ENS 50550
ENS Event | |
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00:51 Oct 20, 2014 | |
Title | Manual Reactor Trip Resulting in Aux Feedwater Actuation |
Event Description | This is an 8-hour notification being made to report that a valid ESF [emergency safety features] auxiliary feed water system actuation occurred. Salem Unit 1 was in mode 1 at 19% reactor power and executed a planned manual reactor trip to begin a scheduled refueling outage (1R23). The 11, 12, and 13 AFW [auxiliary feedwater] pumps were not in service prior to the reactor trip and as a result, narrow range levels in 12, 13, and 14 steam generators reached 14% before recovering. This resulted in a valid ESF actuation for low steam generator water level. Steam generator water levels were restored to normal post trip values as part of the procedurally directed response to a reactor trip.
All safety related equipment was operational before the reactor trip and AFW actuation and responded as required. There were no equipment failures that contributed to this event. There were no personnel injuries as a result of' this event. The NRC Resident Inspector has been informed. A transformer alarm caused the operators to trip the reactor prior to reaching the step in the procedure to start the AFW pumps.
On October 20, 2014 at 0136 EDT, Salem Unit 1 reported an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> notification of a valid ESF Auxiliary Feed Water System actuation following a manual reactor trip at the start of the S1R23 refueling outage. After additional review it was determined that the manual reactor trip met the criteria for a four hour report in accordance with 10CFR50.72(b)(2)(iv)(B), 'Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical...'. The licensee notified the NRC Resident Inspector. Notified R1DO (Noggle). |
Where | |
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Salem New Jersey (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+0.75 h0.0313 days <br />0.00446 weeks <br />0.00103 months <br />) | |
Opened: | Dan Mchugh 01:36 Oct 20, 2014 |
NRC Officer: | Mark Abramovitz |
Last Updated: | Nov 24, 2014 |
50550 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (19 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 562862022-12-24T07:22:00024 December 2022 07:22:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 542112019-08-11T12:14:00011 August 2019 12:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Feedwater Regulating Valve Malfunction ENS 538522019-01-31T08:01:00031 January 2019 08:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip - Circulating Water Icing Conditions ENS 536062018-09-14T04:00:00014 September 2018 04:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Failure of the Steam Generator Feed Regulating Valve ENS 533862018-05-07T07:25:0007 May 2018 07:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 526812017-04-14T17:57:00014 April 2017 17:57:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Emergency Diesel Generator Start Due to Loss of a 4160 V Bus ENS 522132016-08-31T19:11:00031 August 2016 19:11:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Reactor Coolant Flow ENS 520482016-06-28T08:23:00028 June 2016 08:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Main Generator Protection Signal ENS 517382016-02-16T13:27:00016 February 2016 13:27:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auxiliary Feedwater Pump Auto Start Due to Feed Pump Trip ENS 517342016-02-15T01:58:00015 February 2016 01:58:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Main Generator Protection Trip ENS 517082016-02-04T16:21:0004 February 2016 16:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Main Turbine Trip ENS 512902015-08-05T19:38:0005 August 2015 19:38:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Reactor Coolant Flow ENS 505502014-10-20T00:51:00020 October 2014 00:51:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Resulting in Aux Feedwater Actuation ENS 500922014-05-07T08:56:0007 May 2014 08:56:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Trip Due to Generator Protection Relay ENS 500322014-04-14T01:13:00014 April 2014 01:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Actuation of Main Generator Protection Relay ENS 500122014-04-09T01:14:0009 April 2014 01:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Manually Tripped Following the Loss of an Operating Steam Generator Feed Pump (Sgfp) ENS 486172012-12-21T10:28:00021 December 2012 10:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Automatic Reactor Trip on Turbine Trip ENS 485342012-11-25T16:30:00025 November 2012 16:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Steam Generator Feedwater Regulator Valve Not Responding to Demand Signal ENS 484572012-10-30T05:09:00030 October 2012 05:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip from 100% Power ENS 477662012-03-23T18:28:00023 March 2012 18:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip Followed by Automatic Reactor Trip ENS 469922011-06-26T04:00:00026 June 2011 04:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Reactor Coolant Pump ENS 467742011-04-21T20:01:00021 April 2011 20:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Circulating Water Pumps Out of Service ENS 463372010-10-17T09:12:00017 October 2010 09:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to 4 Kv Group Bus Undervoltage Condition ENS 463362010-10-16T03:21:00016 October 2010 03:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Turbine Trip ENS 460752010-07-07T15:17:0007 July 2010 15:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Caused by Main Generator and Turbine Trip ENS 458482010-04-16T20:41:00016 April 2010 20:41:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Emergency Diesel Generator Start Due to Loss of a 4160 V Bus ENS 456472010-01-21T23:20:00021 January 2010 23:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Low Steam Generator Water Level ENS 456042010-01-03T13:04:0003 January 2010 13:04:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Circulators After Uptake of River Ice ENS 446292008-11-05T05:57:0005 November 2008 05:57:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Start Due to Unexpected Esf Signal ENS 438732007-12-28T22:54:00028 December 2007 22:54:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Trip on Failure of Station Power Transformer ENS 435502007-08-06T17:10:0006 August 2007 17:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Spurious Interlock Signal to Feedwater Regulating Valves ENS 432592007-03-28T00:50:00028 March 2007 00:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Low Steam Generator Water Level Initiated Auxiliary Feedwater Signal and a Reactor Trip Signal ENS 429462006-10-30T01:11:00030 October 2006 01:11:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Start of Auxiliary Feedwater During Msiv Testing ENS 423952006-03-08T16:09:0008 March 2006 16:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip as a Result of a Turbine Generator Trip ENS 408752004-07-15T23:44:00015 July 2004 23:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Trip from 8% Power Due to Lowering Water Level on 23 Steam Generator ENS 408652004-07-13T17:05:00013 July 2004 17:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Low Steam Generator Water Level. ENS 406652004-04-11T04:23:00011 April 2004 04:23:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Plant Had a Valid Esf Signal to Start 1C Emergency Diesel Generator ENS 406392004-04-03T15:50:0003 April 2004 15:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of Auxiliary Feedwater System During Maintenance 2022-12-24T07:22:00 | |