ENS 41280: Difference between revisions

From kanterella
Jump to navigation Jump to search
Created page by program invented by Mark Hawes
 
Created page by program invented by StriderTol
 
Line 16: Line 16:
| event date = 12/22/2004 13:07 CST
| event date = 12/22/2004 13:07 CST
| last update date = 12/22/2004
| last update date = 12/22/2004
| title = Rps Actuation Due To Steam Generator Low Level Signal  
| title = Rps Actuation Due to Steam Generator Low Level Signal  
| event text = Unit 2 reactor trip due to 2C steam generator LO-2 reactor protection signal. Auxiliary Feed Water actuated as expected.  No additional malfunctions or unexpected plant response.  Cause of LO-2 steam generator reactor protection signal under investigation.   
| event text = Unit 2 reactor trip due to 2C steam generator LO-2 reactor protection signal. Auxiliary Feed Water actuated as expected.  No additional malfunctions or unexpected plant response.  Cause of LO-2 steam generator reactor protection signal under investigation.   
This is a 4 hour notification of an RPS actuation per 10 CFR 50.72(b)(2)(iv)(B).  The 8 hour notification of Auxiliary Feed Water system actuation per 10 CFR 50.72 (b)(3)(iv)(B) is being made under this same telephone call.
This is a 4 hour notification of an RPS actuation per 10 CFR 50.72(b)(2)(iv)(B).  The 8 hour notification of Auxiliary Feed Water system actuation per 10 CFR 50.72 (b)(3)(iv)(B) is being made under this same telephone call.

Latest revision as of 21:22, 1 March 2018

ENS 41280 +/-
Where
Braidwood 
Illinois (NRC Region 3)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-4.07 h-0.17 days <br />-0.0242 weeks <br />-0.00558 months <br />)
Opened: Frank Ehrhardt
15:03 Dec 22, 2004
NRC Officer: Mike Ripley
Last Updated: Dec 22, 2004
41280 - NRC Website
Loading map...