ENS 49600: Difference between revisions

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| event date = 12/02/2013 17:58 MST
| event date = 12/02/2013 17:58 MST
| last update date = 12/02/2013
| last update date = 12/02/2013
| title = Automatic Reactor Trip Following The Loss Of The 1A Reactor Coolant Pump
| title = Automatic Reactor Trip Following the Loss of the 1A Reactor Coolant Pump
| event text = The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73.
| event text = The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73.
On December 2, 2013, at approximately 1758 Mountain Standard Time (MST), the Palo Verde Nuclear Generating Station (PVNGS) Unit 2 control room received reactor protection system alarms for low departure from nucleate boiling ratio and an automatic reactor trip occurred. Prior to the reactor trip, Unit 2 was operating normally at 100% power. Plant operators entered the emergency operations procedures and diagnosed an uncomplicated reactor trip but noted the 1A reactor coolant pump (RCP) was not running. All CEAs fully inserted into the core. Following the reactor trip, indications on the train A logarithmic (log) power nuclear instrument initially responded normally but then did not trend as expected. All other nuclear instruments responded normally and the train A log power channel was declared inoperable and technical specification limiting conditions for operation 3.3.10 and 3.3.11 were entered. No emergency classification was required per the PVNGS Emergency Plan.
On December 2, 2013, at approximately 1758 Mountain Standard Time (MST), the Palo Verde Nuclear Generating Station (PVNGS) Unit 2 control room received reactor protection system alarms for low departure from nucleate boiling ratio and an automatic reactor trip occurred. Prior to the reactor trip, Unit 2 was operating normally at 100% power. Plant operators entered the emergency operations procedures and diagnosed an uncomplicated reactor trip but noted the 1A reactor coolant pump (RCP) was not running. All CEAs fully inserted into the core. Following the reactor trip, indications on the train A logarithmic (log) power nuclear instrument initially responded normally but then did not trend as expected. All other nuclear instruments responded normally and the train A log power channel was declared inoperable and technical specification limiting conditions for operation 3.3.10 and 3.3.11 were entered. No emergency classification was required per the PVNGS Emergency Plan.

Latest revision as of 21:52, 1 March 2018

ENS 49600 +/-
Where
Palo Verde Arizona Public Service icon.png
Arizona (NRC Region 4)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation
LER: 05000529/LER-2013-002
Time - Person (Reporting Time:+-1.53 h-0.0638 days <br />-0.00911 weeks <br />-0.0021 months <br />)
Opened: Allan Briese
23:26 Dec 2, 2013
NRC Officer: Steve Sandin
Last Updated: Dec 2, 2013
49600 - NRC Website
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