ML20212C914

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Monthly Operating Rept for Nov 1986
ML20212C914
Person / Time
Site: Fermi 
Issue date: 11/30/1986
From: Bregni L
DETROIT EDISON CO.
To:
Shared Package
ML20211Q132 List:
References
NUDOCS 8703040025
Download: ML20212C914 (3)


Text

_

OPERATING DATA REPORT DutMET NO. 50-341 COMPLETED BY L.P.Bregni DATE December 12, 1986 TELEPHONE (313)586-5313 OPEHATING STATUS 1.

UNIT NAME:

Fermi 2 l Notes l

2.

REPORTING PERIOD: November-l l

3 LICENSED THERMAL POWER ( pt):

3292 l

l 4.

NAMEPLATE RATING (GROSS MWe):

1215 l

l 5.

DESIGN ELECT RATING (Net We): 1093 1

l 4

- 6.. MAX DEPENDABLE CAP (GROSS We):

l l

7 MAX DEPENDABLE CAP (Net MWE):

l l

l 8.

IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:

None 9.

POWER LEVEL 10 NHICH RESTRICTED, IF ANY (MWe Net):

218.6

10. REASONS FOR RESTRICTION, IF ANY: Fermi 2 is in the startup test phase and is currently authorized to operate not in excess of 20% of rated thermal power.

(Ref. J. G. Keppler letter of September-12, 1986)

THIS MONTH YR TO DATE CUMULATIVE

11. HRS IN REPORTING PERIOD 720 1,689.9 1,689 9
12. HRS REACTOR WAS CRITICAL 159.1 560.9 560 9
13. REACTOR RESERVE SHUTDOWN HRS 0

0 0

14. HOURS GENERATOR ON-LINE 26.0 95.8 95.8
15. UNIT RESERVE SHUTDOWN HOURS 0

0 0

16. GROSS THERMAL ENERGY GEN (MWH) 36,096 167,568 167,568-
17. GROSS ELECT ENERGY GEN (WH) 2,020 7,640 7,640
18. NET ELECT ENERGY GEN (MWH)

-6,723

-20,907-

-20,907

19. UNIT SERVICE FACTOR N/A N/A N/A
20. UNIT AVAILABILITY FACTOR N/A N/A N/A
21. UNIT CAP FACTOR (USING MDC NET)

N/A N/A N/A l

22. 'JNIT CAP FACTOR (USING DER NET)

N/A N/A N/A i

23. UNIT FORCED OUTAGE RATE N/A N/A N/A
24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, DURATION OF EACH): NONE s
25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: 12/16/86
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

FORECAST ACHIEVED INITIAL CRITICALITY 06/20/85 06/21/85 i

INITIAL ELECTRICITY 10/01/86 09/21/86 l

COMMERCIAL OPERATION 05/01/87

'8703040025 B61212

~

~

PDR ADOCK 05000341

'{(

~

AVERAGE DAILY UNIT POWER LEVEL a

DOCKET NO.

50-341 ___

UNIT FERMI 2 DATE December 12,_1986

. COMPLETED BY L. P. Bregni TELEPHONE (313) 586-5313 MONTH November DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 75.1 17 3

2' 75 18 0

3 0

19 0

4-0 20 0

S 0

21 0

6 0

22 0

7 0

23 0

8 0

24 0-l i

9 0-25 -

0 l

10 0

26 0

l 11 0

27 0

l l

12 0

28 0

l

.13 0

29 0

14 0

30 0

15 0

31 N/A 16 0

l

UNIT SHUTDOWNS AND POWER REDUCTIONS' DOCKET NO.

50-341 DATE

. December 12 1996 UNIT'NAME Fermi 2-COMPLETED BY' L.

P.

Broon t -

TELEPHONE (313)586-5313 REPORT MONTH November I-METHOD OF LER SYS COMP CAUSE & CORRECTIVE NO.

DATE TYPE DUR REASON SHUTTING DOWN NO.

CODE CODE ACTION TO PREVENT (1)

(HRS)

(2)

THE REACTOR (4)

(5)

RECURRLNCE (3) 86-06 861107 F

560.9 A

2 N/A HC HTEXCHD Shutdown to repair the cause of excessive air.in-leakage into the condenser. Outage scope has been expanded to include installation of I new relief valves to prevent future overpressurization of the condensate return line.

On November 17, 1986 overpressurization of thi s -. l i ne caused an expansion joint to rupture and damaged a penetration in the

]

Condensate Storage Tank, l

d I

(1) F: FORCED (2) REASON:

(3) METHOD:

(4) EXHIBIT G - INSTRUCTIOh5 S: SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM ENTRY SHEETS FOk LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM EVENT REPORT (LER) FILL D - REGULATORY RESTRICTION 4 - CONTINUED (NUREG-0161)'

E - OPERATOR TRAINING & LICENSE EXAMINATION 5 - REDUCED LOAD F - ADMINISTRATIVE 9 - OTHER G.- OPERATIONAL ERROR (EXPLAIN)

H - OTHER (EXPLAIN)

(5) EXHIBIT I - SAME SOURCE O