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Unit 2 reactor trip due to 2C steam genera … Unit 2 reactor trip due to 2C steam generator LO-2 reactor protection signal. Auxiliary Feed Water actuated as expected. No additional malfunctions or unexpected plant response. Cause of LO-2 steam generator reactor protection signal under investigation. </br>This is a 4 hour notification of an RPS actuation per 10 CFR 50.72(b)(2)(iv)(B). The 8 hour notification of Auxiliary Feed Water system actuation per 10 CFR 50.72 (b)(3)(iv)(B) is being made under this same telephone call.</br>The licensee notified the NRC Resident Inspector. All control rods fully inserted. Decay heat is being removed to the main condenser via the turbine by-pass valves. The electrical grid is stable.</br>* * * UPDATE FROM F. EHRHARDT TO M. RIPLEY 15:55 ET 12/22/04 * * *</br>The licensee has determined that the RPS and Auxiliary Feed Water actuations were the result of an actual low level in the 2C steam generator. The cause of the low level is under investigation. The NRC Resident Inspector was informed. Notified R3 DO (L. Kozak). was informed. Notified R3 DO (L. Kozak). +
19:07:00, 22 December 2004 +
41,280 +
15:03:00, 22 December 2004 +
19:07:00, 22 December 2004 +
Unit 2 reactor trip due to 2C steam genera … Unit 2 reactor trip due to 2C steam generator LO-2 reactor protection signal. Auxiliary Feed Water actuated as expected. No additional malfunctions or unexpected plant response. Cause of LO-2 steam generator reactor protection signal under investigation. </br>This is a 4 hour notification of an RPS actuation per 10 CFR 50.72(b)(2)(iv)(B). The 8 hour notification of Auxiliary Feed Water system actuation per 10 CFR 50.72 (b)(3)(iv)(B) is being made under this same telephone call.</br>The licensee notified the NRC Resident Inspector. All control rods fully inserted. Decay heat is being removed to the main condenser via the turbine by-pass valves. The electrical grid is stable.</br>* * * UPDATE FROM F. EHRHARDT TO M. RIPLEY 15:55 ET 12/22/04 * * *</br>The licensee has determined that the RPS and Auxiliary Feed Water actuations were the result of an actual low level in the 2C steam generator. The cause of the low level is under investigation. The NRC Resident Inspector was informed. Notified R3 DO (L. Kozak). was informed. Notified R3 DO (L. Kozak). +
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