ENS 44743: Difference between revisions

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| event date = 12/27/2008 14:18 CST
| event date = 12/27/2008 14:18 CST
| last update date = 12/27/2008
| last update date = 12/27/2008
| title = Automatic Reactor Trip As A Result Of A Generator Trip
| title = Automatic Reactor Trip as a Result of a Generator Trip
| event text = At 1418 on 12-27-08 Braidwood Unit 2 experienced an automatic Reactor Trip.  The Reactor Trip red first out annunciator was Turb[ine] Trip above P8 Rx Trip.  At the time of the trip the Unit Aux Transformer [UAT] 241-1 sudden pressure relay actuated causing a main generator trip which resulted in a main turbine trip which resulted in a Reactor Trip.  Also at the same time as the Reactor Trip, the 2C Heater Drain Pump tripped on phase A over current.  Damage was subsequently noted on the pump motor terminal box.  No fire or smoke was observed at UAT 241-1 or the 2C Heater Drain Pump.
| event text = At 1418 on 12-27-08 Braidwood Unit 2 experienced an automatic Reactor Trip.  The Reactor Trip red first out annunciator was Turb[ine] Trip above P8 Rx Trip.  At the time of the trip the Unit Aux Transformer [UAT] 241-1 sudden pressure relay actuated causing a main generator trip which resulted in a main turbine trip which resulted in a Reactor Trip.  Also at the same time as the Reactor Trip, the 2C Heater Drain Pump tripped on phase A over current.  Damage was subsequently noted on the pump motor terminal box.  No fire or smoke was observed at UAT 241-1 or the 2C Heater Drain Pump.
After the Reactor Trip occurred, all four steam generators reached their low-2 Reactor Trip setpoints and the pressurizer reached its low pressure Reactor Trip setpoint all of which is an expected response on a trip from full power.  Steam generator levels and pressurizer pressure have been restored. Both the 2A and the 2B Auxiliary Feedwater Pumps auto started on the low-2 steam generator levels as expected.  All control rods fully inserted into the core.
After the Reactor Trip occurred, all four steam generators reached their low-2 Reactor Trip setpoints and the pressurizer reached its low pressure Reactor Trip setpoint all of which is an expected response on a trip from full power.  Steam generator levels and pressurizer pressure have been restored. Both the 2A and the 2B Auxiliary Feedwater Pumps auto started on the low-2 steam generator levels as expected.  All control rods fully inserted into the core.

Latest revision as of 22:12, 1 March 2018

ENS 44743 +/-
Where
Braidwood Constellation icon.png
Illinois (NRC Region 3)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-1.7 h-0.0708 days <br />-0.0101 weeks <br />-0.00233 months <br />)
Opened: Mike Deboard
18:36 Dec 27, 2008
NRC Officer: Vince Klco
Last Updated: Dec 27, 2008
44743 - NRC Website
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