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        A R E T t,,                                 UNITED STATES                           I
A R E T ,,
              .    o                 NUCLEAR REGULATORY COMMISSION                       I
UNITED STATES
  [               # ,$                               REGION 11
t
  g                   j                       101 MARIETTA STREET, N.W.                   l
o
  *                   2                       ATLANTA, GEORGI A 30323
NUCLEAR REGULATORY COMMISSION
    s,
.
        ...../
[
  Report Nos.: 50-327/85-32 and 50-328/85-32
# ,$
  Licensee:           Tennessee Valley Authority
REGION 11
                        6N11B Missionary Ridge Place
g
                        1101 Market Street
j
                        Chattanooga, TN 37402-2801
101 MARIETTA STREET, N.W.
  Docket Nos.: 50-327 and 50-328                           License Nos.: DPR-77 and DPR-79
*
  Facility Name:             Sequoyah linits 1 and 2
2
    Inspection Conducted:           September 6, - October 5, 1985
ATLANTA, GEORGI A 30323
    Inspectors:             6 f7 . d.,, Ini,                                     /4/34/85
...../
                      K.M.Jenison(/SeniorResidentInspector                     Date Signed
s,
                            C T dlnai,L,                                       An/D /RE
Report Nos.: 50-327/85-32 and 50-328/85-32
                      L. J. Watson, Re ident Inspector                         Date Sfgned
Licensee:
  Approved by:               .     [                                               3v!D
Tennessee Valley Authority
                        S. P. Weise, Section Chief                             Date Signed
6N11B Missionary Ridge Place
                      Division of Reactor Projects
1101 Market Street
                                                    Sl'MMARY
Chattanooga, TN 37402-2801
  Scope:       This routine, announced inspection involved 325 resident inspector-hours
Docket Nos.: 50-327 and 50-328
  onsite in the areas of: operational safety verification including operations
License Nos.: DPR-77 and DPR-79
  performance, system lineups, radiation protection, security and housekeeping
Facility Name:
  inspections; surveillance and maintenance observations; review of previous
Sequoyah linits 1 and 2
  inspection findings; followup of events; review of licensee identified items;
Inspection Conducted:
  Engineered Safety Feature; and review of inspector followup items.
September 6, - October 5, 1985
  Results: One violation was identified - Failure to follow procedure during a
Inspectors:
  test of the Control Room Chlorine Detection System (paragraph 10).
6 f7 . d.,, Ini,
    g1110226851030
/4/34/85
    0      ADOCK 05000327
K.M.Jenison(/SeniorResidentInspector
                                PDR
Date Signed
C T dlnai,L,
An/D /RE
L. J. Watson, Re ident Inspector
Date Sfgned
Approved by:
.
[
3v!D
S. P. Weise, Section Chief
Date Signed
Division of Reactor Projects
Sl'MMARY
Scope:
This routine, announced inspection involved 325 resident inspector-hours
onsite in the areas of: operational safety verification including operations
performance, system lineups, radiation protection, security and housekeeping
inspections; surveillance and maintenance observations; review of previous
inspection findings; followup of events; review of licensee identified items;
Engineered Safety Feature; and review of inspector followup items.
Results:
One violation was identified - Failure to follow procedure during a
test of the Control Room Chlorine Detection System (paragraph 10).
g1110226851030
ADOCK 05000327
0
PDR


        .
.
  .
.
                                  REPORT DETAILS
REPORT DETAILS
1.   Licensee Employees
1.
      Persons Contacted
Licensee Employees
      H. L. Abercrombie, Site Director
Persons Contacted
    *P. R. Wallace, Plant Manager
H. L. Abercrombie, Site Director
      L. M. Nobles, Operations and Engineering Superintendent
*P. R. Wallace, Plant Manager
    *B. M. Patterson, Maintenance Superintendent
L. M. Nobles, Operations and Engineering Superintendent
    *J. M. Anthony, Operations Group Supervisor
*B. M. Patterson, Maintenance Superintendent
    *D. C. Craven, Quality Assurance Supervisor
*J. M. Anthony, Operations Group Supervisor
      D. E. Crawley, Health Physics Supervisor
*D. C. Craven, Quality Assurance Supervisor
      J. L. Hamilton, Quality Engineering Supervisor
D. E. Crawley, Health Physics Supervisor
    *G. B. Kirk, Compliance Supervisor
J. L. Hamilton, Quality Engineering Supervisor
      D. H. Tullis, Mechanical Maintenance Group Supervisor
*G. B. Kirk, Compliance Supervisor
    *R. C. Birchell, Compliance Engineer
D. H. Tullis, Mechanical Maintenance Group Supervisor
    *C. L. Wilson, Nuclear Engineer
*R. C. Birchell, Compliance Engineer
    *C. E. Bosley, QA Evaluator, Division of QA, Quality Assurance Branch
*C. L. Wilson, Nuclear Engineer
    *D. L. Cowart, Quality Surveillance Supervisor
*C. E. Bosley, QA Evaluator, Division of QA, Quality Assurance Branch
      Other licensee employees contacted included technicians, operators, shift
*D. L. Cowart, Quality Surveillance Supervisor
      engineers, security force members, engineers and maintenance personnel.
Other licensee employees contacted included technicians, operators, shift
    * Attended exit interview
engineers, security force members, engineers and maintenance personnel.
2.   Exit Interview
* Attended exit interview
      The inspection scope and findings were summarized with the Plant Manager and
2.
      members of his staff on October 7, 1985. A violation described in paragraph
Exit Interview
      10 and a second example of a previous violation described in paragraph 6
The inspection scope and findings were summarized with the Plant Manager and
      were discussed. The licensee acknowledged the inspection findings and did
members of his staff on October 7, 1985. A violation described in paragraph
      not identify as proprietary any material reviewed by the inspectors during
10 and a second example of a previous violation described in paragraph 6
      this inspection.   During the reporting period, frequent discussions were
were discussed.
      held with the Site Director, Plant Mannger and his assistants concerning
The licensee acknowledged the inspection findings and did
      inspection findings. At no time during the inspection was written material
not identify as proprietary any material reviewed by the inspectors during
      provided to the licensee by the inspector.
this inspection.
3.   Licensee Action on Previous Inspection Findings (92702)
During the reporting period, frequent discussions were
      (Closed) Violation 328/83-16-02. The licensee's response of October 7,
held with the Site Director, Plant Mannger and his assistants concerning
      1983, was reviewed and the indicated corrective actions were audited.   The
inspection findings.
      licensee conducted Mechanical Maintenance Section training on the importance
At no time during the inspection was written material
      of adhering to mandatory Quality Assurance procedural hold points. The
provided to the licensee by the inspector.
      licensee's corrective actions are considered complete.
3.
Licensee Action on Previous Inspection Findings (92702)
(Closed) Violation 328/83-16-02.
The licensee's response of October 7,
1983, was reviewed and the indicated corrective actions were audited.
The
licensee conducted Mechanical Maintenance Section training on the importance
of adhering to mandatory Quality Assurance procedural hold points.
The
licensee's corrective actions are considered complete.


            .
.
                                                                                            '
'
        ,
2
                                                2
,
          (Closed) Violation 328/84-21-05.     The licensee's response of September 20,
(Closed) Violation 328/84-21-05.
          1984, was reviewed and the indicated corrective actions were audited. The
The licensee's response of September 20,
          licensee conducted training on the requirement for the independent verifi-
1984, was reviewed and the indicated corrective actions were audited. The
          cation of processed hold orders. In addition, administrative action was
licensee conducted training on the requirement for the independent verifi-
          taken with respect to the involved individuals. The licensee's corrective
cation of processed hold orders.
          actions are considered complete.
In addition, administrative action was
  *
taken with respect to the involved individuals.
          (Closed) Violation 328/83-31-03.       The licensee's response of March 15,
The licensee's corrective
          1984, was reviewed and the indicated corrective actions were audited. The
actions are considered complete.
          licensee conducted training on a variety of operational subjects involved
*
          with this violation.   Surveillance Instructions were revised to include the
(Closed) Violation 328/83-31-03.
          methods and details of valve locking. The licensee's corrective actions are
The licensee's response of March 15,
          considered complete.
1984, was reviewed and the indicated corrective actions were audited. The
          (Closed) Violation 328/83-31-04.       The licensee's response of March 15,
licensee conducted training on a variety of operational subjects involved
          1984, was reviewed and the indicated corrective actions were audited. The
with this violation.
          licensee amended its maintenance procedures to require that both Assistant
Surveillance Instructions were revised to include the
          Shift Engineers be required to sign prior to the removal from service of any
methods and details of valve locking. The licensee's corrective actions are
          inverter, 6900-volt shutdown board or 480-volt shutdown board.     In addition,
considered complete.
          this topic was included in licensed operator requalification training. The
(Closed) Violation 328/83-31-04.
          licensee's corrective actions are considered complete.
The licensee's response of March 15,
!       (Closed) Unresolved Item 327, 328/85-26-04. Corrective maintenance was
1984, was reviewed and the indicated corrective actions were audited. The
          reviewed on containment isolation valves 2-67-580A through D. Two of these
licensee amended its maintenance procedures to require that both Assistant
y        valves were examined by the inspector after being cut from the Essential Raw
Shift Engineers be required to sign prior to the removal from service of any
          Cooling Water system and disassembled. The valves were badly corroded and
inverter, 6900-volt shutdown board or 480-volt shutdown board.
          the internal flapper arm pins were out of round. The seating surface was
In addition,
          worn, but there was no indication of foreign materials within the valves.
this topic was included in licensed operator requalification training. The
          These valves were retested and determined to be operable. The licensee           ,
licensee's corrective actions are considered complete.
          updated their maintenance history associated with these components. This
!
          item is considered to be closed.
(Closed) Unresolved Item 327, 328/85-26-04.
    4.   Unresolved Items
Corrective maintenance was
          No unresolved items were identified during this,it.spection.
reviewed on containment isolation valves 2-67-580A through D.
    5.   Operational Safety Verification (71707)
Two of these
          a.   Plant Tours
valves were examined by the inspector after being cut from the Essential Raw
                The inspectors observed control room operations, reviewed applicable
y
                logs, conducted discussions with control room operators, observed shift
Cooling Water system and disassembled.
                turnovers, and confirmed operability of instrumentation.         The
The valves were badly corroded and
                inspectors verified the operability of selected emergency systems,
the internal flapper arm pins were out of round.
                reviewed tagout records, verified compliance with Technical
The seating surface was
                Specification (TS) Limiting Conditions for Operation (LCO) and verified
worn, but there was no indication of foreign materials within the valves.
                return to service of affected components. The inspectors verified that
These valves were retested and determined to be operable.
              maintenance work orders had been submitted as required and that
The licensee
                followup activities and prioritization of work was accomplished by the
,
                licensee.
updated their maintenance history associated with these components.
This
item is considered to be closed.
4.
Unresolved Items
No unresolved items were identified during this,it.spection.
5.
Operational Safety Verification (71707)
a.
Plant Tours
The inspectors observed control room operations, reviewed applicable
logs, conducted discussions with control room operators, observed shift
turnovers, and confirmed operability of instrumentation.
The
inspectors verified the operability of selected emergency systems,
reviewed tagout records, verified compliance with Technical
Specification (TS) Limiting Conditions for Operation (LCO) and verified
return to service of affected components. The inspectors verified that
maintenance work orders had been submitted as required and that
followup activities and prioritization of work was accomplished by the
licensee.
-
-
-
-
-
.


                                    .
.
                                '
3
                                                                        3
'
                                      Tours of the diesel generator, auxiliary, control, and turbine
Tours of the diesel generator, auxiliary, control, and turbine
                                      buildings were conducted to observe plant equipment conditions,
buildings were conducted to observe plant equipment conditions,
                                      including potential fire hazards, fluid leaks, and excessive vibrations
including potential fire hazards, fluid leaks, and excessive vibrations
                                      and plant housekeeping / cleanliness conditions.
and plant housekeeping / cleanliness conditions.
                                      The inspectors walked down accessible portions of the following
The inspectors walked down accessible portions of the following
                                      safety-related systems on l' nit 1 and l' nit 2 to verify operability and
safety-related systems on l' nit 1 and l' nit 2 to verify operability and
                                      proper valve alignment:
proper valve alignment:
                                            Residual Heat Removal System (l' nits 1 and 2)
Residual Heat Removal System (l' nits 1 and 2)
                                            Charging Pump Flowpath (l' nits 1 and 2)
Charging Pump Flowpath (l' nits 1 and 2)
                                            Diesel Generators (l' nits 1 and 2)
Diesel Generators (l' nits 1 and 2)
                                            Control Room Ventilation Chlorine Detection System (Common)
Control Room Ventilation Chlorine Detection System (Common)
                                  b.   Security
b.
                                      During the course of the inspection, observations relative to protected
Security
                                      and vital area security were made, including access controls, boundary
During the course of the inspection, observations relative to protected
                                      integrity, search, escort, and badging. No violations or deviations
and vital area security were made, including access controls, boundary
                                      were identified.
integrity, search, escort, and badging.
                                  c.   Radiation Protection
No violations or deviations
                                      The inspectors observed Health Physics (HP) practices and verified
were identified.
                                      implementation of radiation protection control. On a regular basis,
c.
                                      radiation work pennits (RWPs) were reviewed and specific work
Radiation Protection
                                      activities were monitored to assure the activities were being conducted
The inspectors observed Health Physics (HP) practices and verified
                                      in accordance with applicable RWPs. Selected radiation protection
implementation of radiation protection control.
                                      instruments were verified operable and calibration frequencies were
On a regular basis,
                                      reviewed.
radiation work pennits (RWPs) were reviewed and specific work
                                      On September 26, 1985, the inspector observed workers frisking out of a
activities were monitored to assure the activities were being conducted
                                      regulated zone, on EL690 at the hallway laading to the hot machine
in accordance with applicable RWPs.
                                      shop.   The licensee's procedure, Radiological Control Instruction,
Selected radiation protection
                                      RCI-1, Radiological Hygiene Control, requires frisking of the hands and
instruments were verified operable and calibration frequencies were
                                      feet with a counter provided at the ev.it to the area. One maintenance
reviewed.
                                      section worker exiting the regulated area frisked his feet, but did not
On September 26, 1985, the inspector observed workers frisking out of a
                                      frisk his hands. Failure to follow the radiation protection procedure
regulated zone, on EL690 at the hallway laading to the hot machine
                                      for frisking when exiting a regulated zone is a violation; however,
shop.
                                      since the licensee was in the process of implementing corrective action
The licensee's procedure, Radiological Control Instruction,
                                      for a similar violation (327, 328/85-26-03), involving the failure to
RCI-1, Radiological Hygiene Control, requires frisking of the hands and
                                      frisk out of a contaminated zone, this incident constitutes a further
feet with a counter provided at the ev.it to the area. One maintenance
                                      example of that violation.
section worker exiting the regulated area frisked his feet, but did not
                                      Corrective action for this incident included the assignment of an HP
frisk his hands.
                                      technician to the maintenance section to provide additional training
Failure to follow the radiation protection procedure
                                      and assure awareness of Health Physics (HP) procedures and practices.
for frisking when exiting a regulated zone is a violation; however,
                                      This training will be completed by January 3,1986.- Implementation of
since the licensee was in the process of implementing corrective action
                                      these actions are intended to prevent recurrence of similar incidents.
for a similar violation (327, 328/85-26-03), involving the failure to
. - - _ _ _ _ _ _ - _ _ _ _ - .
frisk out of a contaminated zone, this incident constitutes a further
example of that violation.
Corrective action for this incident included the assignment of an HP
technician to the maintenance section to provide additional training
and assure awareness of Health Physics (HP) procedures and practices.
This training will be completed by January 3,1986.- Implementation of
these actions are intended to prevent recurrence of similar incidents.
. - -
-
- .


            .
.
      .
4
                                              4
.
              Current audits conducted by the licensee indicate a substantial
Current audits conducted by the licensee indicate a substantial
              improvement in overall compliance with HP requirements during the past
improvement in overall compliance with HP requirements during the past
              year, and adequacy of corrective actions will be verified by TVA
year, and adequacy of corrective actions will be verified by TVA
              through future audits.
through future audits.
              In addition, the inspector noted that individuals were picking up the
In addition, the inspector noted that individuals were picking up the
              hand held monitor without frisking the hand used to pick up the
hand held monitor without frisking the hand used to pick up the
              monitor. This is a poor health physics practice and was brought to the
monitor. This is a poor health physics practice and was brought to the
              attention of plant management. The inspector will continue to monitor
attention of plant management.
              the frisk out process to assure proper controls are in place.
The inspector will continue to monitor
    6.   Engineered Safety Features Walkdown (71710)
the frisk out process to assure proper controls are in place.
        The inspectors verified operability of the Component Cooling Water System
6.
        (CCS) on Units 1 and 2 by performing a partial walkdown of the accessible
Engineered Safety Features Walkdown (71710)
        portions of the system. The remainder of the walkdown on this system will
The inspectors verified operability of the Component Cooling Water System
        be completed in the next inspection period. The following specifics were
(CCS) on Units 1 and 2 by performing a partial walkdown of the accessible
        reviewed and/or observed as appropriate:
portions of the system.
        a.   that the licensee's system lineup procedures matched plant drawings and
The remainder of the walkdown on this system will
              the as-built configuration;
be completed in the next inspection period.
        b.   that equipment conditions were satisfactory and items that might
The following specifics were
              degrade performance were identified and evaluated;
reviewed and/or observed as appropriate:
        c.   with assistance from licensee personnel, the interior of the breakers
a.
              and electrical or instrumentation cabinets- were inspected for debris,
that the licensee's system lineup procedures matched plant drawings and
              loose material, jumpers, evidence of rodents, etc.;
the as-built configuration;
        d.   that instrumentation was properly valved in and functioning and
b.
              calibration dates were appropriate;
that equipment conditions were satisfactory and items that might
        e.   that valves were in their proper positions, breaker alignment was
degrade performance were identified and evaluated;
              correct, power was available, and valves were locked as required; and
c.
        f.   local and remote instrumentation was compared, and remote instrumen-
with assistance from licensee personnel, the interior of the breakers
              tation was functional.
and electrical or instrumentation cabinets- were inspected for debris,
  ,
loose material, jumpers, evidence of rodents, etc.;
        During the tour, the inspectors identified several discrepancies:
d.
        -
that instrumentation was properly valved in and functioning and
              housekeeping in several areas was marginal
calibration dates were appropriate;
        -
e.
              new piping segments were attached to existing fire protection- piping
that valves were in their proper positions, breaker alignment was
              using masking tape
correct, power was available, and valves were locked as required; and
        -
f.
              valve labelling and location identifier accuracy
local and remote instrumentation was compared, and remote instrumen-
        -   conduit degradation
tation was functional.
        This was brought to the attention of the licensee. The licensee attributed
,
        the problem to outage work activities.
During the tour, the inspectors identified several discrepancies:
housekeeping in several areas was marginal
-
new piping segments were attached to existing fire protection- piping
-
using masking tape
valve labelling and location identifier accuracy
-
conduit degradation
-
This was brought to the attention of the licensee. The licensee attributed
the problem to outage work activities.
.
.


        .
.
  .
5
                                          5
.
    The inspector reviewed housekeeping logs kept by the licensee in accordance
The inspector reviewed housekeeping logs kept by the licensee in accordance
    with procedure SQA-66, Plant Housekeeping. TVA management housekeeping
with procedure SQA-66, Plant Housekeeping.
    tours are performed approximately monthly. Ditcrepant areas identified
TVA management housekeeping
    during tours are rechecked to assure corrective action has been taken. The
tours are performed approximately monthly.
    inspectors also reviewed Operations Section Letter OSLA-99, Auxiliary l' nit
Ditcrepant areas identified
    Operator (Al'0) Duties, and determined that Al'Os are required to identify
during tours are rechecked to assure corrective action has been taken. The
    housekeeping problems. The inspectors will review plant housekeeping and
inspectors also reviewed Operations Section Letter OSLA-99, Auxiliary l' nit
    licensee implementation of SQA-66 and OSLA-99 during the remainder of the
Operator (Al'0) Duties, and determined that Al'Os are required to identify
    outage.     Followu on this issue is an Inspector Followup Item
housekeeping problems.
    (327, 328/85-32-02) p
The inspectors will review plant housekeeping and
                        .
licensee implementation of SQA-66 and OSLA-99 during the remainder of the
    No violations or deviations were identified.
outage.
7.   Monthly Surveillance Observations (61726)
Followu
    The inspectors observed TS required surveillance testing and verified that
on this issue is an Inspector Followup Item
    testing was performed in accordance with adequate procedures; that test
(327, 328/85-32-02) p
    instrumentation was calibrated; that Limiting Conditions for Operation were
.
    met; that test results met acceptance criteria requirements and were
No violations or deviations were identified.
    reviewed by personnel other that the individual directing the test; that
7.
    deficiencies were identified, as appropriate, and that any deficiencies
Monthly Surveillance Observations (61726)
    identified during the testing were properly reviewed and resolved by
The inspectors observed TS required surveillance testing and verified that
    management personnel; and that system restoration was adequate. For the
testing was performed in accordance with adequate procedures; that test
    completed tests, the inspector verified that testing frequencies were met
instrumentation was calibrated; that Limiting Conditions for Operation were
    and tests were performed by qualified individuals.
met; that test results met acceptance criteria requirements and were
    The inspector witnessed / reviewed portions of the following surveillance test
reviewed by personnel other that the individual directing the test; that
    activities:
deficiencies were identified, as appropriate, and that any deficiencies
          SI-688.2       Functional Test for Accident Radi nion Monitor System
identified during the testing were properly reviewed and resolved by
          IMI-99         Reactor Protection System RT 11.6 & 11.8, Response Time
management personnel; and that system restoration was adequate.
                          Test of Delta T/Tavg Channels 2 and 4
For the
          SI-40           Centrifugal Charging Pump
completed tests, the inspector verified that testing frequencies were met
          SMI-0-90-1     High Dose Rate Calibration for Containment High Range
and tests were performed by qualified individuals.
                          Accident Monitors
The inspector witnessed / reviewed portions of the following surveillance test
    No violations or deviations were identified in this area.
activities:
8.   MonthlyMaintenanceObservations(62703)
SI-688.2
    a.   Station maintenance activities of safety-related systems and components
Functional Test for Accident Radi nion Monitor System
          were observed / reviewed to ascertain that they were conducted in
IMI-99
          accordance with approved procedures, regulatory guides, industry codes
Reactor Protection System RT 11.6 & 11.8, Response Time
          and standards, and in conformance with TS.
Test of Delta T/Tavg Channels 2 and 4
SI-40
Centrifugal Charging Pump
SMI-0-90-1
High Dose Rate Calibration for Containment High Range
Accident Monitors
No violations or deviations were identified in this area.
8.
MonthlyMaintenanceObservations(62703)
a.
Station maintenance activities of safety-related systems and components
were observed / reviewed to ascertain that they were conducted in
accordance with approved procedures, regulatory guides, industry codes
and standards, and in conformance with TS.


,
,
              .
.
    .
6
                                                          6
.
                          The following items were considered during this review: LCOs were met
The following items were considered during this review: LCOs were met
                          while components or systems were removed from service; redundant
while components or systems were removed from service; redundant
                          components were operable; approvals were obtained prior to initiating
components were operable; approvals were obtained prior to initiating
                          the work; activities were accomplished using approved procedures and
the work; activities were accomplished using approved procedures and
                          were inspected as applicable; procedures used were adequate to control
were inspected as applicable; procedures used were adequate to control
                          the activity; troubleshooting activities were controlled and the repair
the activity; troubleshooting activities were controlled and the repair
                          record accurately reflected what actually took place; functiona)
record accurately reflected what actually took place; functiona)
                          testing and/or calibrations were perfomed prior to returning
testing and/or calibrations were perfomed prior to returning
                          components or systems to service; quality control records were               -
components or systems to service; quality control records were
                          maintained; activities were accomplished by qualified personnel; parts
-
                          and materials used were properly certified; radiological controls were
maintained; activities were accomplished by qualified personnel; parts
                          implemented; QC hold points were established where required and were
and materials used were properly certified; radiological controls were
                          observed; fire prevention controls were implemented; outside contractor
implemented; QC hold points were established where required and were
                          force activities were controlled in accordance with the approved
observed; fire prevention controls were implemented; outside contractor
                          Quality Assurance (QA) program; and housekeeping was actively pursued.
force activities were controlled in accordance with the approved
  '
Quality Assurance (QA) program; and housekeeping was actively pursued.
      b.                   During the l' nit I refueling outage the inspector observed portions of
'
                          steam generator maintenance and audited documentation of the work                   '
b.
                          activities involving the cleaning of the secondary side by sludge
During the l' nit I refueling outage the inspector observed portions of
                          lancing, primary side eddy current examinations and plugging of the
steam generator maintenance and audited documentation of the work
                          Row I and other tubes for all four steam generators. - The following
'
                          procedures were reviewed / observed by the inspectors:
activities involving the cleaning of the secondary side by sludge
                                Radiation Work Permit:               02-1-85112
lancing, primary side eddy current examinations and plugging of the
Row I and other tubes for all four steam generators. - The following
procedures were reviewed / observed by the inspectors:
Radiation Work Permit:
02-1-85112
Maintenance Requests:
A549689,
A549690, A549692,
;
;
                                Maintenance Requests:                A549689,      A549690, A549692,
AS49528,
                                                                    AS49528,      A549691, A533110,
A549691, A533110,
4                                                                    A301950,     A302397, A302398,
A301950,
:                                                                   A302399
A302397, A302398,
                                                                                                    x
4
                                Vendor Standard:                     CFS-STD-020, Steam Generator
:
                                                                    Tube Sheet Sludge Re1 oval
A302399
                                                                                            '
x
                                Maintenance Instructions:           MI   3.7,   Preparation for
Vendor Standard:
                                                                      Performance of . and Recovery
CFS-STD-020, Steam Generator
                                                                      From Steam Generator Sludge
Tube Sheet Sludge Re1 oval
                                                                      Lancing
'
                                                                    MI 3.1, Removal and Installa-
Maintenance Instructions:
                                                                      tion of Steam Genera' tor' Primary
MI
                                                                    Manway Cover, l' nits 1 an_d 2
3.7,
                                                                    MI   3'. 3 , Steam Generator     *
Preparation
                                                                      Secondary Side Inspection
for
                                                                                                    m3
Performance of . and Recovery
                                                                    MI 3.4, Breaching Penetration
From Steam Generator Sludge
                                                                      X-54 Without Breaching the
Lancing
                                                                      ABSCE for Eddy Current Testing,     "
MI 3.1, Removal and Installa-
                                                                      Helium Leak Testing, Sludge
tion of Steam Genera' tor' Primary
                                                                      Lancing and Other Purposes     w
Manway Cover, l' nits 1 an_d 2
                                                                                                            1
MI
3'. 3 ,
Steam Generator
*
Secondary Side Inspection
m3
MI 3.4, Breaching Penetration
X-54 Without Breaching the
ABSCE for Eddy Current Testing,
"
Helium Leak Testing, Sludge
Lancing and Other Purposes
w
1
'
'
                                                                        s
s
        __.____________m_        _ - . . . _ . _ _ _ _ _
.
.
m
- . . .
.


                ,
,
          -t
-t
              .
.
        .                                           7
7
                                                              MI   3.2, Method of Plugging
.
                                                              Steam Generator Tubes
MI
                            Standard Practices:               SQA 119, l'nreviewed Safety
3.2, Method of Plugging
                                                              Question Determination (l'SQD)
Steam Generator Tubes
                                                              SQM 001,Sequoyah Nuclear Plant
Standard Practices:
                                                              Maintenance Program
SQA 119, l'nreviewed Safety
                            l'SQD Documentation:               l'SQD 85-0998, involving use of
Question Determination (l'SQD)
                                                              a special eddy current test
SQM 001,Sequoyah Nuclear Plant
                                                              probe for Row 1 tubes.
Maintenance Program
                                            d
l'SQD Documentation:
                                                              l'SQD   85-0999,   involving
l'SQD 85-0998, involving use of
                                                              performance of worker platform
a special eddy current test
                                                              training.
probe for Row 1 tubes.
                            ASME Code Document:               ASME Code Section XI, 1977
d
                  <
l'SQD
                                                              amended by Summer 1978 addenda
85-0999,
                    The licensee began steam generator (SG) maintenance with a visual
involving
                    examination of the secondary side using a fiberscope to determine the
performance of worker platform
                    condition of the steam generators. Video recordings were made of the
training.
                      in:;pection. It was determined that sludge lancing was needed to remove
ASME Code Document:
                    sediment on the secondary side at the tube sheet. The inspector
ASME Code Section XI, 1977
                    observed sludge lancing activities, which involved a newly developed
amended by Summer 1978 addenda
                    technique.
<
                    All four SGs were sludge lanced between three to four sweeps each with
The licensee began steam generator (SG) maintenance with a visual
                    a total of approximately 1750 pounds of sludge removed. This averaged
examination of the secondary side using a fiberscope to determine the
                    over 400 pounds'per SG. Fiberscopic examinations after completion
condition of the steam generators.
                      indicated that the SGs were essentially clean. The new technique was
Video recordings were made of the
                    found to be more effective for sludge removal.
in:;pection.
                    The licensee stated that the sludge removed consisted of approximately
It was determined that sludge lancing was needed to remove
                    70% iron and 30% copper. The licensee is also replacing the main
sediment on the secondary side at the tube sheet.
                    feedwater heaters and the moisture separator reheater tube bundles
The inspector
  ,                  during this outage to eliminate copper from the secondary system. The
observed sludge lancing activities, which involved a newly developed
                      licensee recovered two small pieces of a drill bit from one steam
technique.
                    generator.     No damage was attributed to this material. The licensee
All four SGs were sludge lanced between three to four sweeps each with
a total of approximately 1750 pounds of sludge removed. This averaged
over 400 pounds'per SG.
Fiberscopic examinations after completion
indicated that the SGs were essentially clean.
The new technique was
found to be more effective for sludge removal.
The licensee stated that the sludge removed consisted of approximately
70% iron and 30% copper.
The licensee is also replacing the main
feedwater heaters and the moisture separator reheater tube bundles
during this outage to eliminate copper from the secondary system. The
,
licensee recovered two small pieces of a drill bit from one steam
generator.
No damage was attributed to this material.
The licensee
also had to recover parts of a camera that came loose during a
*
*
                    also had to recover parts of a camera that came loose during a
fiberscopic exam.
    s              fiberscopic exam.
s
                "
"
                    The licensee inspected 100% of the tubes on all four SGs using eddy
The licensee inspected 100% of the tubes on all four SGs using eddy
                    current probes, with the exception of the l'-bend portion of the Row 2
current probes, with the exception of the l'-bend portion of the Row 2
                    tubes. This exception was made due to the difficulty associated with
tubes.
                    an inspection of these lf-bends and no industry wide history of failures
This exception was made due to the difficulty associated with
      -
an inspection of these lf-bends and no industry wide history of failures
            \        in the Row 2 l'-bend area.
\\
                    4
in the Row 2 l'-bend area.
                \
-
    8e
4
\\
8e


                                                                                    ____
____
      .
.
  .                                         8
8
        .The eddy current exams identified .that four Row 1 tubes had indications
.
          of corrosive cracking. Although the indications were minor and could
.The eddy current exams identified .that four Row 1 tubes had indications
          riot be categorized as to depth, the licensee decided to plug the Row 1
of corrosive cracking.
          tubes in all four steam generators to ensure that cracks did not
Although the indications were minor and could
          develop in these tubes. The licensee will evaluate the indications and
riot be categorized as to depth, the licensee decided to plug the Row 1
          can later remove the Row 1 tube plugs as desired. The licensee is
tubes in all four steam generators to ensure that cracks did not
          evaluating a stress relieving process which employs electric heaters to
develop in these tubes. The licensee will evaluate the indications and
          remove induced thermal stresses as a part of the process that could
can later remove the Row 1 tube plugs as desired.
          return the plugged Row 1 tubes to service. Three other tubes with
The licensee is
          indications of less than 30% through wall were plugged. At the end of
evaluating a stress relieving process which employs electric heaters to
          this inspection period, the licensee was still evaluating the eddy
remove induced thermal stresses as a part of the process that could
          current data and may elect to plug additional tubes.
return the plugged Row 1 tubes to service. Three other tubes with
          The licensee also utilized a new device for tube plugging developed by
indications of less than 30% through wall were plugged. At the end of
          Combustion Engineering.       The device was installed in the steam
this inspection period, the licensee was still evaluating the eddy
        . generator and manipulated remotely to install *;ube plugs. The device
current data and may elect to plug additional tubes.
          is capable of employing a magazine which can be loaded with a number of
The licensee also utilized a new device for tube plugging developed by
          plugs at one time reducing entries into the SG. The device offered
Combustion Engineering.
          reductions in the dose and time associated with SG tube plugging. The
The device was installed in the steam
          licensee estimated that the dose - associated with the plugging
. generator and manipulated remotely to install *;ube plugs.
          operations during this outage was reduced from approximately 200 rem to
The device
          50 rem.
is capable of employing a magazine which can be loaded with a number of
    c.   Replacement of the 1-A Centrifugal Charging Pump mechanical seals was
plugs at one time reducing entries into the SG.
          observed. The following documents were reviewed / observed in part:
The device offered
                                                    ,
reductions in the dose and time associated with SG tube plugging. The
                Maintenance Instruction (MI) 6.4 - Removal, Inspection and
licensee estimated that the dose - associated with the plugging
                Replacement of Centrifugal Charging Pump Seals
operations during this outage was reduced from approximately 200 rem to
                Surveillance Instruction (SI) 40 - Centrifugal Charging Pump
50 rem.
                Maintenance Request A529430       '
c.
Replacement of the 1-A Centrifugal Charging Pump mechanical seals was
observed. The following documents were reviewed / observed in part:
,
Maintenance Instruction (MI) 6.4 - Removal, Inspection and
Replacement of Centrifugal Charging Pump Seals
Surveillance Instruction (SI) 40 - Centrifugal Charging Pump
Maintenance Request A529430
'
~
~
          During the performance of the seal replacement, the technicians
During the performance of the seal replacement, the technicians
          identified that an 0-ring, issued from Power Stores, was not the size
identified that an 0-ring, issued from Power Stores, was not the size
          specified by the vendor. This appeared to be due to mispackaging of
specified by the vendor.
          the 0-ring by the vendor, since the shipping package and the receipt
This appeared to be due to mispackaging of
          documentation matched the material identification numbers specified by
the 0-ring by the vendor, since the shipping package and the receipt
          the vendor. A new 0-ring was requisitioned to replace the defective
documentation matched the material identification numbers specified by
          one,
the vendor.
    d.   During this outage period, preventive maintenance was conducted on both
A new 0-ring was requisitioned to replace the defective
          l' nit 1 and l' nit 2 Reactor Coolant Pumps (RCP). One activity involved
one,
          an evaluation of the breakaway torque associated with each RCP motor.
d.
          Maintenance Request A529848 was used to obtain the breakaway torque for
During this outage period, preventive maintenance was conducted on both
          each RCP motor and the data was evaluated against vendor's acceptance
l' nit 1 and l' nit 2 Reactor Coolant Pumps (RCP).
          criteria.       The inspector observed the performance of the preventive
One activity involved
          maintenance on the l' nit 2 loop 3 RCP with no discrepancies . identified.
an evaluation of the breakaway torque associated with each RCP motor.
          The licensee later identified the t' nit 1 loop 2 RCP as not meeting the
Maintenance Request A529848 was used to obtain the breakaway torque for
          acceptance criteria and disassembled the subject pump to perform
each RCP motor and the data was evaluated against vendor's acceptance
          corrective maintenance.
criteria.
                                \
The inspector observed the performance of the preventive
                                                                                          - ,
maintenance on the l' nit 2 loop 3 RCP with no discrepancies . identified.
The licensee later identified the t' nit 1 loop 2 RCP as not meeting the
acceptance criteria and disassembled the subject pump to perform
corrective maintenance.
\\
-
,


          .
.
    ..                                     9
9
        No violations or deviations were identified.
..
  9.   Licensee Event Report (LER) Followup (92700)
No violations or deviations were identified.
        The following LER's were reviewed and closed. The inspector verified that:
9.
        reporting requirements had been met; causes had been identified; corrective
Licensee Event Report (LER) Followup (92700)
        actions appeared appropriate; generic applicability had been considered; the
The following LER's were reviewed and closed. The inspector verified that:
        LER forms were complete; the licensee had reviewed the event; no unreviewed
reporting requirements had been met; causes had been identified; corrective
        safety questions were involved; and violations of regulations or TS condi-
actions appeared appropriate; generic applicability had been considered; the
        tions had been identified.
LER forms were complete; the licensee had reviewed the event; no unreviewed
        a.   LER Unit 1
safety questions were involved; and violations of regulations or TS condi-
              327/82115     Inoperable Upper Containment Personnel Airlock
tions had been identified.
                            (Revision 1)
a.
              327/83093     Inoperable Condenser Vacuum Flow Rate Monitor
LER Unit 1
                            (Revision 1)
327/82115
              327/83100   Automatic Control Valve Declared Inoperable
Inoperable Upper Containment Personnel Airlock
(Revision 1)
327/83093
Inoperable Condenser Vacuum Flow Rate Monitor
(Revision 1)
327/83100
Automatic Control Valve Declared Inoperable
327/83165
Primary Containment Internal Pressure (Revision 1)
,
,
              327/83165    Primary Containment Internal Pressure (Revision 1)
327/83168
              327/83168    1 A-A Diesel Generator (DG) Failed to Start
1 A-A Diesel Generator (DG) Failed to Start
              327/83177     2 A-A DG Failed to Trip
327/83177
              327/83183     Limitorque Operator Limit Switch Failed
2 A-A DG Failed to Trip
              327/83186     1 A-A DG Trip
327/83183
Limitorque Operator Limit Switch Failed
327/83186
1 A-A DG Trip
.
327/84011
Control Habitability System (Revision 1)
327/84034
No Flow Indication on 'B'
Essential Raw Cooling Water
Header
327/84045
Inoperable Auxiliary Air Compressors (Revision 1)-
327/85003
Surveillance Interval Exceeded
327/85022
Failure to Complete Hourly Fire Watch
327/85024
Failure to Complete Hourly Fire Watch
'327/85025-
Failure to Obtain a Noble Gas Sample
327/85028
Failure to Complete Hourly Fire Watch
327/85031
Auxiliary Building Isolation
327/85033.
Main Control Room Isolation
-
.
.
              327/84011    Control Habitability System (Revision 1)
-
              327/84034    No Flow Indication on 'B' Essential Raw Cooling Water
- .-
                            Header
-
              327/84045    Inoperable Auxiliary Air Compressors (Revision 1)-
.
              327/85003    Surveillance Interval Exceeded
..
              327/85022    Failure to Complete Hourly Fire Watch
              327/85024    Failure to Complete Hourly Fire Watch
            '327/85025-   Failure to Obtain a Noble Gas Sample
              327/85028    Failure to Complete Hourly Fire Watch
              327/85031    Auxiliary Building Isolation
              327/85033.   Main Control Room Isolation
                                                -        .      -      - .-    -  . ..


          .
.
    ,                                     10
10
            327/85035       Emergency Diesel Generator Start
,
            327/85036       Failure to Complete Hourly Fire Watch
327/85035
      b.   LER l' nit 2
Emergency Diesel Generator Start
            328/84004       Loss of 6900 Volt l' nit Board
327/85036
            328/84020       Inadvertent Safety Inje: tion (Revision 1)
Failure to Complete Hourly Fire Watch
  10. EventFollowup(93702,62703,61726)
b.
      a.   On August 27, 1985 an engineered safety feature actuation occurred as a
LER l' nit 2
            result of a Train B main control room isolation signal.       The main
328/84004
            control room isolation occurred during the performance of Surveillance
Loss of 6900 Volt l' nit Board
            Instruction (SI) 240, Functional Test of Control Room Air Intake
328/84020
            Chlorine Detection System. Step 4.4 of SI 240 requires the technician
Inadvertent Safety Inje: tion (Revision 1)
10. EventFollowup(93702,62703,61726)
a.
On August 27, 1985 an engineered safety feature actuation occurred as a
result of a Train B main control room isolation signal.
The main
control room isolation occurred during the performance of Surveillance
Instruction (SI) 240, Functional Test of Control Room Air Intake
Chlorine Detection System.
Step 4.4 of SI 240 requires the technician
-
-
            to place switch HS-43-205B in the test position prior to introducing
to place switch HS-43-205B in the test position prior to introducing
            chlorine fumes into the detection system.     The technician performing
chlorine fumes into the detection system.
            the surveillance and the assistant observing his actions failed to
The technician performing
            implement step 4.4 of SI 240, and as a consequence, initiated an
the surveillance and the assistant observing his actions failed to
            engineered safety feature actuation when the chlorine fumes were
implement step 4.4 of SI 240, and as a consequence, initiated an
            introduced into the. detection system. This failure to follow procedure
engineered safety feature actuation when the chlorine fumes were
            constitutes a violation (327, 328/85-32-01). The technician placed the
introduced into the. detection system. This failure to follow procedure
            subject switch in the test position after becoming aware of the main
constitutes a violation (327, 328/85-32-01). The technician placed the
            control room isolation. He then continued the surveillance, initialing
subject switch in the test position after becoming aware of the main
            Section 4.4 of Appendix B to SI 240 and reapplying the chlorine
control room isolation. He then continued the surveillance, initialing
            standard to the detection system, without informing appropriate
Section 4.4 of Appendix B to SI 240 and reapplying the chlorine
            supervisory or operations personnel.
standard to the detection system, without informing appropriate
            As a result of previous Inspector Followup Item (327, 328/85-26-07),
supervisory or operations personnel.
            the licensee committed to provide formal instructions to employees on
As a result of previous Inspector Followup Item (327, 328/85-26-07),
            actions to be taken when the employee fails to follow procedures. The
the licensee committed to provide formal instructions to employees on
            licensee issued a maintenance notice entitled, Your Responsibilities
actions to be taken when the employee fails to follow procedures. The
            in Following Instructions,   to all maintenance employees on or about
licensee issued a maintenance notice entitled, Your Responsibilities
            July 22, 1985. Based on inspector review, a majority of the mainte-
in Following Instructions,
            nance technicians appear to have received the notice. The technician
to all maintenance employees on or about
            that was involved in the above failure to follow procedure was tem-
July 22, 1985.
            porarily assigned to the TVA training center during the period that
Based on inspector review, a majority of the mainte-
            the notice was issued and therefore was not . fully aware of its
nance technicians appear to have received the notice.
            contents. Inspector Followup Item 327, 328/85-26-07 will-remain open
The technician
            pending further NRC assessment.-
that was involved in the above failure to follow procedure was tem-
      b.   On' September 27, 1985, a Combustion Engineering employee abraded his
porarily assigned to the TVA training center during the period that
            plastic ~ gloves and scraped his hand on the SG tube sheet while per-
the notice was issued and therefore was not . fully aware of its
            forming steam generator tube plugging activities. The individual
contents.
                      _
Inspector Followup Item 327, 328/85-26-07 will-remain open
            was removed from the area for decontamination. Initial contamination
pending further NRC assessment.-
            was approximately 1,000 cpm. The licensee decontaminated the hand to a
b.
            level of 400 cpm. At the advice of an offsite physician, the licensee
On' September 27, 1985, a Combustion Engineering employee abraded his
                          -                                                         ;
plastic ~ gloves and scraped his hand on the SG tube sheet while per-
forming steam generator tube plugging activities.
The individual
_
was removed from the area for decontamination.
Initial contamination
was approximately 1,000 cpm. The licensee decontaminated the hand to a
level of 400 cpm.
At the advice of an offsite physician, the licensee
-
;


,
,
            *
*
          .
.
      ..                                   11
11
              decided to take the individual to the hospital for further treatment.
..
              The licensee declared an l'nusual Event in accordance with IP-1,
decided to take the individual to the hospital for further treatment.
              Emergency Plan Classification Logic, and IP-2, Notification of l'nusual
The licensee declared an l'nusual Event in accordance with IP-1,
              Event, in anticipation of transporting a contaminated person to an
Emergency Plan Classification Logic, and IP-2, Notification of l'nusual
              offsite medical facility.   The individual, however, refused to be
Event, in anticipation of transporting a contaminated person to an
              transported offsite and continued decontamination efforts.       He
offsite medical facility.
              successfully reduced the contamination to below acceptable limits, and
The individual, however, refused to be
              the t'nusual Event was terminated. Reports of the incident were made to
transported offsite and continued decontamination efforts.
              the NRC and the State of Tennessee, as required.
He
  'll.   Inspector Followup Items (92701)
successfully reduced the contamination to below acceptable limits, and
          Based on inspection activities in the affected functional areas the
the t'nusual Event was terminated.
        .following items were determined to require no additional specific followup
Reports of the incident were made to
          and are closed.
the NRC and the State of Tennessee, as required.
              328/84-21-04
'll.
              328/84-31-05
Inspector Followup Items (92701)
              328/84-31-06
Based on inspection activities in the affected functional areas the
              327/84-11-03
.following items were determined to require no additional specific followup
              327/83-23-04
and are closed.
328/84-21-04
328/84-31-05
328/84-31-06
327/84-11-03
327/83-23-04
}}
}}

Latest revision as of 05:54, 12 December 2024

Insp Repts 50-327/85-32 & 50-328/85-32 on 850906-1005. Violation Noted:Failure to Follow Procedure During Test of Control Room Chlorine Detection Sys
ML20134B074
Person / Time
Site: Sequoyah  
Issue date: 10/30/1985
From: Jenison K, Linda Watson, Weise S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20134B062 List:
References
50-327-85-32, 50-328-85-32, NUDOCS 8511110226
Download: ML20134B074 (12)


See also: IR 05000327/1985032

Text

r-

A R E T ,,

UNITED STATES

t

o

NUCLEAR REGULATORY COMMISSION

.

[

  1. ,$

REGION 11

g

j

101 MARIETTA STREET, N.W.

2

ATLANTA, GEORGI A 30323

...../

s,

Report Nos.: 50-327/85-32 and 50-328/85-32

Licensee:

Tennessee Valley Authority

6N11B Missionary Ridge Place

1101 Market Street

Chattanooga, TN 37402-2801

Docket Nos.: 50-327 and 50-328

License Nos.: DPR-77 and DPR-79

Facility Name:

Sequoyah linits 1 and 2

Inspection Conducted:

September 6, - October 5, 1985

Inspectors:

6 f7 . d.,, Ini,

/4/34/85

K.M.Jenison(/SeniorResidentInspector

Date Signed

C T dlnai,L,

An/D /RE

L. J. Watson, Re ident Inspector

Date Sfgned

Approved by:

.

[

3v!D

S. P. Weise, Section Chief

Date Signed

Division of Reactor Projects

Sl'MMARY

Scope:

This routine, announced inspection involved 325 resident inspector-hours

onsite in the areas of: operational safety verification including operations

performance, system lineups, radiation protection, security and housekeeping

inspections; surveillance and maintenance observations; review of previous

inspection findings; followup of events; review of licensee identified items;

Engineered Safety Feature; and review of inspector followup items.

Results:

One violation was identified - Failure to follow procedure during a

test of the Control Room Chlorine Detection System (paragraph 10).

g1110226851030

ADOCK 05000327

0

PDR

.

.

REPORT DETAILS

1.

Licensee Employees

Persons Contacted

H. L. Abercrombie, Site Director

  • P. R. Wallace, Plant Manager

L. M. Nobles, Operations and Engineering Superintendent

  • B. M. Patterson, Maintenance Superintendent
  • J. M. Anthony, Operations Group Supervisor
  • D. C. Craven, Quality Assurance Supervisor

D. E. Crawley, Health Physics Supervisor

J. L. Hamilton, Quality Engineering Supervisor

  • G. B. Kirk, Compliance Supervisor

D. H. Tullis, Mechanical Maintenance Group Supervisor

  • R. C. Birchell, Compliance Engineer
  • C. L. Wilson, Nuclear Engineer
  • C. E. Bosley, QA Evaluator, Division of QA, Quality Assurance Branch
  • D. L. Cowart, Quality Surveillance Supervisor

Other licensee employees contacted included technicians, operators, shift

engineers, security force members, engineers and maintenance personnel.

  • Attended exit interview

2.

Exit Interview

The inspection scope and findings were summarized with the Plant Manager and

members of his staff on October 7, 1985. A violation described in paragraph

10 and a second example of a previous violation described in paragraph 6

were discussed.

The licensee acknowledged the inspection findings and did

not identify as proprietary any material reviewed by the inspectors during

this inspection.

During the reporting period, frequent discussions were

held with the Site Director, Plant Mannger and his assistants concerning

inspection findings.

At no time during the inspection was written material

provided to the licensee by the inspector.

3.

Licensee Action on Previous Inspection Findings (92702)

(Closed) Violation 328/83-16-02.

The licensee's response of October 7,

1983, was reviewed and the indicated corrective actions were audited.

The

licensee conducted Mechanical Maintenance Section training on the importance

of adhering to mandatory Quality Assurance procedural hold points.

The

licensee's corrective actions are considered complete.

.

'

2

,

(Closed) Violation 328/84-21-05.

The licensee's response of September 20,

1984, was reviewed and the indicated corrective actions were audited. The

licensee conducted training on the requirement for the independent verifi-

cation of processed hold orders.

In addition, administrative action was

taken with respect to the involved individuals.

The licensee's corrective

actions are considered complete.

(Closed) Violation 328/83-31-03.

The licensee's response of March 15,

1984, was reviewed and the indicated corrective actions were audited. The

licensee conducted training on a variety of operational subjects involved

with this violation.

Surveillance Instructions were revised to include the

methods and details of valve locking. The licensee's corrective actions are

considered complete.

(Closed) Violation 328/83-31-04.

The licensee's response of March 15,

1984, was reviewed and the indicated corrective actions were audited. The

licensee amended its maintenance procedures to require that both Assistant

Shift Engineers be required to sign prior to the removal from service of any

inverter, 6900-volt shutdown board or 480-volt shutdown board.

In addition,

this topic was included in licensed operator requalification training. The

licensee's corrective actions are considered complete.

!

(Closed) Unresolved Item 327, 328/85-26-04.

Corrective maintenance was

reviewed on containment isolation valves 2-67-580A through D.

Two of these

valves were examined by the inspector after being cut from the Essential Raw

y

Cooling Water system and disassembled.

The valves were badly corroded and

the internal flapper arm pins were out of round.

The seating surface was

worn, but there was no indication of foreign materials within the valves.

These valves were retested and determined to be operable.

The licensee

,

updated their maintenance history associated with these components.

This

item is considered to be closed.

4.

Unresolved Items

No unresolved items were identified during this,it.spection.

5.

Operational Safety Verification (71707)

a.

Plant Tours

The inspectors observed control room operations, reviewed applicable

logs, conducted discussions with control room operators, observed shift

turnovers, and confirmed operability of instrumentation.

The

inspectors verified the operability of selected emergency systems,

reviewed tagout records, verified compliance with Technical

Specification (TS) Limiting Conditions for Operation (LCO) and verified

return to service of affected components. The inspectors verified that

maintenance work orders had been submitted as required and that

followup activities and prioritization of work was accomplished by the

licensee.

-

-

-

-

-

.

.

3

'

Tours of the diesel generator, auxiliary, control, and turbine

buildings were conducted to observe plant equipment conditions,

including potential fire hazards, fluid leaks, and excessive vibrations

and plant housekeeping / cleanliness conditions.

The inspectors walked down accessible portions of the following

safety-related systems on l' nit 1 and l' nit 2 to verify operability and

proper valve alignment:

Residual Heat Removal System (l' nits 1 and 2)

Charging Pump Flowpath (l' nits 1 and 2)

Diesel Generators (l' nits 1 and 2)

Control Room Ventilation Chlorine Detection System (Common)

b.

Security

During the course of the inspection, observations relative to protected

and vital area security were made, including access controls, boundary

integrity, search, escort, and badging.

No violations or deviations

were identified.

c.

Radiation Protection

The inspectors observed Health Physics (HP) practices and verified

implementation of radiation protection control.

On a regular basis,

radiation work pennits (RWPs) were reviewed and specific work

activities were monitored to assure the activities were being conducted

in accordance with applicable RWPs.

Selected radiation protection

instruments were verified operable and calibration frequencies were

reviewed.

On September 26, 1985, the inspector observed workers frisking out of a

regulated zone, on EL690 at the hallway laading to the hot machine

shop.

The licensee's procedure, Radiological Control Instruction,

RCI-1, Radiological Hygiene Control, requires frisking of the hands and

feet with a counter provided at the ev.it to the area. One maintenance

section worker exiting the regulated area frisked his feet, but did not

frisk his hands.

Failure to follow the radiation protection procedure

for frisking when exiting a regulated zone is a violation; however,

since the licensee was in the process of implementing corrective action

for a similar violation (327, 328/85-26-03), involving the failure to

frisk out of a contaminated zone, this incident constitutes a further

example of that violation.

Corrective action for this incident included the assignment of an HP

technician to the maintenance section to provide additional training

and assure awareness of Health Physics (HP) procedures and practices.

This training will be completed by January 3,1986.- Implementation of

these actions are intended to prevent recurrence of similar incidents.

. - -

-

- .

.

4

.

Current audits conducted by the licensee indicate a substantial

improvement in overall compliance with HP requirements during the past

year, and adequacy of corrective actions will be verified by TVA

through future audits.

In addition, the inspector noted that individuals were picking up the

hand held monitor without frisking the hand used to pick up the

monitor. This is a poor health physics practice and was brought to the

attention of plant management.

The inspector will continue to monitor

the frisk out process to assure proper controls are in place.

6.

Engineered Safety Features Walkdown (71710)

The inspectors verified operability of the Component Cooling Water System

(CCS) on Units 1 and 2 by performing a partial walkdown of the accessible

portions of the system.

The remainder of the walkdown on this system will

be completed in the next inspection period.

The following specifics were

reviewed and/or observed as appropriate:

a.

that the licensee's system lineup procedures matched plant drawings and

the as-built configuration;

b.

that equipment conditions were satisfactory and items that might

degrade performance were identified and evaluated;

c.

with assistance from licensee personnel, the interior of the breakers

and electrical or instrumentation cabinets- were inspected for debris,

loose material, jumpers, evidence of rodents, etc.;

d.

that instrumentation was properly valved in and functioning and

calibration dates were appropriate;

e.

that valves were in their proper positions, breaker alignment was

correct, power was available, and valves were locked as required; and

f.

local and remote instrumentation was compared, and remote instrumen-

tation was functional.

,

During the tour, the inspectors identified several discrepancies:

housekeeping in several areas was marginal

-

new piping segments were attached to existing fire protection- piping

-

using masking tape

valve labelling and location identifier accuracy

-

conduit degradation

-

This was brought to the attention of the licensee. The licensee attributed

the problem to outage work activities.

.

.

5

.

The inspector reviewed housekeeping logs kept by the licensee in accordance

with procedure SQA-66, Plant Housekeeping.

TVA management housekeeping

tours are performed approximately monthly.

Ditcrepant areas identified

during tours are rechecked to assure corrective action has been taken. The

inspectors also reviewed Operations Section Letter OSLA-99, Auxiliary l' nit

Operator (Al'0) Duties, and determined that Al'Os are required to identify

housekeeping problems.

The inspectors will review plant housekeeping and

licensee implementation of SQA-66 and OSLA-99 during the remainder of the

outage.

Followu

on this issue is an Inspector Followup Item

(327, 328/85-32-02) p

.

No violations or deviations were identified.

7.

Monthly Surveillance Observations (61726)

The inspectors observed TS required surveillance testing and verified that

testing was performed in accordance with adequate procedures; that test

instrumentation was calibrated; that Limiting Conditions for Operation were

met; that test results met acceptance criteria requirements and were

reviewed by personnel other that the individual directing the test; that

deficiencies were identified, as appropriate, and that any deficiencies

identified during the testing were properly reviewed and resolved by

management personnel; and that system restoration was adequate.

For the

completed tests, the inspector verified that testing frequencies were met

and tests were performed by qualified individuals.

The inspector witnessed / reviewed portions of the following surveillance test

activities:

SI-688.2

Functional Test for Accident Radi nion Monitor System

IMI-99

Reactor Protection System RT 11.6 & 11.8, Response Time

Test of Delta T/Tavg Channels 2 and 4

SI-40

Centrifugal Charging Pump

SMI-0-90-1

High Dose Rate Calibration for Containment High Range

Accident Monitors

No violations or deviations were identified in this area.

8.

MonthlyMaintenanceObservations(62703)

a.

Station maintenance activities of safety-related systems and components

were observed / reviewed to ascertain that they were conducted in

accordance with approved procedures, regulatory guides, industry codes

and standards, and in conformance with TS.

,

.

6

.

The following items were considered during this review: LCOs were met

while components or systems were removed from service; redundant

components were operable; approvals were obtained prior to initiating

the work; activities were accomplished using approved procedures and

were inspected as applicable; procedures used were adequate to control

the activity; troubleshooting activities were controlled and the repair

record accurately reflected what actually took place; functiona)

testing and/or calibrations were perfomed prior to returning

components or systems to service; quality control records were

-

maintained; activities were accomplished by qualified personnel; parts

and materials used were properly certified; radiological controls were

implemented; QC hold points were established where required and were

observed; fire prevention controls were implemented; outside contractor

force activities were controlled in accordance with the approved

Quality Assurance (QA) program; and housekeeping was actively pursued.

'

b.

During the l' nit I refueling outage the inspector observed portions of

steam generator maintenance and audited documentation of the work

'

activities involving the cleaning of the secondary side by sludge

lancing, primary side eddy current examinations and plugging of the

Row I and other tubes for all four steam generators. - The following

procedures were reviewed / observed by the inspectors:

Radiation Work Permit:

02-1-85112

Maintenance Requests:

A549689,

A549690, A549692,

AS49528,

A549691, A533110,

A301950,

A302397, A302398,

4

A302399

x

Vendor Standard:

CFS-STD-020, Steam Generator

Tube Sheet Sludge Re1 oval

'

Maintenance Instructions:

MI

3.7,

Preparation

for

Performance of . and Recovery

From Steam Generator Sludge

Lancing

MI 3.1, Removal and Installa-

tion of Steam Genera' tor' Primary

Manway Cover, l' nits 1 an_d 2

MI

3'. 3 ,

Steam Generator

Secondary Side Inspection

m3

MI 3.4, Breaching Penetration

X-54 Without Breaching the

ABSCE for Eddy Current Testing,

"

Helium Leak Testing, Sludge

Lancing and Other Purposes

w

1

'

s

.

.

m

- . . .

.

,

-t

.

7

.

MI

3.2, Method of Plugging

Steam Generator Tubes

Standard Practices:

SQA 119, l'nreviewed Safety

Question Determination (l'SQD)

SQM 001,Sequoyah Nuclear Plant

Maintenance Program

l'SQD Documentation:

l'SQD 85-0998, involving use of

a special eddy current test

probe for Row 1 tubes.

d

l'SQD

85-0999,

involving

performance of worker platform

training.

ASME Code Document:

ASME Code Section XI, 1977

amended by Summer 1978 addenda

<

The licensee began steam generator (SG) maintenance with a visual

examination of the secondary side using a fiberscope to determine the

condition of the steam generators.

Video recordings were made of the

in:;pection.

It was determined that sludge lancing was needed to remove

sediment on the secondary side at the tube sheet.

The inspector

observed sludge lancing activities, which involved a newly developed

technique.

All four SGs were sludge lanced between three to four sweeps each with

a total of approximately 1750 pounds of sludge removed. This averaged

over 400 pounds'per SG.

Fiberscopic examinations after completion

indicated that the SGs were essentially clean.

The new technique was

found to be more effective for sludge removal.

The licensee stated that the sludge removed consisted of approximately

70% iron and 30% copper.

The licensee is also replacing the main

feedwater heaters and the moisture separator reheater tube bundles

during this outage to eliminate copper from the secondary system. The

,

licensee recovered two small pieces of a drill bit from one steam

generator.

No damage was attributed to this material.

The licensee

also had to recover parts of a camera that came loose during a

fiberscopic exam.

s

"

The licensee inspected 100% of the tubes on all four SGs using eddy

current probes, with the exception of the l'-bend portion of the Row 2

tubes.

This exception was made due to the difficulty associated with

an inspection of these lf-bends and no industry wide history of failures

\\

in the Row 2 l'-bend area.

-

4

\\

8e

____

.

8

.

.The eddy current exams identified .that four Row 1 tubes had indications

of corrosive cracking.

Although the indications were minor and could

riot be categorized as to depth, the licensee decided to plug the Row 1

tubes in all four steam generators to ensure that cracks did not

develop in these tubes. The licensee will evaluate the indications and

can later remove the Row 1 tube plugs as desired.

The licensee is

evaluating a stress relieving process which employs electric heaters to

remove induced thermal stresses as a part of the process that could

return the plugged Row 1 tubes to service. Three other tubes with

indications of less than 30% through wall were plugged. At the end of

this inspection period, the licensee was still evaluating the eddy

current data and may elect to plug additional tubes.

The licensee also utilized a new device for tube plugging developed by

Combustion Engineering.

The device was installed in the steam

. generator and manipulated remotely to install *;ube plugs.

The device

is capable of employing a magazine which can be loaded with a number of

plugs at one time reducing entries into the SG.

The device offered

reductions in the dose and time associated with SG tube plugging. The

licensee estimated that the dose - associated with the plugging

operations during this outage was reduced from approximately 200 rem to

50 rem.

c.

Replacement of the 1-A Centrifugal Charging Pump mechanical seals was

observed. The following documents were reviewed / observed in part:

,

Maintenance Instruction (MI) 6.4 - Removal, Inspection and

Replacement of Centrifugal Charging Pump Seals

Surveillance Instruction (SI) 40 - Centrifugal Charging Pump

Maintenance Request A529430

'

~

During the performance of the seal replacement, the technicians

identified that an 0-ring, issued from Power Stores, was not the size

specified by the vendor.

This appeared to be due to mispackaging of

the 0-ring by the vendor, since the shipping package and the receipt

documentation matched the material identification numbers specified by

the vendor.

A new 0-ring was requisitioned to replace the defective

one,

d.

During this outage period, preventive maintenance was conducted on both

l' nit 1 and l' nit 2 Reactor Coolant Pumps (RCP).

One activity involved

an evaluation of the breakaway torque associated with each RCP motor.

Maintenance Request A529848 was used to obtain the breakaway torque for

each RCP motor and the data was evaluated against vendor's acceptance

criteria.

The inspector observed the performance of the preventive

maintenance on the l' nit 2 loop 3 RCP with no discrepancies . identified.

The licensee later identified the t' nit 1 loop 2 RCP as not meeting the

acceptance criteria and disassembled the subject pump to perform

corrective maintenance.

\\

-

,

.

9

..

No violations or deviations were identified.

9.

Licensee Event Report (LER) Followup (92700)

The following LER's were reviewed and closed. The inspector verified that:

reporting requirements had been met; causes had been identified; corrective

actions appeared appropriate; generic applicability had been considered; the

LER forms were complete; the licensee had reviewed the event; no unreviewed

safety questions were involved; and violations of regulations or TS condi-

tions had been identified.

a.

LER Unit 1

327/82115

Inoperable Upper Containment Personnel Airlock

(Revision 1)

327/83093

Inoperable Condenser Vacuum Flow Rate Monitor

(Revision 1)

327/83100

Automatic Control Valve Declared Inoperable

327/83165

Primary Containment Internal Pressure (Revision 1)

,

327/83168

1 A-A Diesel Generator (DG) Failed to Start

327/83177

2 A-A DG Failed to Trip

327/83183

Limitorque Operator Limit Switch Failed

327/83186

1 A-A DG Trip

.

327/84011

Control Habitability System (Revision 1)

327/84034

No Flow Indication on 'B'

Essential Raw Cooling Water

Header

327/84045

Inoperable Auxiliary Air Compressors (Revision 1)-

327/85003

Surveillance Interval Exceeded

327/85022

Failure to Complete Hourly Fire Watch

327/85024

Failure to Complete Hourly Fire Watch

'327/85025-

Failure to Obtain a Noble Gas Sample

327/85028

Failure to Complete Hourly Fire Watch

327/85031

Auxiliary Building Isolation

327/85033.

Main Control Room Isolation

-

.

-

- .-

-

.

..

.

10

,

327/85035

Emergency Diesel Generator Start

327/85036

Failure to Complete Hourly Fire Watch

b.

LER l' nit 2

328/84004

Loss of 6900 Volt l' nit Board

328/84020

Inadvertent Safety Inje: tion (Revision 1)

10. EventFollowup(93702,62703,61726)

a.

On August 27, 1985 an engineered safety feature actuation occurred as a

result of a Train B main control room isolation signal.

The main

control room isolation occurred during the performance of Surveillance

Instruction (SI) 240, Functional Test of Control Room Air Intake

Chlorine Detection System.

Step 4.4 of SI 240 requires the technician

-

to place switch HS-43-205B in the test position prior to introducing

chlorine fumes into the detection system.

The technician performing

the surveillance and the assistant observing his actions failed to

implement step 4.4 of SI 240, and as a consequence, initiated an

engineered safety feature actuation when the chlorine fumes were

introduced into the. detection system. This failure to follow procedure

constitutes a violation (327, 328/85-32-01). The technician placed the

subject switch in the test position after becoming aware of the main

control room isolation. He then continued the surveillance, initialing

Section 4.4 of Appendix B to SI 240 and reapplying the chlorine

standard to the detection system, without informing appropriate

supervisory or operations personnel.

As a result of previous Inspector Followup Item (327, 328/85-26-07),

the licensee committed to provide formal instructions to employees on

actions to be taken when the employee fails to follow procedures. The

licensee issued a maintenance notice entitled, Your Responsibilities

in Following Instructions,

to all maintenance employees on or about

July 22, 1985.

Based on inspector review, a majority of the mainte-

nance technicians appear to have received the notice.

The technician

that was involved in the above failure to follow procedure was tem-

porarily assigned to the TVA training center during the period that

the notice was issued and therefore was not . fully aware of its

contents.

Inspector Followup Item 327, 328/85-26-07 will-remain open

pending further NRC assessment.-

b.

On' September 27, 1985, a Combustion Engineering employee abraded his

plastic ~ gloves and scraped his hand on the SG tube sheet while per-

forming steam generator tube plugging activities.

The individual

_

was removed from the area for decontamination.

Initial contamination

was approximately 1,000 cpm. The licensee decontaminated the hand to a

level of 400 cpm.

At the advice of an offsite physician, the licensee

-

,

.

11

..

decided to take the individual to the hospital for further treatment.

The licensee declared an l'nusual Event in accordance with IP-1,

Emergency Plan Classification Logic, and IP-2, Notification of l'nusual

Event, in anticipation of transporting a contaminated person to an

offsite medical facility.

The individual, however, refused to be

transported offsite and continued decontamination efforts.

He

successfully reduced the contamination to below acceptable limits, and

the t'nusual Event was terminated.

Reports of the incident were made to

the NRC and the State of Tennessee, as required.

'll.

Inspector Followup Items (92701)

Based on inspection activities in the affected functional areas the

.following items were determined to require no additional specific followup

and are closed.

328/84-21-04

328/84-31-05

328/84-31-06

327/84-11-03

327/83-23-04