05000321/FIN-2014004-04
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Finding | |
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Title | Licensee-Identified Violation |
Description | Technical Specification 3.4.3 requires 10 of 11 safety relief valves (SRVs) to be operable during Mode 1, 2, and 3. Contrary to the above, the licensee identified during bench testing that five safety relief valves failed to lift at the required technical specification setpoint, and therefore were inoperable when Unit 1 was in Mode 1, 2, and 3. Analysis showed that with the SRVs lifting at the as-found bench test setpoints, the SRVs still would have maintained reactor coolant system pressure below the TS safety limit requirements. The inspectors determined the violation was of very low safety significance (Green) because the SRVs maintained their functionality. This condition was documented in the licensees corrective action program as CR 809721. |
Site: | Hatch |
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Report | IR 05000321/2014004 Section 4OA7 |
Date counted | Sep 30, 2014 (2014Q3) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Licensee-identified |
Inspection Procedure: | |
Inspectors (proximate) | D Hardage D Retterer M Franke T Su |
Violation of: | Technical Specification |
INPO aspect | |
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Finding - Hatch - IR 05000321/2014004 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Hatch) @ 2014Q3
Self-Identified List (Hatch)
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