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OPERATING DATA REPORT DutMET NO. 50-341 | OPERATING DATA REPORT DutMET NO. 50-341 COMPLETED BY L.P.Bregni DATE December 12, 1986 TELEPHONE (313)586-5313 OPEHATING STATUS 1. | ||
DATE | UNIT NAME: | ||
OPEHATING STATUS | Fermi 2 l Notes l | ||
2. | |||
REPORTING PERIOD: November-l l | |||
3 LICENSED THERMAL POWER ( pt): | |||
3292 l | |||
l 4. | |||
NAMEPLATE RATING (GROSS MWe): | |||
LAST REPORT, GIVE REASONS: | 1215 l | ||
l 5. | |||
: 10. REASONS FOR RESTRICTION, IF ANY: Fermi 2 is in the startup test phase and is currently authorized to operate not in excess of 20% of rated thermal power. | DESIGN ELECT RATING (Net We): 1093 1 | ||
THIS MONTH | l 4 | ||
: 11. HRS IN REPORTING PERIOD | - 6.. MAX DEPENDABLE CAP (GROSS We): | ||
: 12. HRS REACTOR WAS CRITICAL | l l | ||
: 13. REACTOR RESERVE SHUTDOWN HRS | 7 MAX DEPENDABLE CAP (Net MWE): | ||
: 14. HOURS GENERATOR ON-LINE | l l | ||
: 15. UNIT RESERVE SHUTDOWN HOURS | l 8. | ||
: 16. GROSS THERMAL ENERGY GEN (MWH) | IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS: | ||
: 17. GROSS ELECT ENERGY GEN (WH) | None 9. | ||
: 18. NET ELECT ENERGY GEN (MWH) | POWER LEVEL 10 NHICH RESTRICTED, IF ANY (MWe Net): | ||
: 19. UNIT SERVICE FACTOR | 218.6 | ||
: 20. UNIT AVAILABILITY FACTOR | : 10. REASONS FOR RESTRICTION, IF ANY: Fermi 2 is in the startup test phase and is currently authorized to operate not in excess of 20% of rated thermal power. | ||
: 21. UNIT CAP FACTOR (USING MDC NET) | (Ref. J. G. Keppler letter of September-12, 1986) | ||
: 24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, DURATION OF EACH): NONE | THIS MONTH YR TO DATE CUMULATIVE | ||
: 11. HRS IN REPORTING PERIOD 720 1,689.9 1,689 9 | |||
: 12. HRS REACTOR WAS CRITICAL 159.1 560.9 560 9 | |||
: 13. REACTOR RESERVE SHUTDOWN HRS 0 | |||
0 0 | |||
: 14. HOURS GENERATOR ON-LINE 26.0 95.8 95.8 | |||
: 15. UNIT RESERVE SHUTDOWN HOURS 0 | |||
0 0 | |||
: 16. GROSS THERMAL ENERGY GEN (MWH) 36,096 167,568 167,568- | |||
: 17. GROSS ELECT ENERGY GEN (WH) 2,020 7,640 7,640 | |||
: 18. NET ELECT ENERGY GEN (MWH) | |||
-6,723 | |||
-20,907- | |||
-20,907 | |||
: 19. UNIT SERVICE FACTOR N/A N/A N/A | |||
: 20. UNIT AVAILABILITY FACTOR N/A N/A N/A | |||
: 21. UNIT CAP FACTOR (USING MDC NET) | |||
N/A N/A N/A l | |||
: 22. 'JNIT CAP FACTOR (USING DER NET) | |||
N/A N/A N/A i | |||
: 23. UNIT FORCED OUTAGE RATE N/A N/A N/A | |||
: 24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, DURATION OF EACH): NONE s | |||
: 25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: 12/16/86 | : 25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: 12/16/86 | ||
: 26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION): | : 26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION): | ||
FORECAST | FORECAST ACHIEVED INITIAL CRITICALITY 06/20/85 06/21/85 i | ||
INITIAL CRITICALITY | INITIAL ELECTRICITY 10/01/86 09/21/86 l | ||
COMMERCIAL OPERATION 05/01/87 | |||
'8703040025 B61212 | |||
~ | |||
PDR | ~ | ||
PDR ADOCK 05000341 | |||
'{( | |||
~ | |||
AVERAGE DAILY UNIT POWER LEVEL a | AVERAGE DAILY UNIT POWER LEVEL a | ||
DOCKET NO. | DOCKET NO. | ||
UNIT | 50-341 ___ | ||
DATE | UNIT FERMI 2 DATE December 12,_1986 | ||
. COMPLETED BY L. P. Bregni TELEPHONE (313) 586-5313 MONTH November DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) | |||
9 | (MWe-Net) 1 75.1 17 3 | ||
2' 75 18 0 | |||
3 0 | |||
14 | 19 0 | ||
4-0 20 0 | |||
S 0 | |||
21 0 | |||
6 0 | |||
22 0 | |||
7 0 | |||
23 0 | |||
8 0 | |||
24 0-l i | |||
9 0-25 - | |||
0 l | |||
10 0 | |||
26 0 | |||
l 11 0 | |||
27 0 | |||
l l | |||
12 0 | |||
28 0 | |||
l | |||
.13 0 | |||
29 0 | |||
14 0 | |||
30 0 | |||
15 0 | |||
31 N/A 16 0 | |||
l | |||
UNIT SHUTDOWNS AND POWER REDUCTIONS' DOCKET NO. 50-341 | UNIT SHUTDOWNS AND POWER REDUCTIONS' DOCKET NO. | ||
TELEPHONE | 50-341 DATE | ||
NO. | . December 12 1996 UNIT'NAME Fermi 2-COMPLETED BY' L. | ||
(3) 86-06 | P. | ||
Condensate Storage Tank, | Broon t - | ||
TELEPHONE (313)586-5313 REPORT MONTH November I-METHOD OF LER SYS COMP CAUSE & CORRECTIVE NO. | |||
E - OPERATOR TRAINING & LICENSE EXAMINATION | DATE TYPE DUR REASON SHUTTING DOWN NO. | ||
H - OTHER (EXPLAIN) | CODE CODE ACTION TO PREVENT (1) | ||
(HRS) | |||
(2) | |||
THE REACTOR (4) | |||
(5) | |||
RECURRLNCE (3) 86-06 861107 F | |||
560.9 A | |||
2 N/A HC HTEXCHD Shutdown to repair the cause of excessive air.in-leakage into the condenser. Outage scope has been expanded to include installation of I new relief valves to prevent future overpressurization of the condensate return line. | |||
On November 17, 1986 overpressurization of thi s -. l i ne caused an expansion joint to rupture and damaged a penetration in the | |||
] | |||
Condensate Storage Tank, l | |||
d I | |||
(1) F: FORCED (2) REASON: | |||
(3) METHOD: | |||
(4) EXHIBIT G - INSTRUCTIOh5 S: SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM ENTRY SHEETS FOk LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM EVENT REPORT (LER) FILL D - REGULATORY RESTRICTION 4 - CONTINUED (NUREG-0161)' | |||
E - OPERATOR TRAINING & LICENSE EXAMINATION 5 - REDUCED LOAD F - ADMINISTRATIVE 9 - OTHER G.- OPERATIONAL ERROR (EXPLAIN) | |||
H - OTHER (EXPLAIN) | |||
(5) EXHIBIT I - SAME SOURCE O}} | |||
Latest revision as of 06:42, 4 December 2024
| ML20212C914 | |
| Person / Time | |
|---|---|
| Site: | Fermi |
| Issue date: | 11/30/1986 |
| From: | Bregni L DETROIT EDISON CO. |
| To: | |
| Shared Package | |
| ML20211Q132 | List: |
| References | |
| NUDOCS 8703040025 | |
| Download: ML20212C914 (3) | |
Text
_
OPERATING DATA REPORT DutMET NO. 50-341 COMPLETED BY L.P.Bregni DATE December 12, 1986 TELEPHONE (313)586-5313 OPEHATING STATUS 1.
UNIT NAME:
Fermi 2 l Notes l
2.
REPORTING PERIOD: November-l l
3 LICENSED THERMAL POWER ( pt):
3292 l
l 4.
NAMEPLATE RATING (GROSS MWe):
1215 l
l 5.
DESIGN ELECT RATING (Net We): 1093 1
l 4
- 6.. MAX DEPENDABLE CAP (GROSS We):
l l
7 MAX DEPENDABLE CAP (Net MWE):
l l
l 8.
IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:
None 9.
POWER LEVEL 10 NHICH RESTRICTED, IF ANY (MWe Net):
218.6
- 10. REASONS FOR RESTRICTION, IF ANY: Fermi 2 is in the startup test phase and is currently authorized to operate not in excess of 20% of rated thermal power.
(Ref. J. G. Keppler letter of September-12, 1986)
THIS MONTH YR TO DATE CUMULATIVE
- 11. HRS IN REPORTING PERIOD 720 1,689.9 1,689 9
- 12. HRS REACTOR WAS CRITICAL 159.1 560.9 560 9
- 13. REACTOR RESERVE SHUTDOWN HRS 0
0 0
- 14. HOURS GENERATOR ON-LINE 26.0 95.8 95.8
- 15. UNIT RESERVE SHUTDOWN HOURS 0
0 0
- 16. GROSS THERMAL ENERGY GEN (MWH) 36,096 167,568 167,568-
- 17. GROSS ELECT ENERGY GEN (WH) 2,020 7,640 7,640
- 18. NET ELECT ENERGY GEN (MWH)
-6,723
-20,907-
-20,907
- 19. UNIT SERVICE FACTOR N/A N/A N/A
- 20. UNIT AVAILABILITY FACTOR N/A N/A N/A
N/A N/A N/A l
- 22. 'JNIT CAP FACTOR (USING DER NET)
N/A N/A N/A i
- 23. UNIT FORCED OUTAGE RATE N/A N/A N/A
- 24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, DURATION OF EACH): NONE s
- 25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: 12/16/86
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
FORECAST ACHIEVED INITIAL CRITICALITY 06/20/85 06/21/85 i
INITIAL ELECTRICITY 10/01/86 09/21/86 l
COMMERCIAL OPERATION 05/01/87
'8703040025 B61212
~
~
PDR ADOCK 05000341
'{(
~
AVERAGE DAILY UNIT POWER LEVEL a
DOCKET NO.
50-341 ___
UNIT FERMI 2 DATE December 12,_1986
. COMPLETED BY L. P. Bregni TELEPHONE (313) 586-5313 MONTH November DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 75.1 17 3
2' 75 18 0
3 0
19 0
4-0 20 0
S 0
21 0
6 0
22 0
7 0
23 0
8 0
24 0-l i
9 0-25 -
0 l
10 0
26 0
l 11 0
27 0
l l
12 0
28 0
l
.13 0
29 0
14 0
30 0
15 0
31 N/A 16 0
l
UNIT SHUTDOWNS AND POWER REDUCTIONS' DOCKET NO.
50-341 DATE
. December 12 1996 UNIT'NAME Fermi 2-COMPLETED BY' L.
P.
Broon t -
TELEPHONE (313)586-5313 REPORT MONTH November I-METHOD OF LER SYS COMP CAUSE & CORRECTIVE NO.
DATE TYPE DUR REASON SHUTTING DOWN NO.
CODE CODE ACTION TO PREVENT (1)
(HRS)
(2)
THE REACTOR (4)
(5)
RECURRLNCE (3) 86-06 861107 F
560.9 A
2 N/A HC HTEXCHD Shutdown to repair the cause of excessive air.in-leakage into the condenser. Outage scope has been expanded to include installation of I new relief valves to prevent future overpressurization of the condensate return line.
On November 17, 1986 overpressurization of thi s -. l i ne caused an expansion joint to rupture and damaged a penetration in the
]
Condensate Storage Tank, l
d I
(1) F: FORCED (2) REASON:
(3) METHOD:
(4) EXHIBIT G - INSTRUCTIOh5 S: SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM ENTRY SHEETS FOk LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM EVENT REPORT (LER) FILL D - REGULATORY RESTRICTION 4 - CONTINUED (NUREG-0161)'
E - OPERATOR TRAINING & LICENSE EXAMINATION 5 - REDUCED LOAD F - ADMINISTRATIVE 9 - OTHER G.- OPERATIONAL ERROR (EXPLAIN)
H - OTHER (EXPLAIN)
(5) EXHIBIT I - SAME SOURCE O