ENS 53091: Difference between revisions

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| event date = 11/25/2017 20:25 CST
| event date = 11/25/2017 20:25 CST
| last update date = 11/26/2017
| last update date = 11/26/2017
| title = Manual Reactor Trip Due To Loss Of Main Feed Water
| title = Manual Reactor Trip Due to Loss of Main Feed Water
| event text = At time 2025 [CST] on 11/25/17, Unit 2 reactor was manually tripped due to a loss of all Main Feedwater. Operators observed both Main Feed Pumps tripped and SG [Steam Generator] levels decreasing, resulting in the direction for a manual reactor trip. The reactor trip actuated a turbine trip, both Motor Driven Auxiliary Feedwater Pumps started on the loss of both Main Feed Pumps, and Steam Generator Lo Lo levels started the Turbine Driven Auxiliary Feedwater Pump. All systems responded as expected. There was no work in progress at the time of the incident.  
| event text = At time 2025 [CST] on 11/25/17, Unit 2 reactor was manually tripped due to a loss of all Main Feedwater. Operators observed both Main Feed Pumps tripped and SG [Steam Generator] levels decreasing, resulting in the direction for a manual reactor trip. The reactor trip actuated a turbine trip, both Motor Driven Auxiliary Feedwater Pumps started on the loss of both Main Feed Pumps, and Steam Generator Lo Lo levels started the Turbine Driven Auxiliary Feedwater Pump. All systems responded as expected. There was no work in progress at the time of the incident.  
Currently Unit 2 is being maintained in Hot Standby (Mode 3) in accordance with Integrated Plant Operating Procedure IP0-0078 and the Emergency Response Guideline Procedure Network has been exited. Decay Heat is being rejected to the Main Condenser via Steam Dump Valves.
Currently Unit 2 is being maintained in Hot Standby (Mode 3) in accordance with Integrated Plant Operating Procedure IP0-0078 and the Emergency Response Guideline Procedure Network has been exited. Decay Heat is being rejected to the Main Condenser via Steam Dump Valves.

Latest revision as of 20:41, 1 March 2018

ENS 53091 +/-
Where
Comanche Peak Luminant icon.png
Texas (NRC Region 4)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-1.82 h-0.0758 days <br />-0.0108 weeks <br />-0.00249 months <br />)
Opened: John Alexander
00:36 Nov 26, 2017
NRC Officer: Andrew Waugh
Last Updated: Nov 26, 2017
53091 - NRC Website
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