ENS 52898
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ENS Event | |
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16:24 Aug 11, 2017 | |
Title | Comanche Peak Automatic Turbine Trip from 10 Percent Power |
Event Description | At 1124 CDT on 11 August 2017, CPNPP [Comanche Peak Nuclear Power Plant] Unit 2 experienced an automatic turbine trip and trip of both main feedwater pumps on high steam generator water level (P-14, 81.5 percent level) in steam generator 2-02. Following the turbine trip, the auxiliary feedwater system actuated as required. The plant was stabilized at 2-3 percent reactor power with auxiliary feedwater feeding all steam generators with all levels within their normal bands.
The cause of the high steam generator level appears to be a mechanical malfunction of steam generator 2-02 flow control valve bypass valve 2-LV-2163 (SG 2-02 FW BYP CTRL VLV) to close when demanded. Troubleshooting and repair of 2-LV-2163 is in progress. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) for an actuation of auxiliary feedwater. The NRC Resident Inspector has been notified. |
Where | |
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Comanche Peak Texas (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-0.2 h-0.00833 days <br />-0.00119 weeks <br />-2.7396e-4 months <br />) | |
Opened: | Jonathan Bain 16:12 Aug 11, 2017 |
NRC Officer: | Jeff Herrera |
Last Updated: | Aug 11, 2017 |
52898 - NRC Website
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WEEKMONTHYEARENS 570332024-03-17T20:15:00017 March 2024 20:15:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Main Feedwater Pump Trip ENS 570242024-03-12T13:16:00012 March 2024 13:16:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 565802023-06-16T23:32:00016 June 2023 23:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to LO-LO Steam Generator Level ENS 560912022-09-06T04:45:0006 September 2022 04:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 540642019-05-15T02:51:00015 May 2019 02:51:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Voltage Transient Due to Loss of Offsite Switchyard ENS 539062019-03-02T09:17:0002 March 2019 09:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Feedwater Isolation Valve Closure ENS 537672018-12-03T06:00:0003 December 2018 06:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of Blackout Sequencers Due to Loss of One Offsite Power Source ENS 535502018-08-13T05:00:00013 August 2018 05:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Generator Lockout ENS 530912017-11-26T02:25:00026 November 2017 02:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Main Feed Water ENS 529452017-09-02T02:40:0002 September 2017 02:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Two Dropped Rods ENS 528982017-08-11T16:24:00011 August 2017 16:24:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Comanche Peak Automatic Turbine Trip from 10 Percent Power ENS 514442015-10-03T15:00:0003 October 2015 15:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip During Shutdown for a Refueling Outage ENS 497432014-01-18T14:40:00018 January 2014 14:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Turbine Trip ENS 496062013-12-04T19:50:0004 December 2013 19:50:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event - Loss of Startup Power Due to a Cut Cable ENS 494972013-11-02T02:47:0002 November 2013 02:47:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip During Solid State Protection System Testing ENS 485142012-11-17T16:23:00017 November 2012 16:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Steam Generator Water Level ENS 484752012-11-02T06:42:0002 November 2012 06:42:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to High Reactor Coolant Pump Motor Bearing Temperature ENS 468632011-05-19T19:07:00019 May 2011 19:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip After a Main Condenser Tube Leak ENS 467482011-04-13T03:15:00013 April 2011 03:15:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Esf Actuation Following Loss of a Safeguard Bus During Edg Testing ENS 458332010-04-12T12:21:00012 April 2010 12:21:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of Blackout Sequencers Due to Loss of One Offsite Power Source ENS 456172010-01-09T16:28:0009 January 2010 16:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip on Sudden Pressure in Output Transformer ENS 440672008-03-16T16:37:00016 March 2008 16:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Broken Sensing Line ENS 429452006-10-29T21:20:00029 October 2006 21:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Trip Due to Lowering Steam Generator Level ENS 429372006-10-27T08:08:00027 October 2006 08:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Loss of Both Main Feed Pumps ENS 414322005-02-23T07:53:00023 February 2005 07:53:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auxiliary Feedwater Action Following Momentary Power Interruption ENS 411342004-10-19T10:28:00019 October 2004 10:28:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Normal Power Supply to "2E" Switchgear Resulted in Afw Autostart ENS 404062003-12-22T14:27:00022 December 2003 14:27:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Main Turbine Trip 2024-03-17T20:15:00 | |
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