 2) | |
License number: | Gdp-1 |
Reporting | |
10 CFR 76.120(c)(2) | |
Time - Person (Reporting Time:+18.08 h0.753 days <br />0.108 weeks <br />0.0248 months <br />) | |
Opened: | R. J. Cook 23:10 Jun 28, 2011 |
NRC Officer: | Pete Snyder |
Last Updated: | Jul 14, 2011 |
46996 - NRC Website | |
Paducah Gaseous Diffusion Plant with 10 CFR 76.120(c)(2) | |
WEEKMONTHYEARENS 500992014-05-08T15:24:0008 May 2014 15:24:00
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Process Gas Leak Detection System ENS 429732006-11-07T22:07:0007 November 2006 22:07:00 10 CFR 76.120(c)(2) Failure of Process Gas Leak Detection System ENS 429722006-11-07T14:59:0007 November 2006 14:59:00 10 CFR 76.120(c)(2) Process Gas Leak Detector Failure ENS 428662006-09-28T23:02:00028 September 2006 23:02:00 10 CFR 76.120(c)(2) Failure of Autoclave High Cylinder Pressure System ENS 427632006-08-10T22:05:00010 August 2006 22:05:00 10 CFR 76.120(c)(2) Inoperable High Pressure Fire Water System ENS 425902006-05-20T12:15:00020 May 2006 12:15:00 10 CFR 76.120(c)(2) High Pressure Transmitter Failure ENS 424942006-04-12T13:13:00012 April 2006 13:13:00 10 CFR 76.120(c)(2) Uf6 Release Detection System Failed During Testing ENS 422382006-01-02T10:38:0002 January 2006 10:38:00 10 CFR 76.120(c)(2) Report of Safety Equipment Failure ENS 421762005-11-29T14:45:00029 November 2005 14:45:00 10 CFR 76.120(c)(2) Faulty Switch Rendered Criticality Accident Alarm System Inoperable ENS 418822005-07-29T02:25:00029 July 2005 02:25:00 10 CFR 76.120(c)(2) Failure of Safety Equipment on C-310 Cylinder Valve Closure System ENS 413782005-02-06T16:08:0006 February 2005 16:08:00 10 CFR 76.120(c)(2) 24 Hour Report of a Safety Equipment Failure ENS 412442004-12-04T12:50:0004 December 2004 12:50:00 10 CFR 76.120(c)(2) High Pressure Transmitter Failure ENS 412232004-11-23T19:25:00023 November 2004 19:25:00 10 CFR 76.120(c)(2) Failure of Uf6 Release Detection System Due to Loss of Electrical Power ENS 407382004-05-09T06:30:0009 May 2004 06:30:00 10 CFR 76.120(c)(2) Failure of the High Voltage Uf6 Release Detection System ENS 404992004-02-02T10:15:0002 February 2004 10:15:00 10 CFR 76.120(c)(2) Failure of C-360 #1 Autoclave High Pressure Isolation System. ENS 404922004-01-30T15:41:00030 January 2004 15:41:00 10 CFR 76.120(c)(2) Safety Equipment Failure ENS 404382004-01-12T00:00:00012 January 2004 00:00:00 10 CFR 76.120(c)(2) Safety Equipment Fails to Function ENS 404232004-01-02T08:30:0002 January 2004 08:30:00 10 CFR 76.120(c)(2) Failure of Autoclave Isolation System 2014-05-08T15:24:00 | |