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{{#Wiki_filter:.                             .    -- --                  .  .    . - . .                  ,
{{#Wiki_filter:.
:    a.   -y-4 j                                            LASALLE NUCLEAR POWER STATION d                                                                      UNIT 1
a.
.i 4                                            MONTHLY PERFORMANCE REPORT APRIL 1987 Cot 990NWEALTH EDISON COMPANY i
-y-4 LASALLE NUCLEAR POWER STATION j
i NHC DOCKET NO. 050-373 d
UNIT 1 d
LICENSE NO. NPP-ll I
.i MONTHLY PERFORMANCE REPORT 4
APRIL 1987 Cot 990NWEALTH EDISON COMPANY i
i NHC DOCKET NO. 050-373 LICENSE NO. NPP-ll d
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n 8705190018 870430 PDR     ADOCK 05000373       PDR-                                                                                           ,
n 8705190018 870430 PDR ADOCK 05000373 PDR-R DOCUMENT ID 0043r/0005r
R DOCUMENT ID 0043r/0005r                                                                                         /p     L-
/p L-


1 TABLE OF CONTENTS I. INTRODUCTION II. MONTHLY REPORT FOR UNIT ONE                                           l A. Sumusary of Operating Experience B. PLANT OR PROCEDURE CHANGES, TESTS, EXPERIMENTS, AND SAFETY RELATED MAINTENANCE
1 TABLE OF CONTENTS I.
: 1. Amendments to Facility Licen.=,e or Technical Specifications
INTRODUCTION II.
: 2. Facility or Procedure Changes Requiring NRC Approval
MONTHLY REPORT FOR UNIT ONE l
: 3. Tests and Experiments Requiring NRC Approval.
A.
: 4. Corrective Maintenance of Safety Related Equipment
Sumusary of Operating Experience B.
: 5. Completed Safety Related Modifications.
PLANT OR PROCEDURE CHANGES, TESTS, EXPERIMENTS, AND SAFETY RELATED MAINTENANCE 1.
C. -LICENSEE EVENT REPORTS D. DATA TABULATIONS
Amendments to Facility Licen.=,e or Technical Specifications 2.
: 1. Operating Data Report
Facility or Procedure Changes Requiring NRC Approval 3.
: 2. Average Daily Unit Power Level
Tests and Experiments Requiring NRC Approval.
: 3. Unit Shutdowns and Power Reductions E. UNIQUE REPORTING REQUIREMENTS
4.
: 1. Main Steam Relief Valve Operations
Corrective Maintenance of Safety Related Equipment 5.
: 2. ECCS System Outages
Completed Safety Related Modifications.
: 3. Off-Site Dose Calculation Manual Changes
C.
: 4. Major Changes to Radioactive Waste Treatment System
-LICENSEE EVENT REPORTS D.
: 5. Indications of Failed Fuel Elements DOCUMENT ID 0043r/0005r
DATA TABULATIONS 1.
                =
Operating Data Report 2.
Average Daily Unit Power Level 3.
Unit Shutdowns and Power Reductions E.
UNIQUE REPORTING REQUIREMENTS 1.
Main Steam Relief Valve Operations 2.
ECCS System Outages 3.
Off-Site Dose Calculation Manual Changes 4.
Major Changes to Radioactive Waste Treatment System 5.
Indications of Failed Fuel Elements DOCUMENT ID 0043r/0005r
=


e   1 I. INTRODUCTION a
e 1
I.
INTRODUCTION a
The LaSalle County Nuclear Power Station is a two-unit facility owned by commonwealth Edison Company and located near Marseilles, Illinois.
The LaSalle County Nuclear Power Station is a two-unit facility owned by commonwealth Edison Company and located near Marseilles, Illinois.
Each unit is a Boiling Water Reactor with a designed net electrical
Each unit is a Boiling Water Reactor with a designed net electrical
                                                                    ~
~
output of 1078 Megawatts. Waste heat is rejected to a man-made cooling                             l pond using the. Illinois River for make-up and blowdown. The                                       '
output of 1078 Megawatts. Waste heat is rejected to a man-made cooling pond using the. Illinois River for make-up and blowdown. The architect-engineer was Sargent and Lundy and the primary construction
architect-engineer was Sargent and Lundy and the primary construction
. contractor was commonwealth Edison Company.
          . contractor was commonwealth Edison Company.                                                       1 l
1 Unit one was issued operating license number NPF-11 on April 17, 1982.
Unit one was issued operating license number NPF-11 on April 17, 1982.                             '
Initial criticality was achieved on June 21, 1982 and commercial power operation was commenced on January 1, 1984.
Initial criticality was achieved on June 21, 1982 and commercial power operation was commenced on January 1, 1984.                                                       l
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                                                                                                              \
This report was compiled by Gregory J. Kirchner, telephone number (815)357-6761, extension 704.
This report was compiled by Gregory J. Kirchner, telephone number (815)357-6761, extension 704.
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i DOCUMENT ID 0043r/0005r
i DOCUMENT ID 0043r/0005r


II.     MONTHLY REPORT FOR UNIT ONE A.      
II.
MONTHLY REPORT FOR UNIT ONE A.


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE FOR UNIT ONE APRIL 1987 4-1-87 0000 hours -         Rx Critical, generator at 600 MWe.
OF OPERATING EXPERIENCE FOR UNIT ONE APRIL 1987 4-1-87 0000 hours -
4-2-87 2100 hours -         Commence power increase to 620 MWe at 10 MWe/hr.
Rx Critical, generator at 600 MWe.
4-13-87 2310 hours -       Reduce power to 600 MWe in order to take                 'A' TDRFP out of service.
4-2-87 2100 hours -
4-14-87 2050 hours -       Start ramp at 10 MWe/hr to 620 MWe to put
Commence power increase to 620 MWe at 10 MWe/hr.
                                            'A' TDRFP on.
4-13-87 2310 hours -
4-24-87 2200 hours -       Drop 30 MWe to 590 MWe to perform LOS-AA-W1 on HCU pressures, then recover to 625 MWe.
Reduce power to 600 MWe in order to take
4-30-87 2400 hours -       Rx critical, generator on line at_630 MWe.
'A' TDRFP out of service.
4-14-87 2050 hours -
Start ramp at 10 MWe/hr to 620 MWe to put
'A' TDRFP on.
4-24-87 2200 hours -
Drop 30 MWe to 590 MWe to perform LOS-AA-W1 on HCU pressures, then recover to 625 MWe.
4-30-87 2400 hours -
Rx critical, generator on line at_630 MWe.
DOCUMENT ID 0043r/0005r
DOCUMENT ID 0043r/0005r


D.       PLANT OR PROCEDURE CHANGES, TESTS,' EXPERIMENTS AND' SAFETY RELATED                             l
D.
        .,        g MAINTENANCE.
PLANT OR PROCEDURE CHANGES, TESTS,' EXPERIMENTS AND' SAFETY RELATED MAINTENANCE.
l
g 1.
: 1. Amendments to. Facility License or Technical Specification.                                 i l
Amendments to. Facility License or Technical Specification.
There were no ammendments to-Facility License or Technical i                      Specifications during this reporting period.
There were no ammendments to-Facility License or Technical Specifications during this reporting period.
s
i s
                                                        ~
~
,                  2. Facility or Procedure changes requiring NRC approval.
2.
l 4
Facility or Procedure changes requiring NRC approval.
There were no Facility or Procedural changes requiring NRC approval during this reporting period.
There were no Facility or Procedural changes requiring NRC approval 4
: 3. Tests and Experiments requiring NRC approval.
during this reporting period.
                                                                            ~
3.
Tests and Experiments requiring NRC approval.
~
There were no tests or experiments requiring NRC approval during this reporting period.
There were no tests or experiments requiring NRC approval during this reporting period.
: 4. Corrective Maintenance of Safety Related Equipment.
4.
Corrective Maintenance of Safety Related Equipment.
The following table (Table 1) presents a Summary of safety-related maintenance completed on Unit one during the reporting period. The headings ~ indicated in this summary include:
The following table (Table 1) presents a Summary of safety-related maintenance completed on Unit one during the reporting period. The headings ~ indicated in this summary include:
Work Request number, Component Name, Cause_of Malfunction, Results
Work Request number, Component Name, Cause_of Malfunction, Results and Effects on Safe Operation, and Corrective Action.
.;                      and Effects on Safe Operation, and Corrective Action.
5.
: 5. Completed Safety Related Modifications.
Completed Safety Related Modifications.
i The following Table (Table 2) presents a list of completed Modifications during this reporting period. Each entry will have a short synopsis explaining details involved with each modification.
i The following Table (Table 2) presents a list of completed Modifications during this reporting period. Each entry will have a short synopsis explaining details involved with each modification.
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-~ -,_


TABLE 1 CORRECTIVE MAINTENANCE OF                                             .
TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT UNIT #1 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 63159 RCIC Steam Supply Valve Packing Leaks Repack Valve Valve Repacked.
SAFETY RELATED EQUIPMENT UNIT #1 WORK REQUEST   COMPONENT             CAUSE OF MALFUNCTION           RESULTS AND EFFECTS           CORRECTIVE ACTION ON SAFE PLANT OPERATION 63159       RCIC Steam Supply     Valve Packing Leaks         Repack Valve                   Valve Repacked.
Drain Pot Steam Trap Assembly Inlet Stop Valve IE51-F038 64940 HPCS D/G Low Air Alarm Setpoint High Calibrate Recalibrated Switch Pressure Alarm lE22-Verified proper Ops.
Drain Pot Steam Trap Assembly Inlet Stop Valve IE51-F038 64940       HPCS D/G Low Air       Alarm Setpoint High         Calibrate                       Recalibrated Switch Pressure Alarm lE22-                                                               Verified proper Ops.
N504 64941 HPCS D/G Low Air Pressure Alarm lE22--
N504 64941       HPCS D/G Low Air Pressure Alarm lE22--
N505 1
,              N505 1
65144 Isolation Damper to Damper Failed in Close Bad Limit Switch Adjusted Travel Limit East Control Room Position Switch Arm to proper tension.
65144       Isolation Damper to   Damper Failed in Close     Bad Limit Switch                 Adjusted Travel Limit East Control Room     Position                                                     Switch Arm to proper tension.
l l
l l 66051       HPCS Diesel Vent     Air Filter Diff. Press. Hi Recalibrate                       Recalibrated IPDS--VD004 l
66051 HPCS Diesel Vent Air Filter Diff. Press. Hi Recalibrate Recalibrated IPDS--VD004 l
Intake Filter D/P     Alarm                                                         and IPDI-VD004.
Intake Filter D/P Alarm and IPDI-VD004.
l             IPDS-VD004 1
l IPDS-VD004 1
66761       RCIC Water Leg Pump   Pump is binding             Breaker trip on high current     New pump installed.
66761 RCIC Water Leg Pump Pump is binding Breaker trip on high current New pump installed.
66766       1A RHR Hx Vent V1v   Valve will not full close   Vlv not travelling full close   Contacts loose on limit-IE12-F073A                                                                         orque. Tightened contact and assured proper ops.
66766 1A RHR Hx Vent V1v Valve will not full close Vlv not travelling full close Contacts loose on limit-IE12-F073A orque. Tightened contact and assured proper ops.
66800       RCIC Steam Vlv. IF51- Valve didn't auto open       Auto open does not function on   Adjusted micro-switch N010                                               High Steam Line Drain Pot Alarm assured proper ops.
66800 RCIC Steam Vlv. IF51-Valve didn't auto open Auto open does not function on Adjusted micro-switch N010 High Steam Line Drain Pot Alarm assured proper ops.
I 66832       Ammonia Detector     Manual zero adjust is       Replace meter                   Replaced meter and damaged on meter.                                             calibrated.
I 66832 Ammonia Detector Manual zero adjust is Replace meter Replaced meter and damaged on meter.
calibrated.
DOCUMENT ID 0043r/0005r
DOCUMENT ID 0043r/0005r


TABLE 1 CORRECTIVE MAINTENANCE CF                                             .
TABLE 1 CORRECTIVE MAINTENANCE CF SAFETY RELATED EQUIPMENT UNIT #1 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 66867 RCIC Water Lcg Pump Valve did not seat Disassemble / Repair Valve cleaned internally, Discharge Valve IE51-properly new bonnet gasket installed F061 proper ops.
SAFETY RELATED EQUIPMENT UNIT #1                                                                                               -
66869 Containment Monitoring Paper does not advance.
WORK REQUEST     COMPONENT             CAUSE OF MALFUNCTION           RESULTS AND EFFECTS           CORRECTIVE ACTION ON SAFE PLANT OPERATION 66867       RCIC Water Lcg Pump   Valve did not seat           Disassemble / Repair           Valve cleaned internally, Discharge Valve IE51- properly                                                     new bonnet gasket installed F061                                                                               proper ops.
Bad Drive Gear.
66869       Containment Monitoring Paper does not advance.     Bad Drive Gear.                 Replace Drive Gear Temp. Recorder ITR-                                                                 observed for 24 hours CM037                                                                               satisfactorily.
Replace Drive Gear Temp. Recorder ITR-observed for 24 hours CM037 satisfactorily.
66998       DWEDS Outboard Iso-   Valve dos not fully open. Adjust limit switch             Adjusted limit switch for lation Valve 1RE025                                                                 proper Ops.
66998 DWEDS Outboard Iso-Valve dos not fully open.
67031       D/P Gage & Alarm       Gage reading low.           Recalibrate                     Recalibrated and assured IPDI-VX014                                                                         proper Ops.
Adjust limit switch Adjusted limit switch for lation Valve 1RE025 proper Ops.
67168       DIV 1 POST LOCA Lvl/   Motor Making Noise.         Recorder is oscilloting.       Rcplaced faulty servo' Press Recorder 1B21-                                                               motor assembly.
67031 D/P Gage & Alarm Gage reading low.
R884A 67225       Ammonia Detector       Detector Failed.             Troubleshoot                   Replaced photocell board, 0XY- VC125B                                                                         magnets, drive motor, and calibrated.
Recalibrate Recalibrated and assured IPDI-VX014 proper Ops.
67449       Supp. Pool Temp.       Does not Print               Repair / Replace               Adjusted printhead solen-Recorder ITR-CM038                                                                 old for proper Ops.
67168 DIV 1 POST LOCA Lvl/
67507       Accumulator 22--19     Vlv. Leaks                   Repla$e (111) Cartridge.         (111) Cartridge replaced.
Motor Making Noise.
Recorder is oscilloting.
Rcplaced faulty servo' Press Recorder 1B21-motor assembly.
R884A 67225 Ammonia Detector Detector Failed.
Troubleshoot Replaced photocell board, 0XY-VC125B magnets, drive motor, and calibrated.
67449 Supp. Pool Temp.
Does not Print Repair / Replace Adjusted printhead solen-Recorder ITR-CM038 old for proper Ops.
67507 Accumulator 22--19 Vlv. Leaks Repla$e (111) Cartridge.
(111) Cartridge replaced.
111 Valve.
111 Valve.
67535       Suppression Chamber   Temperature Recorder off     Recalibrate                     Calibrated and observed Air Temperature ITR-   by 10*F.                                                     proper Ops.
67535 Suppression Chamber Temperature Recorder off Recalibrate Calibrated and observed Air Temperature ITR-by 10*F.
CM040 67569       CRD Accumulator #26 -43 (111) Valve leaks           Replace cartridge               Cartridge replaced.
proper Ops.
67399       'D' APRM             'D' APRM Giving Half Scrams Gives half scrams on Hi Neutron Replaced Kl8 Relay verified Flux.                           proper Ops.
CM040 67569 CRD Accumulator #26 -43 (111) Valve leaks Replace cartridge Cartridge replaced.
DOCUMENT ID 0043r/0005r                                                                                                     l
67399
'D' APRM
'D' APRM Giving Half Scrams Gives half scrams on Hi Neutron Replaced Kl8 Relay verified Flux.
proper Ops.
DOCUMENT ID 0043r/0005r l


. i TABLE 2 COMPLETED SAFETY RELATED MODIFICATIONS MODIPICATION NUMBdR: A brief synopsis of incorporated modification objectives with final design resolution. Also, state reviewed or unreviewed safety questions.
i TABLE 2 COMPLETED SAFETY RELATED MODIFICATIONS MODIPICATION NUMBdR: A brief synopsis of incorporated modification objectives with final design resolution. Also, state reviewed or unreviewed safety questions.
UNIT ONE M-1-0-85-008     This Modification provided access to various fire dampers that are not accessable per the August, 19d4, technical basis of the LaSalle County Station Fire Damper Surveillance program. There were no unreviewed safety questions.
UNIT ONE M-1-0-85-008 This Modification provided access to various fire dampers that are not accessable per the August, 19d4, technical basis of the LaSalle County Station Fire Damper Surveillance program. There were no unreviewed safety questions.
M-J-0-85-011     This Modification was to install the interconnections required for the interim Redwaste Storage Facility telephone connection, paging connection, fire detection alarm connection, and the potentially contaminated sump high level alarm connection. There were no unreviewed safety questions.
M-J-0-85-011 This Modification was to install the interconnections required for the interim Redwaste Storage Facility telephone connection, paging connection, fire detection alarm connection, and the potentially contaminated sump high level alarm connection. There were no unreviewed safety questions.
M-1-0-86-023     This Modification was to improve the exiting method of sampling the flow in the Mid/Hi Range portio of the Stadnby Gas Treatment Wide Range Gas Monitor (WRGM). This change will minimize the amount of iodine plateout in the sample line. There were no unreviewed safety questions.
M-1-0-86-023 This Modification was to improve the exiting method of sampling the flow in the Mid/Hi Range portio of the Stadnby Gas Treatment Wide Range Gas Monitor (WRGM). This change will minimize the amount of iodine plateout in the sample line. There were no unreviewed safety questions.
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            .C.     ' LICENSEE EVENT REPORTS                                                                                                                               l I
.C.
' LICENSEE EVENT REPORTS I
The following is a tabular summary of all licensee event reports for LaSalle Nuclear Power Station, Unit One, logged during the reporting period, April 1, 1987 through April 30, 1987. This information is provided pursuant to the reportable occurrence reporting requirements as set forth in 10CFR 50.73.
The following is a tabular summary of all licensee event reports for LaSalle Nuclear Power Station, Unit One, logged during the reporting period, April 1, 1987 through April 30, 1987. This information is provided pursuant to the reportable occurrence reporting requirements as set forth in 10CFR 50.73.
Licensee Event Report Number                     Date                     Title of Occurrence 87-016-00                                     4/1/87                     RCIC Isolation on Steam Line High Flow.
Licensee Event Report Number Date Title of Occurrence 87-016-00 4/1/87 RCIC Isolation on Steam Line High Flow.
.            87-017-00                                     4/2/87                     1.69 PSIG DW Pressure Switch
87-017-00 4/2/87 1.69 PSIG DW Pressure Switch valved out.
!                                                                                                                                                                5 valved out.
5
                                                                                                                                                                    -\
-\\
87-018-00                                     4/13/87                     'A' VC Ammonia Detector spurious trip.
87-018-00 4/13/87
87-019-00                                     4/3/87                     Incomplete surveillance on CRD
'A' VC Ammonia Detector spurious trip.
'                                                                                      cycling.
87-019-00 4/3/87 Incomplete surveillance on CRD cycling.
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87-020-00                                     4/16/87                   Loss of 12C/208 Distribution at i                                                                                     MCC 136X-1.                                                                     ,
(
87-020-00 4/16/87 Loss of 12C/208 Distribution at i
MCC 136X-1.
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DOCUMENT ID 0043r/0005r                                                                                                                                     i i
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D.           DATA TABULATIONS The following data tabulations are presented in this report:
5' D.
: 1. Operating Data Report
DATA TABULATIONS The following data tabulations are presented in this report:
: 2. Average Daily Unit Power Level
1.
: 3. Unit Shutdowns and Power Reductions i
Operating Data Report 2.
i                                                                                                                                                   l 4 -
Average Daily Unit Power Level 3.
Unit Shutdowns and Power Reductions i
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$                          DOCUMENT ID 0043r/0005r
DOCUMENT ID 0043r/0005r


                                                                                                                                                            . ~ , . - _ -
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                      ,  1. _ OPERATING DATA REPORT-                   )
T.
                                                                              .                                  DOCKET No. 050-373 UNIT LaSalle One
1.
                                                                        'I                               ,
_ OPERATING DATA REPORT-
DATE May 10. 1987 1              j.                                    !. COMPLETED BY G. J. Kirchner
)
                                                            ,,  [                                     r v        TELEPHONE (815)357-6761
DOCKET No. 050-373 UNIT LaSalle One
,                        OPERATING STATUS       >  +
'I DATE May 10. 1987
                                    ,              <      c[s                                                                                                           ,
,!. COMPLETED BY G. J. Kirchner 1
1.-   REPORTING' PERIOD: _ _ _ ADril. 1987 GROSS HOURS IN REPORTING PERIOD: 719
j.
: 2. CURRENTLY AUTHORIZED POWER LEVEL (MWt):2 H1 MAX DEPEND CAPACITY (MWe-Net): 1036         DESIGN ELECTRICAL RATING (MWe-Net): 1078
[
: 3. POWER LEVEL TO WHICH RESTRICTED (IF ANY) (MWe-Net):                                         1050
TELEPHONE (815)357-6761 v
: 4.   . REASONS FOR RESTRICTION (IF ANY): Administrative
r OPERATING STATUS
              ,          s vI               f THIS MONTH YR TO DATE                     CUMULATIVE
[s
            "            5                                                                             719             2471.60                 18164.40 NUMBER OF HOURS REACTOR WAS_ CRITICAL
+
: 6. REACTOR RESERVII SHUTDOWN HOURS                                         0.0:               0.0                   1642.0,_
c 1.-
: 7. HOURS, GENERATOR ON LINE           , , ,'-                              719             2356.90                 17506.40 1
REPORTING' PERIOD: _ _ _ ADril. 1987 GROSS HOURS IN REPORTING PERIOD: 719 2.
: g.          8. UNIT RESERVE SHUTDOWN HOURS _ j*                                       0.0               0.0                   0.0
CURRENTLY AUTHORIZED POWER LEVEL (MWt):2 H1 MAX DEPEND CAPACITY (MWe-Net): 1036 DESIGN ELECTRICAL RATING (MWe-Net): 1078 3.
: 9. GROSS THERMAL ENERGY GENERATED (MWH)                                 1399704           5029296                 45614218 l                       10. GROSS ELEC. ENERGY GENERATED (MWH)                                     446508           1629188                 14319865-
POWER LEVEL TO WHICH RESTRICTED (IF ANY) (MWe-Net):
: 11. NET ELEC.' ENEEGY GENERATED (MWH)                                     431404           1565969                 13588543
1050 4.
: 12. REACTOR SERVICE FACTOR                                                 100%               85%                     62%
. REASONS FOR RESTRICTION (IF ANY): Administrative vI f
    +
THIS MONTH YR TO DATE CUMULATIVE s
: 13. REACTOR AVAILABILITY FACTOR                                           100%               85%                   _ 68%
5 NUMBER OF HOURS REACTOR WAS_ CRITICAL 719 2471.60 18164.40 6.
i                       14. UNIT SERVICE FACTOR                                                   100%               82%                     60%
REACTOR RESERVII SHUTDOWN HOURS 0.0:
4
0.0 1642.0,_
: 15. UNIT AVAILABILITY FACTOR                                               100%               82%                     60%
7.
: 16. UNIT CAPACITY FACTOR (USING MDC)                                       60% ___           56%                     45%
HOURS, GENERATOR ON LINE 719 2356.90 17506.40 1
: 17. UNIT CAPACITY FACTOR (USING DESIGN-MWe)                                                                   55%               50%                     43%
8.
: 18. UNIT FORCED OUTAGE RATE                                                   0%             21%                   15.2%
UNIT RESERVE SHUTDOWN HOURS _ j*
: 19. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH)
0.0 0.0 0.0 g.
9.
GROSS THERMAL ENERGY GENERATED (MWH) 1399704 5029296 45614218 l
10.
GROSS ELEC. ENERGY GENERATED (MWH) 446508 1629188 14319865-11.
NET ELEC.' ENEEGY GENERATED (MWH) 431404 1565969 13588543 12.
REACTOR SERVICE FACTOR 100%
85%
62%
13.
REACTOR AVAILABILITY FACTOR 100%
85%
_ 68%
+
i 14.
UNIT SERVICE FACTOR 100%
82%
60%
15.
UNIT AVAILABILITY FACTOR 100%
82%
60%
4 16.
UNIT CAPACITY FACTOR (USING MDC) 60% ___
56%
45%
17.
UNIT CAPACITY FACTOR (USING DESIGN-MWe) 55%
50%
43%
18.
UNIT FORCED OUTAGE RATE 0%
21%
15.2%
19.
SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH)
On June 13, 1987, Unit I will be shutdown to repair the IB Reactor Recirc Pump. The chutdown is scheduled to last fifty (50) days.
On June 13, 1987, Unit I will be shutdown to repair the IB Reactor Recirc Pump. The chutdown is scheduled to last fifty (50) days.
: 20. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
20.
IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
N/A i
N/A i
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i DOCUMENT ID 0043r/0005r l
                                                                  - _ _ . _ . . _ _ _ . . _ _ _ _ _                              _ _ . _ _ _ .          _ . . _ ~ . _ _
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: 2. AVERAGE DAILY UNIT POWER LEVEL DOCKET NO: 050-373 UNIT: LASALLE ONE DATE: May 10, 1987 COMPLETED BY: Gregory Kirchner i
: 2. AVERAGE DAILY UNIT POWER LEVEL DOCKET NO: 050-373 UNIT: LASALLE ONE DATE: May 10, 1987 COMPLETED BY: Gregory Kirchner i
TELEPHONE: (815) 357-6761 MONTH: April. 1987 DAY AVERAGE DAILY POWER LEVEL       DAY AVERAGE DAILY POWER LEVEL (MWe-Net)                             (MWe-Net) i          1.           580               17.                   606
TELEPHONE: (815) 357-6761 MONTH: April. 1987 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
: 2.           580               18.                   604 3           607               19.                   601
(MWe-Net) 1.
          <.          608               20.                   603
580 17.
: 5. .         582               21.                   600 l
606 i
: 6.           606             _
2.
: 22.                   601
580 18.
: 7.           605               23.                   602
604 3
: 8.           604               24.                   601 9._         602               25.                   601
607 19.
: 10.           602               26.                   602 11.__         600               27.                   600 12._         597               28.                   600
601 608 20.
: 13.           599               29.                   604
603
: 14.           580               30.                   602
: 5..
: 15.           596               31.                   ---
582 21.
: 16.           598 l
600 l
DOCUMENT ID 0043r/0005r
6.
: 3. UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 050-373     ,
606 22.
UNIT NAME LaSalle One DATE     May 10, 1987 REPORT MONTil APRIL, 1987               COMPLETED BY Gregory Icirchner TELEPliONE (815)357-6761 METilOD OF TYPE                                               SliUTTING DOWN F: FORCED         DURATION                           TIIE REACTOR OR   CORRECTIVE NO. DATE         S: SCl!EDULED       (liOURS)         REASON           REDUCING POWER   ACTIONS / COMMENTS Unit was critical for 719 hours during April, 1987 s
601 7.
605 23.
602 8.
604 24.
601 9._
602 25.
601 10.
602 26.
602 11.__
600 27.
600 12._
597 28.
600 13.
599 29.
604 14.
580 30.
602 15.
596 31.
16.
598 DOCUMENT ID 0043r/0005r
 
3.
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 050-373 UNIT NAME LaSalle One DATE May 10, 1987 REPORT MONTil APRIL, 1987 COMPLETED BY Gregory Icirchner TELEPliONE (815)357-6761 METilOD OF TYPE SliUTTING DOWN F: FORCED DURATION TIIE REACTOR OR CORRECTIVE NO.
DATE S: SCl!EDULED (liOURS)
REASON REDUCING POWER ACTIONS / COMMENTS Unit was critical for 719 hours during April, 1987 s
DOCUMENT ID 0043r/0005r
DOCUMENT ID 0043r/0005r


E. UNIQUE REPORTING REQUIREMENTS
E.
UNIQUE REPORTING REQUIREMENTS
: 1. Safety / Relief valve operations for Unit One.
: 1. Safety / Relief valve operations for Unit One.
VALVES       NO & TYPE     PLANT                                   DESCRIPTION DATE         ACTUATED     ACTUATION     CONDITION                               OF EVENT There were no Safety Relief Valves Operated for Unit One during this reporting period.
VALVES NO & TYPE PLANT DESCRIPTION DATE ACTUATED ACTUATION CONDITION OF EVENT There were no Safety Relief Valves Operated for Unit One during this reporting period.
t 1
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DOCUMENT ID 0043r/0005r l
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_    _                          =-. .             . _ . . _ . - . - . , . . . _ _.. ,,,-.- _
                                                                                                        -_ -..-._. - - . _ -1


                .                .                        -                            - ~ .
~.
: 2. ECCS Systems Outagns Tha following outagsa were takin on ECCS Systems during' the reporting period.
2.
OUTAGE NO.           EOUIPMENT                   EURPOSE OF OUTAGE U-l and Common il 0-74-87                   'O' Diesel Generator         Lube and Filter Change 0-75-87                   'O' D/G                     Temperature and Oil Switches I
ECCS Systems Outagns Tha following outagsa were takin on ECCS Systems during' the reporting period.
OUTAGE NO.
EOUIPMENT EURPOSE OF OUTAGE U-l and Common il 0-74-87
'O' Diesel Generator Lube and Filter Change 0-75-87
'O' D/G Temperature and Oil Switches I
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DOCUMENT ID 0043r/0005r 1
DOCUMENT ID 0043r/0005r 1
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      . s
s 3.
: 3. Off-Site Dose Calculation Manual l
Off-Site Dose Calculation Manual There were no changes to the ODCM during this reporting period.
There were no changes to the ODCM during this reporting period.
4.
: 4. Radioactive Waste Treatment Systems.
Radioactive Waste Treatment Systems.
There were no changes to the Radioactive Waste treatment systems during this reporting period.
There were no changes to the Radioactive Waste treatment systems during this reporting period.
: 5. Indications of Failed Fuel Elements There were no indications of Failed Fuel Elements during this reporting period.
5.
Indications of Failed Fuel Elements There were no indications of Failed Fuel Elements during this reporting period.
l l
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DOCUMENT ID 0043r/0005r


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  !                          LASALLE NUCLEAR POWER STATION UNIT 2 i
LASALLE NUCLEAR POWER STATION UNIT 2 i
i                               MONTHLY PERFORMANCE REPORT 1
i MONTHLY PERFORMANCE REPORT 1
I                                     ~ APRIL, 1987 l
I
!                              COMMONWEALTH EDISON COMPANY i
~ APRIL, 1987 l
f                                 NRC DOCKET NO. 050-374 i
COMMONWEALTH EDISON COMPANY i
t                                   LICENSE NO. NPF-18 i
f NRC DOCKET NO. 050-374 i
t LICENSE NO. NPF-18 i
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l DOCUMENT ID 0036r/0005r t                                                           _
l DOCUMENT ID 0036r/0005r t
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TABLE OF CONTENTS 4
TABLE OF CONTENTS 4
I.         INTRODL37 TION II.         MONTHLY REPORT FOR UNIT TWO A.         Summary of Operating Experience
I.
                            -B.           PLANT OR PROCEDURE CHANGES, TESTS, EXPERIMENTS, AND SAFETY RELATED MAINTENANCE 4,
INTRODL37 TION II.
: 1. Amendments to Facility License'or Technical Specifications
MONTHLY REPORT FOR UNIT TWO A.
: 2. Facility or Procedure Changes Requiring NRC Approval
Summary of Operating Experience
: 3. Tests and Experiments Requiring NRC Approval
-B.
: 4. Corrective Maintenance of Safety Related Equipment i
PLANT OR PROCEDURE CHANGES, TESTS, EXPERIMENTS, AND 4,
: 5. Completed Safety Related Modifications C.         LICENSEE EVENT REPORTS 1
SAFETY RELATED MAINTENANCE 1.
D.         DATA TABULATIONS 4
Amendments to Facility License'or Technical Specifications 2.
: 1. Operating Data Report
Facility or Procedure Changes Requiring NRC Approval 3.
: 2. Average Daily Unit Power Level
Tests and Experiments Requiring NRC Approval 4.
: 3. Unit Shutdowns and Power Reductions E.         UNIQUE REPORTING REQUIREMENTS
Corrective Maintenance of Safety Related Equipment 5.
: 1. Safety / Relief Valve Operations
Completed Safety Related Modifications i
: 2. ECCS System Outages
C.
: 3. Off-Site Dose Calculation Manual Changes
LICENSEE EVENT REPORTS 1
: 4. Major Changes to Radioactive Waste Treatment j                                             System
D.
: 5. Indications of Failed Fuel Elements 1
DATA TABULATIONS 4
l l
1.
.                                                                                                                              1 l
Operating Data Report 2.
i                                                                                                                             !
Average Daily Unit Power Level 3.
:-                                                                                                                          l i
Unit Shutdowns and Power Reductions E.
i
UNIQUE REPORTING REQUIREMENTS 1.
;                                                                                                                              l 1
Safety / Relief Valve Operations 2.
1 I
ECCS System Outages 3.
1                                                                                                                             I
Off-Site Dose Calculation Manual Changes 4.
  )                                                                                                                             j
Major Changes to Radioactive Waste Treatment j
.i                                                                                                                             i DOCUMENT ID 0036r/0005r t
System 5.
r----r-ev     -r----               ~r- -
Indications of Failed Fuel Elements 1
                                                              -~ -         -         -       -* -~--- - - - - - -
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Q:   6 I.         INTRODUCTION The LaSalle County Nuclear Power Station is a two-unit facility owned by Commonwealth Edison Company and located near Marseilles, Illinois.
Q:
6 I.
INTRODUCTION The LaSalle County Nuclear Power Station is a two-unit facility owned by Commonwealth Edison Company and located near Marseilles, Illinois.
Each unit is a Boiling Water Reactor with a designed net electrical output of 1078 Megawatts. Waste heat ir rejseted to a man-made cooling pond using the Illinois River for make-up and blowdown. The architect-engineer was Sargent and Lundy and the primary construction contractor was commonwealth Edison Company.
Each unit is a Boiling Water Reactor with a designed net electrical output of 1078 Megawatts. Waste heat ir rejseted to a man-made cooling pond using the Illinois River for make-up and blowdown. The architect-engineer was Sargent and Lundy and the primary construction contractor was commonwealth Edison Company.
Unit two was issued operating license number NPF-18 on December 16, 1983. Initial criticality was achieved on March 10, 1984 and commercial power operation was commenced on June 19, 1984.
Unit two was issued operating license number NPF-18 on December 16, 1983. Initial criticality was achieved on March 10, 1984 and commercial power operation was commenced on June 19, 1984.
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II..         MCNTHLY REPORT FOR UNIT TWO
II..
: e.         's
MCNTHLY REPORT FOR UNIT TWO e.
          'A.         . SU19tARY OF OPERATING EXPERIENCE FOR UNIT TWO APRIL 01-30, 1987                                                             ,
's
4-1-87, 0000 hours -           Rx in refuel 4-30-87, 2400 hours -           Rx in refuel.
'A.
. SU19tARY OF OPERATING EXPERIENCE FOR UNIT TWO APRIL 01-30, 1987 4-1-87, 0000 hours -
Rx in refuel 4-30-87, 2400 hours -
Rx in refuel.
i
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                                                                                                                                ?
?
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1 D.
  , D. , PLANT OR PROCEDURE CHANGES, TESTS, EXPERIMENTS AND SAFETY RELATED                       1 MAINTENANCE.
PLANT OR PROCEDURE CHANGES, TESTS, EXPERIMENTS AND SAFETY RELATED MAINTENANCE.
: 1. Amendments to Facility license, or Technical Specification.
1.
Amendments to Facility license, or Technical Specification.
AMENDMENT
AMENDMENT
            #30     This amendment revises the LSCS Unit 2 Technical Specifications to permit replacing an existing peripheral (02-43) locking piston control rod drive module with a fine motion control rod drive module during one fuel cycle (Cycle 2).
#30 This amendment revises the LSCS Unit 2 Technical Specifications to permit replacing an existing peripheral (02-43) locking piston control rod drive module with a fine motion control rod drive module during one fuel cycle (Cycle 2).
            #31     This amendment revises the LSCS Unit 2 Technical Specifications to reflect a low and/or degraded grid voltage modification in Division I of the electrical divisions.
#31 This amendment revises the LSCS Unit 2 Technical Specifications to reflect a low and/or degraded grid voltage modification in Division I of the electrical divisions.
            #32     This amendment revises the LSCS Unit 2 Technical Specifications to support operation of Unit 2 at rated power during Cycle 2 operation.
#32 This amendment revises the LSCS Unit 2 Technical Specifications to support operation of Unit 2 at rated power during Cycle 2 operation.
: 2. Facility or Procedure changes requiring NRC approval.
2.
Facility or Procedure changes requiring NRC approval.
There were no Facility or Procedure changes requiring NRC approval curing the reporting period.
There were no Facility or Procedure changes requiring NRC approval curing the reporting period.
: 3. Tests and Experiments requiring NRC approval.
3.
Tests and Experiments requiring NRC approval.
There were no Tests or Experiments requiring NRC approval during the reporting period.
There were no Tests or Experiments requiring NRC approval during the reporting period.
: 4. Corrective Maintenance of Safety Related Equipment.
4.
Corrective Maintenance of Safety Related Equipment.
The following table (Table 1) presents a summary of Safety-Related Maintenance completed on Unit Two during the reporting period. The headings indicated in this summary include: Work Request number, Component Name, cause of malfunction, results and effects on safe operation, and corrective action.
The following table (Table 1) presents a summary of Safety-Related Maintenance completed on Unit Two during the reporting period. The headings indicated in this summary include: Work Request number, Component Name, cause of malfunction, results and effects on safe operation, and corrective action.
: 5. Completed Safety Related Modifications.
5.
Completed Safety Related Modifications.
The following table (Table 2) presents a list of completed Modifications during this reporting period. Each entry will have a short synopsis explaining details involved with each modification.
The following table (Table 2) presents a list of completed Modifications during this reporting period. Each entry will have a short synopsis explaining details involved with each modification.
DOCUMENT ID 0036r/0005r
DOCUMENT ID 0036r/0005r


s TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST           COMPONENT                     CAUSE OF MALFUNCTION           RESULTS AND EFFECTS           CORRECTIVE ACTION ON SAFE PLANT OPERATION 49687               HPCS Switchgear Room         Door seal is cracked.         Replace seal.                 Seal Replaced.
s TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 49687 HPCS Switchgear Room Door seal is cracked.
Replace seal.
Seal Replaced.
Water Tight door.
Water Tight door.
54665               2B RHR S/D Cooling         Valve binding.                 Repair                         Torque bonnet and stroked Check valve 2E12-                                                                         valve. No binding problem F050B                                                                                     observed.
54665 2B RHR S/D Cooling Valve binding.
61481               Remove indicated             Snubbers SC02-2808S and       Remove snubbers on piping sub- Snubbers eliminated due to mechanical snubbers         SC02-2805                     system 2SCO2                   reanalyze of subsystem.
Repair Torque bonnet and stroked Check valve 2E12-valve. No binding problem F050B observed.
61686               Reanalyze piping sub - Snubbers RH73-2003S 2004S, Remove snubbers                         Snubbers removed.
61481 Remove indicated Snubbers SC02-2808S and Remove snubbers on piping sub-Snubbers eliminated due to mechanical snubbers SC02-2805 system 2SCO2 reanalyze of subsystem.
system 2RH73 to             2005S, and 2006S, delete unnecessary snubbers.
61686 Reanalyze piping sub - Snubbers RH73-2003S 2004S, Remove snubbers Snubbers removed.
61942               Valve 2VP- 063B             Torque switch failed           suspect loose contact         Tightened loose torque switch contacts, valve cycle sat.
system 2RH73 to 2005S, and 2006S, delete unnecessary snubbers.
62600                 2A RHR SDC Return           Valve leaking                 'A' RHR discharge pressure     Disassembled, repaired Isolation Stop 2E12-                                       pressure slowly increases     and reassembled. Proper F053A                                                                                     operations observed.
61942 Valve 2VP- 063B Torque switch failed suspect loose contact Tightened loose torque switch contacts, valve cycle sat.
62888                 Drywell Oil Plug             Oil Plug on containment       Clean and inspect             Drain plug cleaned and Fitting                     wall is leaking                                               re-tapped.
62600 2A RHR SDC Return Valve leaking
63333                 HPCS Suction Isolation Test Valve under design             Fould faulty torque switch     Torque switch replaced.
'A' RHR discharge pressure Disassembled, repaired Isolation Stop 2E12-pressure slowly increases and reassembled. Proper F053A operations observed.
Valve                       conditions.                   502A05.
62888 Drywell Oil Plug Oil Plug on containment Clean and inspect Drain plug cleaned and Fitting wall is leaking re-tapped.
63550                 HPCS Water Leg Relief Remove relief valve and               Unit--2 Refuel Requirement     Valve removed and tested Valve 2E22-F014             test                                                         eatisfactorily.
63333 HPCS Suction Isolation Test Valve under design Fould faulty torque switch Torque switch replaced.
63697                 Fuel Zone Level             Chart drive does not           Repair                         Cleaned and aligned chart Recorder 2B21-R615           advance                                                       drive. Verified proper Ops.
Valve conditions.
502A05.
63550 HPCS Water Leg Relief Remove relief valve and Unit--2 Refuel Requirement Valve removed and tested Valve 2E22-F014 test eatisfactorily.
63697 Fuel Zone Level Chart drive does not Repair Cleaned and aligned chart Recorder 2B21-R615 advance drive. Verified proper Ops.
DOCUMENT ID 0036r/0005r
DOCUMENT ID 0036r/0005r


TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST   COMPONENT         CAUSE OF MALFUNCTION         RESULTS AND EFFECTS       CORRECTIVE ACTION ON SAFE PLANT OPERATION 63870       Accumulator 38--59 When full closed valve     Replace (111) cartridge   (111) - cartridge replaced 2Cll-D001--lll     leaks badly.
TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 63870 Accumulator 38--59 When full closed valve Replace (111) cartridge (111) - cartridge replaced 2Cll-D001--lll leaks badly.
64038       Accumulator 22-03 Packing leak               Replace (111) cartridge   Cartridge replaced.
64038 Accumulator 22-03 Packing leak Replace (111) cartridge Cartridge replaced.
64039       Accumulator 18-07 Packing leak               Replace (111) cartridge   Cartridge replaced.
64039 Accumulator 18-07 Packing leak Replace (111) cartridge Cartridge replaced.
64040       Accumulator 10-11 Packing leak               Replace (111) cartridge   Cartridge replaced.
64040 Accumulator 10-11 Packing leak Replace (111) cartridge Cartridge replaced.
64041       Accumulator 14-11 Packing leak               Replace (111) cartridge   Cartridge replaced.
64041 Accumulator 14-11 Packing leak Replace (111) cartridge Cartridge replaced.
i   64042       Accumulator 30-15 Packing leak               Replace (111) cartridge   Cartridge replaced.
i 64042 Accumulator 30-15 Packing leak Replace (111) cartridge Cartridge replaced.
64043       Accumulator 22-15 Packing leak               Replace (111) cartridge   Cartridge replaced.
64043 Accumulator 22-15 Packing leak Replace (111) cartridge Cartridge replaced.
64044       Accumulator 18- 15 Packing leak               Replace (111) cartridge   Cartridge replaced.
64044 Accumulator 18-15 Packing leak Replace (111) cartridge Cartridge replaced.
64045       Accumulator 10-15 Packing leak               Replace (111) cartr idge   Cartridge replaced.
64045 Accumulator 10-15 Packing leak Replace (111) cartr idge Cartridge replaced.
64046       Accumulator 02- 19 Packing leak               Replace (111) cartridge   Cartridge replaced.
64046 Accumulator 02-19 Packing leak Replace (111) cartridge Cartridge replaced.
I 64047       Accumulator 06-19 Packing leak               Replace (111) cartridge   Cartridge replaced.
I 64047 Accumulator 06-19 Packing leak Replace (111) cartridge Cartridge replaced.
64048       Accumulator 18--19 Packing leak               Replace (111) cartridge   Cartridge replaced.
64048 Accumulator 18--19 Packing leak Replace (111) cartridge Cartridge replaced.
64049       Accumulator 22 19 Packing leak               Replace (111) cartridge   Cartridge replaced.
64049 Accumulator 22 19 Packing leak Replace (111) cartridge Cartridge replaced.
64050       Accumulator 26-19 Packing leak               Replace (111) cartridge   Cartridge replaced.
64050 Accumulator 26-19 Packing leak Replace (111) cartridge Cartridge replaced.
64051       Accumulator 30-19 Packing leak               Replace (111) cartridge   Cartridge replaced.
64051 Accumulator 30-19 Packing leak Replace (111) cartridge Cartridge replaced.
64052       Accumulator 30- 23 Packing leak               Replace (111) cartridge   Cartridge replaced.
64052 Accumulator 30- 23 Packing leak Replace (111) cartridge Cartridge replaced.
64053       Accumulator 26-23 Packing leak               Replace (111) cartridge   Cartridge replaced.
64053 Accumulator 26-23 Packing leak Replace (111) cartridge Cartridge replaced.
DOCUMENT ID 0036r/0005r
DOCUMENT ID 0036r/0005r


I j
I TABLE 1 j
TABLE 1 i                                                                                                                   .
i CORRECTIVE MAINTENANCE OF l
CORRECTIVE MAINTENANCE OF l                                               SAFETY RELATED EQUIPMENT I
SAFETY RELATED EQUIPMENT I
Unit #2 i WORK REQUEST   COMPONENT         CAUSE OF MALFUNCTION               RESULTS AND EFFECTS       CORRECTIVE ACTION l                                                               ON SAFE PLANT OPERATION l 64054       Accumulator 10-23 Packing leak               Replace (111) cartridge         Cartridge replaced.
Unit #2 i
64056       Accumulator 06-31 Packing leak               Replace (111) cartridge         Cartridge replaced.
WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION l
64057       Accumulator 02-31 Packing leak               Replace (111) cartridge         Cartridge replaced.
ON SAFE PLANT OPERATION l
64058       Accumulator 02--35 Packing leak               Replace (111) cartridge         Cartridge replaced.
64054 Accumulator 10-23 Packing leak Replace (111) cartridge Cartridge replaced.
64059       Accumulator 14-35 Packing leak               Replace (111) cartridge         Cartridge replaced.
64056 Accumulator 06-31 Packing leak Replace (111) cartridge Cartridge replaced.
64060       Accumulator 18-35 Packing leak               Replace (111) cartridge         Cartridge replaced.
64057 Accumulator 02-31 Packing leak Replace (111) cartridge Cartridge replaced.
64061       Accumulator 02-39 Packing leak               Replace (111) cartridge         Cartridge replaced.
64058 Accumulator 02--35 Packing leak Replace (111) cartridge Cartridge replaced.
64062       Accumulator 06-43 Packing leak               Replace (111) cartridge         Cartridge replaced.
64059 Accumulator 14-35 Packing leak Replace (111) cartridge Cartridge replaced.
64063       Accumulator 10-43 Packing leak               Replace (111) cartridge         Cartridge replaced.
64060 Accumulator 18-35 Packing leak Replace (111) cartridge Cartridge replaced.
64064       Accumulator 26-47 Packing leak               Replace (111) cartridge         Cartridge replaced.
64061 Accumulator 02-39 Packing leak Replace (111) cartridge Cartridge replaced.
E4065       Accumulator 14-47 Packing leak               Replace (111) cartridge         Cartridge replaced.
64062 Accumulator 06-43 Packing leak Replace (111) cartridge Cartridge replaced.
64066       Accumulator 06-47 Packing leak               Replace (111) cartridge         Cartridge replaced.
64063 Accumulator 10-43 Packing leak Replace (111) cartridge Cartridge replaced.
64067       Accumulator 26-51 Packing leak               Replace (111) cartridge         Cartridge replaced.
64064 Accumulator 26-47 Packing leak Replace (111) cartridge Cartridge replaced.
64068       Accumulator 26-59 Packing leak               Replace (111) cartridge         Cartridge replaced.
E4065 Accumulator 14-47 Packing leak Replace (111) cartridge Cartridge replaced.
64104       Accumulator 38-43 Packing leak               Replace (111) cartridge         Cartridge replaced.
64066 Accumulator 06-47 Packing leak Replace (111) cartridge Cartridge replaced.
64105       Accumulator 58-43 Packing leak               Replace (111) cartridge         Cartridge replaced.
64067 Accumulator 26-51 Packing leak Replace (111) cartridge Cartridge replaced.
64106       Accumulator 54-43 Packing leak               Replace (111) cartr.dge         Cartridge replaced.
64068 Accumulator 26-59 Packing leak Replace (111) cartridge Cartridge replaced.
64104 Accumulator 38-43 Packing leak Replace (111) cartridge Cartridge replaced.
64105 Accumulator 58-43 Packing leak Replace (111) cartridge Cartridge replaced.
64106 Accumulator 54-43 Packing leak Replace (111) cartr.dge Cartridge replaced.
DOCUMENT ID 0036r/0005r
DOCUMENT ID 0036r/0005r


TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST     COMPONENT                                 CAUSE OF MALFUNCTION               RESULTS AND EFFECTS         CORRECTIVE ACTION ON SAFE PLANT OPERATION 64116         Damper Actuators for                     To prevent seals from de-       Remove / Replace Cylinders. Two (2) cylinders replaced 2VR04YB (2FZ-VR015)                       grading, vendor recommends                                   with new ones.
TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 64116 Damper Actuators for To prevent seals from de-Remove / Replace Cylinders.
Two (2) cylinders replaced 2VR04YB (2FZ-VR015) grading, vendor recommends with new ones.
air cylinders be replaced each refueling outage.
air cylinders be replaced each refueling outage.
264117       Damper actuators for                     To prevent seals from de--     Remove / Replace Cylinders. Two (2) cylinders replaced 2VR04YA (2FZ-VR014)                       grading, vendor recommends                                   with new ones.
264117 Damper actuators for To prevent seals from de--
Remove / Replace Cylinders.
Two (2) cylinders replaced 2VR04YA (2FZ-VR014) grading, vendor recommends with new ones.
air Cylinders be replaced each refueling outage.
air Cylinders be replaced each refueling outage.
264118       Damper actuators for                     To prevent seals from de-       Remove / Replace Cylinders. Two (2) cylinders replaced 2VR05YD (2FZ-VR002)                       grading, vendor recommends                                   with new ones.
264118 Damper actuators for To prevent seals from de-Remove / Replace Cylinders.
Two (2) cylinders replaced 2VR05YD (2FZ-VR002) grading, vendor recommends with new ones.
air cylindars be replaced each refueling outage.
air cylindars be replaced each refueling outage.
64141       Accumulator 42-55                         Packing leak                     Replace (111) Cartridge. Cartridge replaced.
64141 Accumulator 42-55 Packing leak Replace (111) Cartridge.
64142         Accumulator 42-51                         Packing leak                     Replace (111) Cartridge. Cartridge replaced.
Cartridge replaced.
64144         Accumulator 38-51                         Packing leak                     Replace (111) Cartridge. Cartridge replaced.
64142 Accumulator 42-51 Packing leak Replace (111) Cartridge.
64145         Accumulator 34-47                         Packing leak                     Replace (111) Cartridge. Cartridge replaced.
Cartridge replaced.
64146         Accumulator 42-47                         Packing leak                     Replace (111) Cartridge. Cartridge replaced.
64144 Accumulator 38-51 Packing leak Replace (111) Cartridge.
64147         Accumulator 46-47                         Packing leak                     Replace (111) Cartridge. Cartridge replaced.
Cartridge replaced.
64148         Accumulator 34-43                         Packing leak                     Replace (111) Cartridge. Cartridge replaced.
64145 Accumulator 34-47 Packing leak Replace (111) Cartridge.
64202         Accumulator 34-35                         Packing leak                     Replace (111) Cartridge. Cartridge replaced.
Cartridge replaced.
64248         Accumulator 42"27                         Packing leak                     Replace (111) Cartridge. Cartridge replaced.
64146 Accumulator 42-47 Packing leak Replace (111) Cartridge.
64249.       Accumulator 42-23                         Packing leak                     Replace (111) Cartridge. Cartridge replaced.
Cartridge replaced.
l l DOCUMENT ID 0036r/0005r
64147 Accumulator 46-47 Packing leak Replace (111) Cartridge.
Cartridge replaced.
64148 Accumulator 34-43 Packing leak Replace (111) Cartridge.
Cartridge replaced.
64202 Accumulator 34-35 Packing leak Replace (111) Cartridge.
Cartridge replaced.
64248 Accumulator 42"27 Packing leak Replace (111) Cartridge.
Cartridge replaced.
64249.
Accumulator 42-23 Packing leak Replace (111) Cartridge.
Cartridge replaced.
l l
DOCUMENT ID 0036r/0005r


TABLE 1
TABLE 1 I
* I f                                               CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT                                             .
f CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT CORRECTIVE ACTION Unit #2 RESULTS AND EFFECTS CAUSE OF MALFUNCTION WORK REQUEST COMPONENT ON SAFE PLANT OPERATION Cartridge replaced.
CORRECTIVE ACTION Unit #2                                               RESULTS AND EFFECTS COMPONENT            CAUSE OF MALFUNCTION WORK REQUEST                                                       ON SAFE PLANT OPERATION Cartridge replaced.
Replace (111) Cartridge.
Packing leak                  Replace (111) Cartridge.
64250 Accumulator 38--27 Packing leak Cartridge replaced.
64250       Accumulator 38--27                                                                 Cartridge replaced.
Replace (111) Cartridge.
Packing leak Replace (111) Cartridge.
UI251 Accumulator 34--27 Packing leak Cartridge replaced.
UI251       Accumulator 34--27                                                                 Cartridge replaced.
Replace (111) Cartridge.
Packing leak                  Replace (111) Cartridge.
64253 Accumulator 46-27 Packing leak Cartridge replaced.
64253       Accumulator 46-27                                                                   Cartridge replaced.
Replace (111) Cartridge.
Packing leak Replace (111) Cartridge.
64055 Accumulator 18-27 Packing leak Transmitter recalibrated Pressure gage damaged Reading full scale.
64055       Accumulator 18-27 Reading full scale.            Transmitter recalibrated RCIC Pressure Gage  Pressure gage damaged                                         and assured proper Ops.
and assured proper Ops.
64294 Set limimts and cycled Valve does not cycle.          Troubleshoot                   valve satisfactorily.
64294 RCIC Pressure Gage Set limimts and cycled Troubleshoot 64441
64441        *B* RHR S/D Cooling Test. Check Valve 2R12-F0508 Snap ring replaced.
*B* RHR S/D Cooling Valve does not cycle.
Yaglve 2E32-F002E Handwheel rises when valve Repair 64490                            is stroked, declutch lever does not work properly.
valve satisfactorily.
Troubleshoot Solenoid valve found off.
Test. Check Valve 2R12-F0508 Snap ring replaced.
RHR Testable Check   No indication of the                                           Reterminated and tested 64602                            Control Room.                                                 satisfactorily.
64490 Yaglve 2E32-F002E Handwheel rises when valve Repair is stroked, declutch lever does not work properly.
Valve 2E12-F050A Dirty or intermittent contacts Replaced relay 74Fl.
Solenoid valve found off.
Relay 74F1 at SVGR Relay not functioning.         on relay.
Troubleshoot Reterminated and tested 64602 RHR Testable Check No indication of the Valve 2E12-F050A Control Room.
64937 243 ACB 2433                                                                       Cartridge replaced.
satisfactorily.
Packing Leak                  Replace (111) Cartridge.
Dirty or intermittent contacts Replaced relay 74Fl.
65096       Accumulator 54--23                                                                 Cartridge replaced.
64937 Relay 74F1 at SVGR Relay not functioning.
Packing Leak                  Replace (111) Cartridge.
on relay.
65097       Accumulator 50 -23                                                                 Cartridge replaced.
243 ACB 2433 Cartridge replaced.
Packing Leak                  Replace (111) Cartridge.
Replace (111) Cartridge.
65098       Accumulator 50-19                                                                   Cartridge replaced.
65096 Accumulator 54--23 Packing Leak Cartridge replaced.
Packing Leak                  Replace (111) Cartridge.
Replace (111) Cartridge.
65099       Accumulator 34-15 DOCUMENT ID 0036r/0005r
65097 Accumulator 50 -23 Packing Leak Cartridge replaced.
Replace (111) Cartridge.
65098 Accumulator 50-19 Packing Leak Cartridge replaced.
Replace (111) Cartridge.
65099 Accumulator 34-15 Packing Leak DOCUMENT ID 0036r/0005r


TABLE 1 CORRECTIVE MAINTENANCE OF
TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT
                                                                                                                ~
~
SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST     COMPONENT         CAUSE OF MALFUNCTION           RESULTS AND EFFECTS       CORRECTIVE ACTION ON SAFE PLANT OPERATION 65100       Accumulator 34-19 Packing Leak               Replace (111) Cartridge. Cartridge replaced.
Unit #2 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 65100 Accumulator 34-19 Packing Leak Replace (111) Cartridge.
65101       Accumulator 38--15 Packing Leak               Replace (111) Cartridge. Cartridge replaced.
Cartridge replaced.
65102       Accumulator 50--15 Packing Leak               Replace (111) Cartridge,   Cartridge replaced.
65101 Accumulator 38--15 Packing Leak Replace (111) Cartridge.
65103       Accumulator 46-11 Packing Leak               Replace (111) Cartridge. Cartridge replaced.
Cartridge replaced.
65104       Accumulator 38--07 Packing Leak               Replace (111) Cartridge. Cartridge replaced.
65102 Accumulator 50--15 Packing Leak Replace (111) Cartridge, Cartridge replaced.
65105       Accumulator 42-07 Packing Leak               Replace (111) Cartridge. Cartridge replaced.
65103 Accumulator 46-11 Packing Leak Replace (111) Cartridge.
65106       Accumulator 34-03 Packing Leak               Replace (111) Cartridge. Cartridge replaced.
Cartridge replaced.
65107       Accumulator 42-03 Packing Leak               Replace (111) Cartridge. Cartridge replaced.
65104 Accumulator 38--07 Packing Leak Replace (111) Cartridge.
65319       Penetration E-26   Leak found at the input to Repair                     Repair leak and charged the flange.                                           to 30 lbs.
Cartridge replaced.
65368       FBCCW Otbd. Isol. Snap ring missing from     Replace                   Snap ring replaced.
65105 Accumulator 42-07 Packing Leak Replace (111) Cartridge.
Valve 2WR029       handwheel.
Cartridge replaced.
65371       RWCU Otbd. Isol. Valve failed L.L.R.T.       Repair                     Torque switch adjusted.
65106 Accumulator 34-03 Packing Leak Replace (111) Cartridge.
Valve 2G33-F004                                                           Proper Ops. observed.
Cartridge replaced.
65384       Valve 2E12-F041C   Valve does not cycle       Air cylinder leaks.       Replaced air cylinder and spring.
65107 Accumulator 42-03 Packing Leak Replace (111) Cartridge.
65553       MCC 235x--I       Contactor sticks           Repair                     Adjusted mechanical interlocks assured proper Cps, i
Cartridge replaced.
65319 Penetration E-26 Leak found at the input to Repair Repair leak and charged the flange.
to 30 lbs.
65368 FBCCW Otbd. Isol.
Snap ring missing from Replace Snap ring replaced.
Valve 2WR029 handwheel.
65371 RWCU Otbd. Isol.
Valve failed L.L.R.T.
Repair Torque switch adjusted.
Valve 2G33-F004 Proper Ops. observed.
65384 Valve 2E12-F041C Valve does not cycle Air cylinder leaks.
Replaced air cylinder and spring.
65553 MCC 235x--I Contactor sticks Repair Adjusted mechanical interlocks assured proper
: Cps, i
DOCUMENT ID 0036r/0005r
DOCUMENT ID 0036r/0005r


TABLE 1
TABLE 1 CORRECTIVE MAINTENANCE OF i
;                                                  CORRECTIVE MAINTENANCE OF i                                                   SAFETY RELATED EQUIPMENT 1
SAFETY RELATED EQUIPMENT 1
Unit #2 WORK REQUEST     COMPONENT             CAUSE OF MALFUNCTION           RESULTS AND EFFECTS           CORRECTIVE ACTION l
Unit #2 l
I                                                                    ON SAFE PLANT OPERATION l
WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION I
ON SAFE PLANT OPERATION l
l l
l l
l 67570       2H-IRM 2C51AZ009D     2H-IRM will not drive       Investigate -- Drive Cable     Reset the limits and out.                         insulation was worn allowing   repaired the insulation.
l 67570 2H-IRM 2C51AZ009D 2H-IRM will not drive Investigate -- Drive Cable Reset the limits and l
l l                                                                  water to drain through the     Assured proper Ops.
out.
insulation was worn allowing repaired the insulation.
l water to drain through the Assured proper Ops.
drive cable, into the gear box.
drive cable, into the gear box.
65735       RHR Heat Exchanger     Torque Switch contacts       Internal mechanical problem. Replaced worm and worm Shell Side Bypass     make after torquing out.                                     gear. Verified proper 2E12-F048B                                                                         Ops.
65735 RHR Heat Exchanger Torque Switch contacts Internal mechanical problem.
65957       RHR S/D Cooling Vlv   Stem is leaking water.       Repack                         Valve repacked.
Replaced worm and worm Shell Side Bypass make after torquing out.
2E12-F006A 66050       HPCS p.p. Breaker     Nylon bushings for Cam       Replace                         Removed and replaced nylon 2E22-C001             shaft bearings are badly                                     bushings.
gear. Verified proper 2E12-F048B Ops.
65957 RHR S/D Cooling Vlv Stem is leaking water.
Repack Valve repacked.
2E12-F006A 66050 HPCS p.p. Breaker Nylon bushings for Cam Replace Removed and replaced nylon 2E22-C001 shaft bearings are badly bushings.
frayed.
frayed.
66109       RHR Pump Min Flow     Stem end of viv operator. Replaced                       Missing bolts have been bypass viv 2E12-F064C Missing bolts and lock--                                     replaced, washers.
66109 RHR Pump Min Flow Stem end of viv operator.
66164       Flange Upstream of     Flange leaking when         Repair - Torque as needed.     Bolts not torqued as re--
Replaced Missing bolts have been bypass viv 2E12-F064C Missing bolts and lock--
2E12- F003B           pressure testing.                                           quired. Cleaned faces of flange and torqued to 750 Ft. Lbs.
: replaced, washers.
66211       valve 2B21-N020D       Valve Leaks                 Repair                         Valve repaired and Q.C.
66164 Flange Upstream of Flange leaking when Repair - Torque as needed.
Bolts not torqued as re--
2E12-F003B pressure testing.
quired. Cleaned faces of flange and torqued to 750 Ft. Lbs.
66211 valve 2B21-N020D Valve Leaks Repair Valve repaired and Q.C.
Inspected for no leaks.
Inspected for no leaks.
66212       Mechanical Snubber     Damaged Snubber             Replace                         Damaged snubber replaced MSO4-2794-S                                                                         with a new one.
66212 Mechanical Snubber Damaged Snubber Replace Damaged snubber replaced MSO4-2794-S with a new one.
66213       Mechaalcal Snubber     Damaged Snubber             Replace                         Damaged snubber replaced MS00 2013-S                                                                         with a new one.
66213 Mechaalcal Snubber Damaged Snubber Replace Damaged snubber replaced MS00 2013-S with a new one.
66214       Mechanical Snubber     Damaged Snubber             Replace                         Damaged snubber replaced MS06-2004-S                                                                         with a new one.
66214 Mechanical Snubber Damaged Snubber Replace Damaged snubber replaced MS06-2004-S with a new one.
DOCUMENT ID 0036r/0005r
DOCUMENT ID 0036r/0005r


      -.                -        - _.                -      -  ~
~
TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST   COMPONENT             CAUSE OF MALFUNCTION           RESULTS AND EFFECTS       CORRECTIVE ACTION l                                                                     ON SAFE PLANT CPERATION 66215       Mechanical Snubber     Damaged Snubber               Replace                   Damaged snubber replaced M334-2810-S                                                                     with a new one.
TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION l
66216       Mechanical Snubber     Damaged Snubber               Replace                   Damaged snubber replaced MS04-2645-S                                                                     with a new one.
ON SAFE PLANT CPERATION 66215 Mechanical Snubber Damaged Snubber Replace Damaged snubber replaced M334-2810-S with a new one.
i 66217       Mechanical Snubber     Damaged Snubber               Replace                   Damaged snubber replaced MSO4-2808-S                                                                     with a new one.
66216 Mechanical Snubber Damaged Snubber Replace Damaged snubber replaced MS04-2645-S with a new one.
66218       Mechanical Snubber     Damaged Snubber               Replace with new snubber. Damaged snubber replaced.
i 66217 Mechanical Snubber Damaged Snubber Replace Damaged snubber replaced MSO4-2808-S with a new one.
LC01-2967-S 66409       2E31- F005B4           Broken Flex on 2LD184.       Determ Cable and repair. Flex repaired and cable reterminated.
66218 Mechanical Snubber Damaged Snubber Replace with new snubber.
66420       2E12-F050B             Broken Flex on Cable 2RH253 Determ cable and repair. Flex repaired and cable reterminated.
Damaged snubber replaced.
66459       2E12-F041C Actuator   Wiring to Solenald are       Replace                   Replaced Solenoid Valve twisted and appear heat                                 Coll, cable and sealtite.
LC01-2967-S 66409 2E31-F005B4 Broken Flex on 2LD184.
Determ Cable and repair.
Flex repaired and cable reterminated.
66420 2E12-F050B Broken Flex on Cable 2RH253 Determ cable and repair.
Flex repaired and cable reterminated.
66459 2E12-F041C Actuator Wiring to Solenald are Replace Replaced Solenoid Valve twisted and appear heat Coll, cable and sealtite.
damaged.
damaged.
66587       Accumulator 50-23     Solenoid Blowing Air         Repair                     Bonnet screws loose.
66587 Accumulator 50-23 Solenoid Blowing Air Repair Bonnet screws loose.
Retorqued to 120 inch-lbs.
Retorqued to 120 inch-lbs.
66612       3/4" Flex conduit at   Conduit damaged               Replace                   Replaced damaged flex.
66612 3/4" Flex conduit at Conduit damaged Replace Replaced damaged flex.
2E22-S001 66720       Mechanical Snubber     Damaged Snubber.             ' Replace snubber           Damage snubber replaced M204-2711-S                                                                     with a new one.
2E22-S001 66720 Mechanical Snubber Damaged Snubber.
66755       Rx. Vessel Shroud     Transmitter does not re-     Replace                   New transmitter installed Level Transmitter     spond to test inputs.                                   and calibrated.
' Replace snubber Damage snubber replaced M204-2711-S with a new one.
2B21-N044B l DOCUMENT ID 0036r/0005r
66755 Rx. Vessel Shroud Transmitter does not re-Replace New transmitter installed Level Transmitter spond to test inputs.
and calibrated.
2B21-N044B l
l DOCUMENT ID 0036r/0005r


TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST   COMPONENT               CAUSE Ot7 MALFUNCTION           RESULTS AND EFFECTS       CORRECTIVE ACTION ON SAFE PLANT OPERATION 66774       Div I Battery Gnd. Alarm sounds whenever viv     Troubleshoot and repair. Removed limitorque cover Alarm                 2E12-F006A is open                                       and found pinched wire between body and cover.
TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST COMPONENT CAUSE Ot7 MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 66774 Div I Battery Gnd.
Alarm sounds whenever viv Troubleshoot and repair.
Removed limitorque cover Alarm 2E12-F006A is open and found pinched wire between body and cover.
Repair and assured proper Ops.
Repair and assured proper Ops.
66830       Valve 2E12-F026A     No light indication in         Bad Relay                 Replaced relay and assured Control Room.                                             proper Ops.
66830 Valve 2E12-F026A No light indication in Bad Relay Replaced relay and assured Control Room.
66848       Fuse Holder for 2E22- Side broken out of fuse       Replace holder             Replaced fuse holder C001                 Block.
proper Ops.
66885       Mechanical Snubber   Snubber damaged               Replace snubber           Snubber replaced.
66848 Fuse Holder for 2E22-Side broken out of fuse Replace holder Replaced fuse holder C001 Block.
RH27-2003-S 66935       CRD HCU 34-39         Blowing Air from gaskets       Check torque               Tightened union above l
66885 Mechanical Snubber Snubber damaged Replace snubber Snubber replaced.
RH27-2003-S 66935 CRD HCU 34-39 Blowing Air from gaskets Check torque Tightened union above l
scram valve.
scram valve.
l   66968       HPCS Pump Disch.     Threads on body of trans-     Replace transmitter.       Transmitter replaced and l               Pressure Indicator   mitter are gone.                                         calibrated.
l 66968 HPCS Pump Disch.
2E22- N004 I   67003       Directional Control   Valve is leaking water         Repair leak               Leak repaired.
Threads on body of trans-Replace transmitter.
l               Valve Solenoid 123 HCU 26-59 l
Transmitter replaced and l
67016       Mechanical Snubber   Snubber damaged               Replace snubber           Snubber replaced with new RIA2 2999-S                                         one.
Pressure Indicator mitter are gone.
67076       HCU 58-35             Scram Pilot Solenoid has a Rebuild 118 Viv.               Rebuilt 118 Valve.
calibrated.
2E22-N004 I
67003 Directional Control Valve is leaking water Repair leak Leak repaired.
l Valve Solenoid 123 l
HCU 26-59 67016 Mechanical Snubber Snubber damaged Replace snubber Snubber replaced with new RIA2 2999-S one.
67076 HCU 58-35 Scram Pilot Solenoid has a Rebuild 118 Viv.
Rebuilt 118 Valve.
blown diaphragm.
blown diaphragm.
67129       RHR B/C Water Leg     Control relay contacts are Repair / replace               Cleaned relay contact and
67129 RHR B/C Water Leg Control relay contacts are Repair / replace Cleaned relay contact and Pump 2E12-C003 intermittent.
!                Pump 2E12-C003       intermittent.                                             verified proper ops.
verified proper ops.
DOCUMENT ID 0036r/0005r
DOCUMENT ID 0036r/0005r


l l
l l
l                                                               TABLE 1 l
l TABLE 1 l
l                                                   CORRECTIVE MAINTENANCE OF l                                                     SAFETY RELATED EQUIPMENT 1
l CORRECTIVE MAINTENANCE OF l
i l                 Unit #2 WORK REQUEST     COMPONENT             CAUSE OF MALFUNCTION             RESULTS AND EFFECTS       CORRECTIVE ACTION l                                                                        ON SAFE PLANT OPERATION 67131       RHR Heat Exchanger A   Overload Relay would not       Repair / Replace           Overload relay replaced.
SAFETY RELATED EQUIPMENT 1
Discharge 2E12--F068A   trip when tested.
i l
67188       RHR S/D Cooling Inj. Breaker contacts show           Replace                   Replaced breaker for a new valve 2E12-F053A       evidence of pitting / mis-                                 one.
Unit #2 l
WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 67131 RHR Heat Exchanger A Overload Relay would not Repair / Replace Overload relay replaced.
Discharge 2E12--F068A trip when tested.
67188 RHR S/D Cooling Inj.
Breaker contacts show Replace Replaced breaker for a new valve 2E12-F053A evidence of pitting / mis-one.
alignment.
alignment.
l l 67194       Supp. Pool Temp         Reading Downscale               Troubleshoot               Replaced wiring harness.
l l
Monitoring Recorder 2TR-CM037 67350       2E12-F020               Loose Limit Switch Arm on       Repa?r                     Tightened limit switch the valve stem.                                           actuating arm. Verified proper ops.
67194 Supp. Pool Temp Reading Downscale Troubleshoot Replaced wiring harness.
67368       HCU 42-03               Packing Leak                   Replace (113) cartridge. Cartridge replaced.
Monitoring Recorder 2TR-CM037 67350 2E12-F020 Loose Limit Switch Arm on Repa?r Tightened limit switch the valve stem.
67496       HPCS Water Leg Pump     Does not hold pressure.         Repair                     Lapped seat, reassembled Check Valve                                                                       and seal welded bonnet.
actuating arm. Verified proper ops.
67368 HCU 42-03 Packing Leak Replace (113) cartridge.
Cartridge replaced.
67496 HPCS Water Leg Pump Does not hold pressure.
Repair Lapped seat, reassembled Check Valve and seal welded bonnet.
l l
l l
l I
l I
Line 555: Line 764:
DOCUMENT ID 0036r/0005r i
DOCUMENT ID 0036r/0005r i


.  . .                                      TABLE 2 COMPLETED SAFETY RELATED MODIFICATIONS MODIFICATION NUMBER: A brief Synopsis of Incorporated Modification Objectives with final design resolution. Also, state reviewed or unreviewed safety questions.
TABLE 2 COMPLETED SAFETY RELATED MODIFICATIONS MODIFICATION NUMBER: A brief Synopsis of Incorporated Modification Objectives with final design resolution. Also, state reviewed or unreviewed safety questions.
UNIT TWO M-1-2-82-014             This Modification was to remove a G.E. pushbutton and control switches located in the Diesel Generator 2A engine gauge panel from the engine skid to meet NRC requirements.
UNIT TWO M-1-2-82-014 This Modification was to remove a G.E. pushbutton and control switches located in the Diesel Generator 2A engine gauge panel from the engine skid to meet NRC requirements.
There were no unreviewed safety questions.
There were no unreviewed safety questions.
M-1-2-83-012             This Modification was to implement the Electrical Maintenance Department M.I. 9644 lube oil system change on the '2B' diesel generator. This will improve the oil circulating subsystem which supplies ol' to the engine for emergency starts. There were no unreviewed safety questions.
M-1-2-83-012 This Modification was to implement the Electrical Maintenance Department M.I. 9644 lube oil system change on the '2B' diesel generator. This will improve the oil circulating subsystem which supplies ol' to the engine for emergency starts. There were no unreviewed safety questions.
M-1-2-84-110             This Modification was for the addition of new pressure switches and also new relays for the low RHR pump discharge pressure alarms and the engineered safety feature status.
M-1-2-84-110 This Modification was for the addition of new pressure switches and also new relays for the low RHR pump discharge pressure alarms and the engineered safety feature status.
There were no unreviewed safety features.
There were no unreviewed safety features.
M-1-2-84-111             This modification was to install a Thermowell in the RHR Shutdown cooling line 2RH04C-20. There were no unreviewed safety questions.
M-1-2-84-111 This modification was to install a Thermowell in the RHR Shutdown cooling line 2RH04C-20. There were no unreviewed safety questions.
M-1-2-84-129             This modification was to separate the High/ Low pressure alarms in the LPCS pump discharge pressure switches. There were no unreviewed safety questions.
M-1-2-84-129 This modification was to separate the High/ Low pressure alarms in the LPCS pump discharge pressure switches. There were no unreviewed safety questions.
M-1-2-85-049             This modification was for the replacement of the GE Model NA-200 Local Power Range Monitors (LPRM's) with the Westinghouse model WL-24286 LPRM. There were no unreviewed safety questions.
M-1-2-85-049 This modification was for the replacement of the GE Model NA-200 Local Power Range Monitors (LPRM's) with the Westinghouse model WL-24286 LPRM. There were no unreviewed safety questions.
M-1-2-86-039             This modification was to add a high point vent to the existing piping of the RHR system on line 2RH41AA-3" and 2RH70A-3". There were no unreviewed safety questions.
M-1-2-86-039 This modification was to add a high point vent to the existing piping of the RHR system on line 2RH41AA-3" and 2RH70A-3".
M-1-2-86-041             This modification was to add a high point vent to the existing piping of the RHR system in line 2RH038B-12".
There were no unreviewed safety questions.
M-1-2-86-041 This modification was to add a high point vent to the existing piping of the RHR system in line 2RH038B-12".
There were no unreviewed safety questions.
M-1-2-86-042 This modification was to add a high point vent to the existingpiping of the RHR system on lines 2RH03BA-12" and 2RH34A-6".
There were no unreviewed safety questions.
There were no unreviewed safety questions.
M-1-2-86-042            This modification was to add a high point vent to the existingpiping of the RHR system on lines 2RH03BA-12" and 2RH34A-6". There were no unreviewed safety questions.
DOCUMENT ID 0036r/0005r
DOCUMENT ID 0036r/0005r


        . *. .                                      TABLE 2 (cont'd)
TABLE 2 (cont'd)
COMPLETED SAFETY RELATED MODIFICATIONS MODIFICATION NUMBER: A brief Synopsis of Incorporated Modification Objectives with final design resolution. Also, state reviewed or unreviewed safety questions.
COMPLETED SAFETY RELATED MODIFICATIONS MODIFICATION NUMBER: A brief Synopsis of Incorporated Modification Objectives with final design resolution. Also, state reviewed or unreviewed safety questions.
M-1-2-86-050                   This mod was to add a redundant contact from a different relay in series with the existing contact. This will prevent a single short of a relay from operating the pilot valve. There were no unreviewed safety questions.
M-1-2-86-050 This mod was to add a redundant contact from a different relay in series with the existing contact. This will prevent a single short of a relay from operating the pilot valve. There were no unreviewed safety questions.
M-1-2-86-053                   This modification was part of the snubber reduction program for subsystem 2SC02. There were no unreviewed safety questions.
M-1-2-86-053 This modification was part of the snubber reduction program for subsystem 2SC02. There were no unreviewed safety questions.
M-1-2-86-054                   This modification was part of the snubber reduction program for subsystem 2RIO3. There were no unreviewed safety questions.
M-1-2-86-054 This modification was part of the snubber reduction program for subsystem 2RIO3. There were no unreviewed safety questions.
M-1-2-86-058                   This modification was part of the snubber reduction program for subsystem 2RRC2. There were no unreviewed safety questions.
M-1-2-86-058 This modification was part of the snubber reduction program for subsystem 2RRC2. There were no unreviewed safety questions.
M-1-2-86-060                   This modification was part of the snubber reduction program for subsystem 2RRA9. There were no unreviewed safety questione.
M-1-2-86-060 This modification was part of the snubber reduction program for subsystem 2RRA9. There were no unreviewed safety questione.
M-1-2-86-061                   This modification was part of the snubber reduction program for subsystem 2MS648. There were no unreviewed safety questions.
M-1-2-86-061 This modification was part of the snubber reduction program for subsystem 2MS648. There were no unreviewed safety questions.
M-1-2-86-066                   This modification was part of the snubber reduction program for subsystem 2MS64F. There were no unreviewed safety questions.
M-1-2-86-066 This modification was part of the snubber reduction program for subsystem 2MS64F. There were no unreviewed safety questions.
;        M-1-2-86-068                   This mexlification was part of the snubber reduction program for subsystem 2RHBl. There were no unreviewed safety questions.
M-1-2-86-068 This mexlification was part of the snubber reduction program for subsystem 2RHBl. There were no unreviewed safety questions.
M-1-2-86-069                   This modification was part of the snubber reduction program for subsystem 2RRC7A. There were no unreviewed safety features.
M-1-2-86-069 This modification was part of the snubber reduction program for subsystem 2RRC7A. There were no unreviewed safety features.
M-1-2-86-071                   This modification was part of the snubber reduction program for subsystem 2HpA1. There were no unreviewed safety                         )
M-1-2-86-071 This modification was part of the snubber reduction program for subsystem 2HpA1. There were no unreviewed safety questions.
questions.                                                                   l M-1-2-86-078                   This modification was part of the snubber reduction program for subsystem 2MS258. There were no unreviewed safety questions.
l M-1-2-86-078 This modification was part of the snubber reduction program for subsystem 2MS258. There were no unreviewed safety questions.
l l
I DOCUMENT ID 0036r/0005r
I DOCUMENT ID 0036r/0005r l


r                                                   -
r i
i 1
1 e *. s TABLE 2 (cont'd)
e *. s TABLE 2 (cont'd)
COMPLETED SAFETY RELATED MODIFICATIONS MODIFICATION NUMBER: A brief Synopsis of Incorporated Modification Objectives with final design resolution. Also, state reviewed or unreviewed safety questions.
COMPLETED SAFETY RELATED MODIFICATIONS MODIFICATION NUMBER: A brief Synopsis of Incorporated Modification Objectives with final design resolution. Also, state reviewed or unreviewed safety questions.
M-1-2-86-085             This modification was to remove the existing Static-o-Ring level switch and replace it with a qualified Barton Level switch. There were no unreviewed safety questions.
M-1-2-86-085 This modification was to remove the existing Static-o-Ring level switch and replace it with a qualified Barton Level switch. There were no unreviewed safety questions.
l DOCUMENT ID 0036r/0005r
l DOCUMENT ID 0036r/0005r


                                                                ,                  o. o C.       LICENSEE EVENT REPORTS The following is a tabular summary of all licensee event reports for LaSalle Nuclear Power Station, Unit Two, logged during the reporting I
o.
o C.
LICENSEE EVENT REPORTS The following is a tabular summary of all licensee event reports for LaSalle Nuclear Power Station, Unit Two, logged during the reporting I
period, April 01, through April 30, 1987. This information is provided pursuant to the reportable occurrence reporting requirements as set forth in 10CPR 50.73.
period, April 01, through April 30, 1987. This information is provided pursuant to the reportable occurrence reporting requirements as set forth in 10CPR 50.73.
Licensee Event Report Number   Date     I.itle of Occurrence 87-005-00                       4/2/87   Auto start of 2B D/G during testing.
Licensee Event Report Number Date I.itle of Occurrence 87-005-00 4/2/87 Auto start of 2B D/G during testing.
87-006-00                       4/2/87   Group II pCIS Isolation during Mod Test.
87-006-00 4/2/87 Group II pCIS Isolation during Mod Test.
87-007-00                       4-12-87   Group II Isolation during 1
87-007-00 4-12-87 Group II Isolation during 1
testing due to failed 2C71-K4Dl.
testing due to failed 2C71-K4Dl.
i
i 87-008-00 4-14-87 Scram Signal while moving mode l
;                                                                              87-008-00                       4-14-87   Scram Signal while moving mode l                                                                                                                         switch due to blown fuses.
switch due to blown fuses.
i 87-009-00                       4-15-87   ESP Actuation during LLRT due to leakage past stop valve.
i 87-009-00 4-15-87 ESP Actuation during LLRT due to leakage past stop valve.
i 87-010-00                       4-17-87   Scram Signal while defueled/ contractor bumped APRM Cable under RPV.
i 87-010-00 4-17-87 Scram Signal while defueled/ contractor bumped APRM Cable under RPV.
87-011-00                       4-30-87   Static 'O' Ring differential                                                       i pressure switch out.
87-011-00 4-30-87 Static 'O' Ring differential i
pressure switch out.
i 1
i 1
i                                                                                                                                                                                                            !
l 1
i I
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l 1
DOCU:1ENT ID 0036r/0005r
:                                                                              DOCU:1ENT ID 0036r/0005r


l 1
1 D.
l D. DATA TABULATIONS The following data tabulations are presented in this report:
DATA TABULATIONS The following data tabulations are presented in this report:
: 1. Operating Data Report
: 1. Operating Data Report
: 2. Average Daily Unit Power Level
: 2. Average Daily Unit Power Level
: 3. Unit shutdowns and Power Reductions i
: 3. Unit shutdowns and Power Reductions i
I             DOCUMENT ID 0036r/0005r i
I DOCUMENT ID 0036r/0005r i
_ _ _ -      _            _____  ,    . - ~ - - .      - . -    _    , _ _ . _ . - _ _ _ _ _ - . _ _.                _ - - _ . _ _ _
- ~ -


  . a.     ,
a.
: 1. OPERATING DATA REPORT DOCKET NO. 050-374 UNIT ],aSalle Two DATE May 10. 1987 COMPLETED BY Gregory Kirchner TELEPHONE (815)357-6761 MONTH     APRIL 1987 OPERATING STATUS f
: 1. OPERATING DATA REPORT DOCKET NO. 050-374 UNIT ],aSalle Two DATE May 10. 1987 COMPLETED BY Gregory Kirchner TELEPHONE (815)357-6761 MONTH APRIL 1987 OPERATING STATUS f
: 1.       REPORTING PERIOD:     April, 1987 GROSS IlOURS IN REPORTING PERIOD: 719
1.
: 2.       CURRENTLY AUT140RIZED POWER LEVEL (MWt):3323 MAX DEPEND CAPACITY (MWe-Net): 1036   DESIGN ELECTRICAL RATING (MWe-Net): 1078,
REPORTING PERIOD:
: 3.       POWER LEVEL TO WiiICH RESTRICTt!D (IF PNY) (MWe-Net):     1050
April, 1987 GROSS IlOURS IN REPORTING PERIOD: 719 2.
: 4.       REASONS FOR RESTRICTION (IP ANY); Administrative TilIS MONTH YR TO DATE . CUMULATIVE 5         NUMBER OF llOURS REACTOR WAS CRITICAL       0.0         66.05     'l"069.5
CURRENTLY AUT140RIZED POWER LEVEL (MWt):3323 MAX DEPEND CAPACITY (MWe-Net): 1036 DESIGN ELECTRICAL RATING (MWe-Net): 1078, 3.
: 6.       REACTOR RESERVE SHUTDOWN }{OURS             0.0           0.0         29.83
POWER LEVEL TO WiiICH RESTRICTt!D (IF PNY) (MWe-Net):
: 7.       HOURS GENERATOR ON LINE                     0.0         59.92     11830.84
1050 4.
REASONS FOR RESTRICTION (IP ANY); Administrative TilIS MONTH YR TO DATE. CUMULATIVE 5
NUMBER OF llOURS REACTOR WAS CRITICAL 0.0 66.05
'l"069.5 6.
REACTOR RESERVE SHUTDOWN }{OURS 0.0 0.0 29.83 7.
HOURS GENERATOR ON LINE 0.0 59.92 11830.84
]
]
: 8.       UNIT RESERVE SHUTDOWN llOURS               0.0           0.0         0.0
8.
: 9.       GROSS TIIERMAL ENERGY GENERATED (MWil)     0.0       120864     23635128
UNIT RESERVE SHUTDOWN llOURS 0.0 0.0 0.0 9.
: 10.       GROSS ELEC. ENERGY GENERATED (MWH)         0.0         39232     11100804
GROSS TIIERMAL ENERGY GENERATED (MWil) 0.0 120864 23635128 10.
: 11.       NET ELEC. ENERGY GENERATED (MWil)       -7324             4757     10544986
GROSS ELEC. ENERGY GENERATED (MWH) 0.0 39232 11100804 11.
: 12.       REACTOR SERVICE FACTOR                         0%     2.2%           53.3%
NET ELEC. ENERGY GENERATED (MWil)
: 13.       REACTOR AVAILABILITY FACTOR                   0%     2.2%           54.5%
-7324 4757 10544986 12.
: 14.       UNIT SERVICE FACTOR                           0%     2.1.%         53%
REACTOR SERVICE FACTOR 0%
: 15.       UNIT AVAILABILITY FACTOR                       Q1     2.1.%         53%
2.2%
: 16.       UNIT CIPACITY FACTOR (USING MDC)         -0.9%       0.16%       __.45,81_
53.3%
: 17.       UNIT CAPACITY FACTOR (USING DESIGN MWe)                                     -0.9%         0.15%           44%
13.
18.       UNIT FORCED OUTAGE RATE                     0%           0%         26.2%
REACTOR AVAILABILITY FACTOR 0%
: 19.       bHUTDOWNS SCllEDULED OVER NEXT 6 MONTilS (TYPE, DATE, AND DURATION OF EACH):
2.2%
54.5%
14.
UNIT SERVICE FACTOR 0%
2.1.%
53%
15.
UNIT AVAILABILITY FACTOR Q1 2.1.%
53%
16.
UNIT CIPACITY FACTOR (USING MDC)
-0.9%
0.16%
__.45,81_
17.
UNIT CAPACITY FACTOR (USING DESIGN MWe)
-0.9%
0.15%
44%
18.
UNIT FORCED OUTAGE RATE 0%
0%
26.2%
19.
bHUTDOWNS SCllEDULED OVER NEXT 6 MONTilS (TYPE, DATE, AND DURATION OF EACH):
N/A Unit is in shutdown during this period.
N/A Unit is in shutdown during this period.
: 20.       IF S!!UT DOVN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP 5/30/87 I
20.
l I
IF S!!UT DOVN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP 5/30/87 l
l i
DOCUMENT ID 0036r/0005r l
I DOCUMENT ID 0036r/0005r                                                                     l l
1
1


r                                                                                                                                                                               1
r 1
      ~1
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: 2. AVERAGE DAILY UNIT POWER LEVEL' DOCKET NO: 050-374                                           '
: 2. AVERAGE DAILY UNIT POWER LEVEL' DOCKET NO: 050-374 UNIT: ' LASALLE 'i'WO DATE: May 10. 1987 COMPLETED BY: Gregory Kirchner TELEPHONE: (815) 357-6761 MONTH: April 1987 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
UNIT: ' LASALLE 'i'WO DATE: May 10. 1987 COMPLETED BY: Gregory Kirchner TELEPHONE: (815) 357-6761 MONTH: April 1987 DAY AVERAGE DAILY POWER LEVEL                               DAY AVERAGE DAILY POWER LEVEL                                                                           l (MWe-Net)                                                                       (MWe-Net)                                                                 l 4
(MWe-Net) 4 l
l
1.
: 1.           -8                                           17.                                 -10
-8 17.
: 2. -         -9                                           18.                                 -9 3             -10                                           19.                                 -9
-10
: 4.           -10                                           20.                                 -9
: 2. -
: 5.           -9                                           21.                                 -9
-9 18.
: 6.           -9                                           22.                                 -9'
-9 3
: 7.           -10                                           23.                                 -11
-10 19.
: 8.           -9                                           24.                                 -13 s
-9 4.
: 9.           -10                                           25.                                 -
-10 20.
12
-9 5.
: 10.           -10                                           26.                                 -
-9 21.
14
-9 6.
: 11.           -9                                           27.                                 r14
-9 22.
: 12.           -8                                           28.                                 -
-9' 7.
14                                                     >
-10 23.
: 13.           -8                                           29.                                 -14
-11 8.
: 14.           -7                                           30.                                 -14
-9 24.
: 15.           -8                                           31.                                 ---
-13 s
: 16.           -10 f                           I I
9.
l DOCUMENT ID 0036r/000Sr
-10 25.
                                    %,y.,--, --, , - -w-_m_ .-
12 10.
                                                                .,...#,,,p,,     , , . . . . ,  ,-.-. y. , , ._  _,.-_..,.-,,,.~,%., _    , .
-10 26.
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14 11.
: 3. UNIT SHUTDOWNS AND POWER REDUC' CIONS
-9 27.
                                                                                                                                                      . DOCKET NO. 050-374-UNIT NAME LaSalle Tt_oo ,        ,
r14 12.
DATE           May 10, 1987 REPORT MONTH                   April, 1987                                     COMPLETED BY G.J. Kircfaner TELEPHONE (815)357-6761 METHOD OF TYPE                                                                         SHUTTING DOWN F: FORCED                 DURATION                                               THE REACTOR OR                     CORRECTIVE
-8 28.
;      NO.       DATE           S: SCHEDULED                   (HOURS)           REASON                         REDUCING POWER                     ACTIONS / COP 9fENTS a
14 13.
:      1         4/1/87         S                           719                     C                             1                                   Refuel i
-8 29.
J 1
-14 14.
-7 30.
-14 15.
-8 31.
16.
-10 f
I I
DOCUMENT ID 0036r/000Sr
%,y.,--,
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.,...#,,,p,,
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: y.,,._
 
3.
UNIT SHUTDOWNS AND POWER REDUC' CIONS
. DOCKET NO. 050-374-UNIT NAME LaSalle Tt_oo,
DATE May 10, 1987 REPORT MONTH April, 1987 COMPLETED BY G.J. Kircfaner TELEPHONE (815)357-6761 METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR OR CORRECTIVE NO.
DATE S: SCHEDULED (HOURS)
REASON REDUCING POWER ACTIONS / COP 9fENTS a
1 4/1/87 S
719 C
1 Refuel i
J l
1 i
?
+
+
1 i
1 i
i 1                                                                                                                                                                                       !
t i
1 I
i l
I i
I i
I 2
I 2
1 l
1 l
DOCUMENT ID 0036r/0005r i
DOCUMENT ID 0036r/0005r i
__            _            . _ _    , _ _ . - . _      ._        ~. _              _      - _ _  - - . .          _          .        _ _ . _ .      .        _
~.


p l
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i s .. s E. UNIQUE REPORTING REQUIREMENTS
i s.. s E.
: 1.     Safety / Relief Valve Operations for Unit Two.
UNIQUE REPORTING REQUIREMENTS 1.
DATE         VALVES         NO & TYPE       PLANT         DESCRIPTION ACTUATED       ACTUATIONS     CONDITION     OF EVENT There were no safety relief valves operated for Unit #2 during this reporting period.
Safety / Relief Valve Operations for Unit Two.
l l
DATE VALVES NO & TYPE PLANT DESCRIPTION ACTUATED ACTUATIONS CONDITION OF EVENT There were no safety relief valves operated for Unit #2 during this reporting period.
DOCUMENT ID 0026r/0005r
DOCUMENT ID 0026r/0005r


e
e J.
  . . J. ECCS Systcm3 Outcg:s The following outages were taken on ECCS Systems during the reporting period.
ECCS Systcm3 Outcg:s The following outages were taken on ECCS Systems during the reporting period.
OUTAGE NO.         ROUIPMENT                     PURPOSE OF OUTAGE 2-1036-87         2E12-C300D                     Prevent use of motor which is torn apart.
OUTAGE NO.
2-1044-87         2HG-006A                       Rebuild 2HG006A.
ROUIPMENT PURPOSE OF OUTAGE 2-1036-87 2E12-C300D Prevent use of motor which is torn apart.
2-1047-87         2E12-F092B                     Prevent inadvertantly filling the reactor.
2-1044-87 2HG-006A Rebuild 2HG006A.
2-1048-87         D/G 2B - Soak Back oil pump   Replace damaged flex.
2-1047-87 2E12-F092B Prevent inadvertantly filling the reactor.
2-1051-87         2B D/G                         Calibrate relays.
2-1048-87 D/G 2B - Soak Back oil pump Replace damaged flex.
2-1056-87         2E51-F064                     Perform E.Q. Inspection.
2-1051-87 2B D/G Calibrate relays.
2-1063-87         2A D/G                         Replace Air Start motors.
2-1056-87 2E51-F064 Perform E.Q. Inspection.
2-1069-87         RCIC Turbine Trip Throttle     Replace Packing bushing.
2-1063-87 2A D/G Replace Air Start motors.
2-1070-87         2E12-F050B                     Replace Flex.
2-1069-87 RCIC Turbine Trip Throttle Replace Packing bushing.
2-1075-87         2E12-F024A and B               Install temporary system change for full closure of valves.
2-1070-87 2E12-F050B Replace Flex.
2-1076-87         2E51-F059                     Troubleshoot Limitorque.
2-1075-87 2E12-F024A and B Install temporary system change for full closure of valves.
2-1101-87         2A RHR Heat Exchanger Switch   Replace overload relay.
2-1076-87 2E51-F059 Troubleshoot Limitorque.
2-1101-87 2A RHR Heat Exchanger Switch Replace overload relay.
Outlet.
Outlet.
2-1102-87         B and C RHR Water Leg Pump     Replace control relay.
2-1102-87 B and C RHR Water Leg Pump Replace control relay.
2-1104-87         2E12-F074B                     Replace nicked wire.
2-1104-87 2E12-F074B Replace nicked wire.
2-1107-87         2B RRR System                 Repair leaking flow orifice.
2-1107-87 2B RRR System Repair leaking flow orifice.
2-1111-87         2E12-F006A                     Repack Valve.
2-1111-87 2E12-F006A Repack Valve.
2-1118-87         2E12-F050B                     Repair sealtite.
2-1118-87 2E12-F050B Repair sealtite.
2-1121-87         2E12-F041B                     Replace limit switch.
2-1121-87 2E12-F041B Replace limit switch.
2-1122-87         2E12-F041C                     Replace sealtite and solenoid.
2-1122-87 2E12-F041C Replace sealtite and solenoid.
2-1127-87         2E12-F099A                     Replace reverse contactor.
2-1127-87 2E12-F099A Replace reverse contactor.
2-1128-87         2E12-F053A                     Replace circuit breaker.
2-1128-87 2E12-F053A Replace circuit breaker.
2-1150-87         ".CIC Division 1 Power         Ground Isolate.
2-1150-87
2-1158-87         ZE12-F047B                     Repair / Replace Butt Splice.
".CIC Division 1 Power Ground Isolate.
2-1157-87         2E12-F048B                     Repair / Replace Butt Splice.
2-1158-87 ZE12-F047B Repair / Replace Butt Splice.
2-1159-87         2E12-F006B                     Repair / Replace Butt Splice.
2-1157-87 2E12-F048B Repair / Replace Butt Splice.
2-1160-87         2E12-F009                     Repair / Replace Butt Splice.
2-1159-87 2E12-F006B Repair / Replace Butt Splice.
2-1161-87         2E12-F049B                     Repair / Replace Butt Splice.
2-1160-87 2E12-F009 Repair / Replace Butt Splice.
2-1162-87         2E12-F042B                     Repair / Replace Butt Splice.
2-1161-87 2E12-F049B Repair / Replace Butt Splice.
2-1163-87         2E12-F016B                     Repair / Replace Butt Splice.
2-1162-87 2E12-F042B Repair / Replace Butt Splice.
2-1165-87         2E51-F019                     Limitorque Work.
2-1163-87 2E12-F016B Repair / Replace Butt Splice.
2-1170-87         2E51-F054                     Replace cable 2RIO95.
2-1165-87 2E51-F019 Limitorque Work.
2-1173-87         2E12-F027B                     Repair overload relay and wires.
2-1170-87 2E51-F054 Replace cable 2RIO95.
2-1174-87         2E12-F050A                     Reconnect solenoid.
2-1173-87 2E12-F027B Repair overload relay and wires.
2-1191-87         2A RHR Pump                   Inspect motor.
2-1174-87 2E12-F050A Reconnect solenoid.
2-1203-87         2E12-F332C                     Lock throttle at 4000 G.P.M.
2-1191-87 2A RHR Pump Inspect motor.
2-1203-87 2E12-F332C Lock throttle at 4000 G.P.M.
while 2 'D' Service Water Pump is Out-of-Service.
while 2 'D' Service Water Pump is Out-of-Service.
DOCUMENT ID 0036r/0005r
DOCUMENT ID 0036r/0005r


e OUTAGE NO.         EOUIPMENT                       PUNPOSE OF OUTAGE 2-1215-87         HCU 22-23                       Repair leaking 113 viv.
e OUTAGE NO.
2-1224-87         2A RHR Pump Seal Cooler         Clean and inspect.
EOUIPMENT PUNPOSE OF OUTAGE 2-1215-87 HCU 22-23 Repair leaking 113 viv.
2-1228-87         2A RHR Pump                     inspect Motor.
2-1224-87 2A RHR Pump Seal Cooler Clean and inspect.
2-1241-87         2E12-F083B and -F084B           Laak Repair.
2-1228-87 2A RHR Pump inspect Motor.
2-1242-87         2E12-F087B                       Repair contactor.
2-1241-87 2E12-F083B and -F084B Laak Repair.
2-1245-87         2E51-F064                       Repair limitorque compartment cover.
2-1242-87 2E12-F087B Repair contactor.
2-1250-87         2E12-F049A                       Replace overload relay.
2-1245-87 2E51-F064 Repair limitorque compartment cover.
2-1251-87         2E12-F086                       Replace 74-relay.
2-1250-87 2E12-F049A Replace overload relay.
2-1253-87         HPCS D/G Air Start Solenoid     Repair / Replace Air Start Solenoid Vlv.
2-1251-87 2E12-F086 Replace 74-relay.
2-1261-87         RI Hd Spray                     Remove blank flange and install HD Spray Line.
2-1253-87 HPCS D/G Air Start Solenoid Repair / Replace Air Start Solenoid Vlv.
2-1262-87         2E12-C300D 2D RHR Service       Repair Seized Pump.
2-1261-87 RI Hd Spray Remove blank flange and install HD Spray Line.
2-1262-87 2E12-C300D 2D RHR Service Repair Seized Pump.
Water Pump.
Water Pump.
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d * . 8. Off-site Doso calculation Manual There were no changes to the ODCM diiring this reporting period.
d *. 8.
: 4. Radioactive Waste Treatment Systems.
Off-site Doso calculation Manual There were no changes to the ODCM diiring this reporting period.
4.
Radioactive Waste Treatment Systems.
There were no changes to the Radioactive Waste Treatment Systems during this reporting period.
There were no changes to the Radioactive Waste Treatment Systems during this reporting period.
: 5. Indications of Failed Puel Elements.
5.
Indications of Failed Puel Elements.
There were no indications of failed fuel elements during this reporting period.
There were no indications of failed fuel elements during this reporting period.
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Line 770: Line 1,039:


I May 7, 1987 I
I May 7, 1987 I
Director, Office of Managemc7t Information and Program Control j United States Nuclear Regulatory Commission Washington, D.C. 20555 ATTN: Document Control Desk Gentlemen:
Director, Office of Managemc7t Information and Program Control j
United States Nuclear Regulatory Commission Washington, D.C.
20555 ATTN: Document Control Desk Gentlemen:
Enclosed for your information is the monthly performance report covering LaSalle County Nuclear Power Station for the period April 1, 1987 through April 30, 1987.
Enclosed for your information is the monthly performance report covering LaSalle County Nuclear Power Station for the period April 1, 1987 through April 30, 1987.
Very truly yours, fh-
Very truly yours, fh-
                                              +G.J.       Diederich Station Manager LaSalle County Station GJD/GJK/sjc l Enclosure xc: J. G. Keppler, NRC, Region III NRC Resident Inspector LaSalle Gary Wright, Ill. Dept. of Nuclear Safety A. Bournia, NRR Project Manager D. P. Galle, CECO D. L. Farrar, CECO INPO Records Center L. J. Anastasia, PIP Coordinator SNED M. A. Ortin, GE Resident H. E. Bliss, Nuclear Fuel Services Manager                     /
+G.J. Diederich Station Manager LaSalle County Station GJD/GJK/sjc l
                                                                        /(f.
Enclosure xc:
r C. F. Dillon, Senior Financial Coordinator, LaSalle J. C. Klika, Surveillance Group Leader                               I
J. G. Keppler, NRC, Region III NRC Resident Inspector LaSalle Gary Wright, Ill. Dept. of Nuclear Safety A. Bournia, NRR Project Manager D. P. Galle, CECO D. L. Farrar, CECO INPO Records Center L. J. Anastasia, PIP Coordinator SNED M. A. Ortin, GE Resident
/(f.
H. E. Bliss, Nuclear Fuel Services Manager
/
r C. F. Dillon, Senior Financial Coordinator, LaSalle J. C. Klika, Surveillance Group Leader I (
Dennis Carlson/ Tech Staff
(
(
Dennis Carlson/ Tech Staff                                              (
Terry Novotney/ Training Central File DOCUMENT ID 0043r/0005r
Terry Novotney/ Training Central File DOCUMENT ID 0043r/0005r
_            - _ _ _ - -}}
- _ _ _ - -}}

Latest revision as of 02:56, 4 December 2024

Monthly Operating Repts for Apr 1987
ML20213G900
Person / Time
Site: LaSalle  
Issue date: 04/30/1987
From: Diederich G, Kirchner G
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM), NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
OO43R-OOO5R, NUDOCS 8705190018
Download: ML20213G900 (44)


Text

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a.

-y-4 LASALLE NUCLEAR POWER STATION j

UNIT 1 d

.i MONTHLY PERFORMANCE REPORT 4

APRIL 1987 Cot 990NWEALTH EDISON COMPANY i

i NHC DOCKET NO. 050-373 LICENSE NO. NPP-ll d

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n 8705190018 870430 PDR ADOCK 05000373 PDR-R DOCUMENT ID 0043r/0005r

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1 TABLE OF CONTENTS I.

INTRODUCTION II.

MONTHLY REPORT FOR UNIT ONE l

A.

Sumusary of Operating Experience B.

PLANT OR PROCEDURE CHANGES, TESTS, EXPERIMENTS, AND SAFETY RELATED MAINTENANCE 1.

Amendments to Facility Licen.=,e or Technical Specifications 2.

Facility or Procedure Changes Requiring NRC Approval 3.

Tests and Experiments Requiring NRC Approval.

4.

Corrective Maintenance of Safety Related Equipment 5.

Completed Safety Related Modifications.

C.

-LICENSEE EVENT REPORTS D.

DATA TABULATIONS 1.

Operating Data Report 2.

Average Daily Unit Power Level 3.

Unit Shutdowns and Power Reductions E.

UNIQUE REPORTING REQUIREMENTS 1.

Main Steam Relief Valve Operations 2.

ECCS System Outages 3.

Off-Site Dose Calculation Manual Changes 4.

Major Changes to Radioactive Waste Treatment System 5.

Indications of Failed Fuel Elements DOCUMENT ID 0043r/0005r

=

e 1

I.

INTRODUCTION a

The LaSalle County Nuclear Power Station is a two-unit facility owned by commonwealth Edison Company and located near Marseilles, Illinois.

Each unit is a Boiling Water Reactor with a designed net electrical

~

output of 1078 Megawatts. Waste heat is rejected to a man-made cooling pond using the. Illinois River for make-up and blowdown. The architect-engineer was Sargent and Lundy and the primary construction

. contractor was commonwealth Edison Company.

1 Unit one was issued operating license number NPF-11 on April 17, 1982.

Initial criticality was achieved on June 21, 1982 and commercial power operation was commenced on January 1, 1984.

\\

This report was compiled by Gregory J. Kirchner, telephone number (815)357-6761, extension 704.

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II.

MONTHLY REPORT FOR UNIT ONE A.

SUMMARY

OF OPERATING EXPERIENCE FOR UNIT ONE APRIL 1987 4-1-87 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> -

Rx Critical, generator at 600 MWe.

4-2-87 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br /> -

Commence power increase to 620 MWe at 10 MWe/hr.

4-13-87 2310 hours0.0267 days <br />0.642 hours <br />0.00382 weeks <br />8.78955e-4 months <br /> -

Reduce power to 600 MWe in order to take

'A' TDRFP out of service.

4-14-87 2050 hours0.0237 days <br />0.569 hours <br />0.00339 weeks <br />7.80025e-4 months <br /> -

Start ramp at 10 MWe/hr to 620 MWe to put

'A' TDRFP on.

4-24-87 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> -

Drop 30 MWe to 590 MWe to perform LOS-AA-W1 on HCU pressures, then recover to 625 MWe.

4-30-87 2400 hours0.0278 days <br />0.667 hours <br />0.00397 weeks <br />9.132e-4 months <br /> -

Rx critical, generator on line at_630 MWe.

DOCUMENT ID 0043r/0005r

D.

PLANT OR PROCEDURE CHANGES, TESTS,' EXPERIMENTS AND' SAFETY RELATED MAINTENANCE.

g 1.

Amendments to. Facility License or Technical Specification.

There were no ammendments to-Facility License or Technical Specifications during this reporting period.

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2.

Facility or Procedure changes requiring NRC approval.

There were no Facility or Procedural changes requiring NRC approval 4

during this reporting period.

3.

Tests and Experiments requiring NRC approval.

~

There were no tests or experiments requiring NRC approval during this reporting period.

4.

Corrective Maintenance of Safety Related Equipment.

The following table (Table 1) presents a Summary of safety-related maintenance completed on Unit one during the reporting period. The headings ~ indicated in this summary include:

Work Request number, Component Name, Cause_of Malfunction, Results and Effects on Safe Operation, and Corrective Action.

5.

Completed Safety Related Modifications.

i The following Table (Table 2) presents a list of completed Modifications during this reporting period. Each entry will have a short synopsis explaining details involved with each modification.

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TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT UNIT #1 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 63159 RCIC Steam Supply Valve Packing Leaks Repack Valve Valve Repacked.

Drain Pot Steam Trap Assembly Inlet Stop Valve IE51-F038 64940 HPCS D/G Low Air Alarm Setpoint High Calibrate Recalibrated Switch Pressure Alarm lE22-Verified proper Ops.

N504 64941 HPCS D/G Low Air Pressure Alarm lE22--

N505 1

65144 Isolation Damper to Damper Failed in Close Bad Limit Switch Adjusted Travel Limit East Control Room Position Switch Arm to proper tension.

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66051 HPCS Diesel Vent Air Filter Diff. Press. Hi Recalibrate Recalibrated IPDS--VD004 l

Intake Filter D/P Alarm and IPDI-VD004.

l IPDS-VD004 1

66761 RCIC Water Leg Pump Pump is binding Breaker trip on high current New pump installed.

66766 1A RHR Hx Vent V1v Valve will not full close Vlv not travelling full close Contacts loose on limit-IE12-F073A orque. Tightened contact and assured proper ops.

66800 RCIC Steam Vlv. IF51-Valve didn't auto open Auto open does not function on Adjusted micro-switch N010 High Steam Line Drain Pot Alarm assured proper ops.

I 66832 Ammonia Detector Manual zero adjust is Replace meter Replaced meter and damaged on meter.

calibrated.

DOCUMENT ID 0043r/0005r

TABLE 1 CORRECTIVE MAINTENANCE CF SAFETY RELATED EQUIPMENT UNIT #1 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 66867 RCIC Water Lcg Pump Valve did not seat Disassemble / Repair Valve cleaned internally, Discharge Valve IE51-properly new bonnet gasket installed F061 proper ops.

66869 Containment Monitoring Paper does not advance.

Bad Drive Gear.

Replace Drive Gear Temp. Recorder ITR-observed for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> CM037 satisfactorily.

66998 DWEDS Outboard Iso-Valve dos not fully open.

Adjust limit switch Adjusted limit switch for lation Valve 1RE025 proper Ops.

67031 D/P Gage & Alarm Gage reading low.

Recalibrate Recalibrated and assured IPDI-VX014 proper Ops.

67168 DIV 1 POST LOCA Lvl/

Motor Making Noise.

Recorder is oscilloting.

Rcplaced faulty servo' Press Recorder 1B21-motor assembly.

R884A 67225 Ammonia Detector Detector Failed.

Troubleshoot Replaced photocell board, 0XY-VC125B magnets, drive motor, and calibrated.

67449 Supp. Pool Temp.

Does not Print Repair / Replace Adjusted printhead solen-Recorder ITR-CM038 old for proper Ops.

67507 Accumulator 22--19 Vlv. Leaks Repla$e (111) Cartridge.

(111) Cartridge replaced.

111 Valve.

67535 Suppression Chamber Temperature Recorder off Recalibrate Calibrated and observed Air Temperature ITR-by 10*F.

proper Ops.

CM040 67569 CRD Accumulator #26 -43 (111) Valve leaks Replace cartridge Cartridge replaced.

67399

'D' APRM

'D' APRM Giving Half Scrams Gives half scrams on Hi Neutron Replaced Kl8 Relay verified Flux.

proper Ops.

DOCUMENT ID 0043r/0005r l

i TABLE 2 COMPLETED SAFETY RELATED MODIFICATIONS MODIPICATION NUMBdR: A brief synopsis of incorporated modification objectives with final design resolution. Also, state reviewed or unreviewed safety questions.

UNIT ONE M-1-0-85-008 This Modification provided access to various fire dampers that are not accessable per the August, 19d4, technical basis of the LaSalle County Station Fire Damper Surveillance program. There were no unreviewed safety questions.

M-J-0-85-011 This Modification was to install the interconnections required for the interim Redwaste Storage Facility telephone connection, paging connection, fire detection alarm connection, and the potentially contaminated sump high level alarm connection. There were no unreviewed safety questions.

M-1-0-86-023 This Modification was to improve the exiting method of sampling the flow in the Mid/Hi Range portio of the Stadnby Gas Treatment Wide Range Gas Monitor (WRGM). This change will minimize the amount of iodine plateout in the sample line. There were no unreviewed safety questions.

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.C.

' LICENSEE EVENT REPORTS I

The following is a tabular summary of all licensee event reports for LaSalle Nuclear Power Station, Unit One, logged during the reporting period, April 1, 1987 through April 30, 1987. This information is provided pursuant to the reportable occurrence reporting requirements as set forth in 10CFR 50.73.

Licensee Event Report Number Date Title of Occurrence 87-016-00 4/1/87 RCIC Isolation on Steam Line High Flow.

87-017-00 4/2/87 1.69 PSIG DW Pressure Switch valved out.

5

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87-018-00 4/13/87

'A' VC Ammonia Detector spurious trip.

87-019-00 4/3/87 Incomplete surveillance on CRD cycling.

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87-020-00 4/16/87 Loss of 12C/208 Distribution at i

MCC 136X-1.

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5' D.

DATA TABULATIONS The following data tabulations are presented in this report:

1.

Operating Data Report 2.

Average Daily Unit Power Level 3.

Unit Shutdowns and Power Reductions i

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1.

_ OPERATING DATA REPORT-

)

DOCKET No. 050-373 UNIT LaSalle One

'I DATE May 10. 1987

,!. COMPLETED BY G. J. Kirchner 1

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TELEPHONE (815)357-6761 v

r OPERATING STATUS

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REPORTING' PERIOD: _ _ _ ADril. 1987 GROSS HOURS IN REPORTING PERIOD: 719 2.

CURRENTLY AUTHORIZED POWER LEVEL (MWt):2 H1 MAX DEPEND CAPACITY (MWe-Net): 1036 DESIGN ELECTRICAL RATING (MWe-Net): 1078 3.

POWER LEVEL TO WHICH RESTRICTED (IF ANY) (MWe-Net):

1050 4.

. REASONS FOR RESTRICTION (IF ANY): Administrative vI f

THIS MONTH YR TO DATE CUMULATIVE s

5 NUMBER OF HOURS REACTOR WAS_ CRITICAL 719 2471.60 18164.40 6.

REACTOR RESERVII SHUTDOWN HOURS 0.0:

0.0 1642.0,_

7.

HOURS, GENERATOR ON LINE 719 2356.90 17506.40 1

8.

UNIT RESERVE SHUTDOWN HOURS _ j*

0.0 0.0 0.0 g.

9.

GROSS THERMAL ENERGY GENERATED (MWH) 1399704 5029296 45614218 l

10.

GROSS ELEC. ENERGY GENERATED (MWH) 446508 1629188 14319865-11.

NET ELEC.' ENEEGY GENERATED (MWH) 431404 1565969 13588543 12.

REACTOR SERVICE FACTOR 100%

85%

62%

13.

REACTOR AVAILABILITY FACTOR 100%

85%

_ 68%

+

i 14.

UNIT SERVICE FACTOR 100%

82%

60%

15.

UNIT AVAILABILITY FACTOR 100%

82%

60%

4 16.

UNIT CAPACITY FACTOR (USING MDC) 60% ___

56%

45%

17.

UNIT CAPACITY FACTOR (USING DESIGN-MWe) 55%

50%

43%

18.

UNIT FORCED OUTAGE RATE 0%

21%

15.2%

19.

SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH)

On June 13, 1987, Unit I will be shutdown to repair the IB Reactor Recirc Pump. The chutdown is scheduled to last fifty (50) days.

20.

IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

N/A i

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2. AVERAGE DAILY UNIT POWER LEVEL DOCKET NO: 050-373 UNIT: LASALLE ONE DATE: May 10, 1987 COMPLETED BY: Gregory Kirchner i

TELEPHONE: (815) 357-6761 MONTH: April. 1987 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1.

580 17.

606 i

2.

580 18.

604 3

607 19.

601 608 20.

603

5..

582 21.

600 l

6.

606 22.

601 7.

605 23.

602 8.

604 24.

601 9._

602 25.

601 10.

602 26.

602 11.__

600 27.

600 12._

597 28.

600 13.

599 29.

604 14.

580 30.

602 15.

596 31.

16.

598 DOCUMENT ID 0043r/0005r

3.

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 050-373 UNIT NAME LaSalle One DATE May 10, 1987 REPORT MONTil APRIL, 1987 COMPLETED BY Gregory Icirchner TELEPliONE (815)357-6761 METilOD OF TYPE SliUTTING DOWN F: FORCED DURATION TIIE REACTOR OR CORRECTIVE NO.

DATE S: SCl!EDULED (liOURS)

REASON REDUCING POWER ACTIONS / COMMENTS Unit was critical for 719 hours0.00832 days <br />0.2 hours <br />0.00119 weeks <br />2.735795e-4 months <br /> during April, 1987 s

DOCUMENT ID 0043r/0005r

E.

UNIQUE REPORTING REQUIREMENTS

1. Safety / Relief valve operations for Unit One.

VALVES NO & TYPE PLANT DESCRIPTION DATE ACTUATED ACTUATION CONDITION OF EVENT There were no Safety Relief Valves Operated for Unit One during this reporting period.

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2.

ECCS Systems Outagns Tha following outagsa were takin on ECCS Systems during' the reporting period.

OUTAGE NO.

EOUIPMENT EURPOSE OF OUTAGE U-l and Common il 0-74-87

'O' Diesel Generator Lube and Filter Change 0-75-87

'O' D/G Temperature and Oil Switches I

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Off-Site Dose Calculation Manual There were no changes to the ODCM during this reporting period.

4.

Radioactive Waste Treatment Systems.

There were no changes to the Radioactive Waste treatment systems during this reporting period.

5.

Indications of Failed Fuel Elements There were no indications of Failed Fuel Elements during this reporting period.

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LASALLE NUCLEAR POWER STATION UNIT 2 i

i MONTHLY PERFORMANCE REPORT 1

I

~ APRIL, 1987 l

COMMONWEALTH EDISON COMPANY i

f NRC DOCKET NO. 050-374 i

t LICENSE NO. NPF-18 i

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TABLE OF CONTENTS 4

I.

INTRODL37 TION II.

MONTHLY REPORT FOR UNIT TWO A.

Summary of Operating Experience

-B.

PLANT OR PROCEDURE CHANGES, TESTS, EXPERIMENTS, AND 4,

SAFETY RELATED MAINTENANCE 1.

Amendments to Facility License'or Technical Specifications 2.

Facility or Procedure Changes Requiring NRC Approval 3.

Tests and Experiments Requiring NRC Approval 4.

Corrective Maintenance of Safety Related Equipment 5.

Completed Safety Related Modifications i

C.

LICENSEE EVENT REPORTS 1

D.

DATA TABULATIONS 4

1.

Operating Data Report 2.

Average Daily Unit Power Level 3.

Unit Shutdowns and Power Reductions E.

UNIQUE REPORTING REQUIREMENTS 1.

Safety / Relief Valve Operations 2.

ECCS System Outages 3.

Off-Site Dose Calculation Manual Changes 4.

Major Changes to Radioactive Waste Treatment j

System 5.

Indications of Failed Fuel Elements 1

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6 I.

INTRODUCTION The LaSalle County Nuclear Power Station is a two-unit facility owned by Commonwealth Edison Company and located near Marseilles, Illinois.

Each unit is a Boiling Water Reactor with a designed net electrical output of 1078 Megawatts. Waste heat ir rejseted to a man-made cooling pond using the Illinois River for make-up and blowdown. The architect-engineer was Sargent and Lundy and the primary construction contractor was commonwealth Edison Company.

Unit two was issued operating license number NPF-18 on December 16, 1983. Initial criticality was achieved on March 10, 1984 and commercial power operation was commenced on June 19, 1984.

This report was compiled by Gregory J. Kirchner, telephone number (815)357-6761 extension 704.

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MCNTHLY REPORT FOR UNIT TWO e.

's

'A.

. SU19tARY OF OPERATING EXPERIENCE FOR UNIT TWO APRIL 01-30, 1987 4-1-87, 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> -

Rx in refuel 4-30-87, 2400 hours0.0278 days <br />0.667 hours <br />0.00397 weeks <br />9.132e-4 months <br /> -

Rx in refuel.

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PLANT OR PROCEDURE CHANGES, TESTS, EXPERIMENTS AND SAFETY RELATED MAINTENANCE.

1.

Amendments to Facility license, or Technical Specification.

AMENDMENT

  1. 30 This amendment revises the LSCS Unit 2 Technical Specifications to permit replacing an existing peripheral (02-43) locking piston control rod drive module with a fine motion control rod drive module during one fuel cycle (Cycle 2).
  1. 31 This amendment revises the LSCS Unit 2 Technical Specifications to reflect a low and/or degraded grid voltage modification in Division I of the electrical divisions.
  1. 32 This amendment revises the LSCS Unit 2 Technical Specifications to support operation of Unit 2 at rated power during Cycle 2 operation.

2.

Facility or Procedure changes requiring NRC approval.

There were no Facility or Procedure changes requiring NRC approval curing the reporting period.

3.

Tests and Experiments requiring NRC approval.

There were no Tests or Experiments requiring NRC approval during the reporting period.

4.

Corrective Maintenance of Safety Related Equipment.

The following table (Table 1) presents a summary of Safety-Related Maintenance completed on Unit Two during the reporting period. The headings indicated in this summary include: Work Request number, Component Name, cause of malfunction, results and effects on safe operation, and corrective action.

5.

Completed Safety Related Modifications.

The following table (Table 2) presents a list of completed Modifications during this reporting period. Each entry will have a short synopsis explaining details involved with each modification.

DOCUMENT ID 0036r/0005r

s TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 49687 HPCS Switchgear Room Door seal is cracked.

Replace seal.

Seal Replaced.

Water Tight door.

54665 2B RHR S/D Cooling Valve binding.

Repair Torque bonnet and stroked Check valve 2E12-valve. No binding problem F050B observed.

61481 Remove indicated Snubbers SC02-2808S and Remove snubbers on piping sub-Snubbers eliminated due to mechanical snubbers SC02-2805 system 2SCO2 reanalyze of subsystem.

61686 Reanalyze piping sub - Snubbers RH73-2003S 2004S, Remove snubbers Snubbers removed.

system 2RH73 to 2005S, and 2006S, delete unnecessary snubbers.

61942 Valve 2VP- 063B Torque switch failed suspect loose contact Tightened loose torque switch contacts, valve cycle sat.

62600 2A RHR SDC Return Valve leaking

'A' RHR discharge pressure Disassembled, repaired Isolation Stop 2E12-pressure slowly increases and reassembled. Proper F053A operations observed.

62888 Drywell Oil Plug Oil Plug on containment Clean and inspect Drain plug cleaned and Fitting wall is leaking re-tapped.

63333 HPCS Suction Isolation Test Valve under design Fould faulty torque switch Torque switch replaced.

Valve conditions.

502A05.

63550 HPCS Water Leg Relief Remove relief valve and Unit--2 Refuel Requirement Valve removed and tested Valve 2E22-F014 test eatisfactorily.

63697 Fuel Zone Level Chart drive does not Repair Cleaned and aligned chart Recorder 2B21-R615 advance drive. Verified proper Ops.

DOCUMENT ID 0036r/0005r

TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 63870 Accumulator 38--59 When full closed valve Replace (111) cartridge (111) - cartridge replaced 2Cll-D001--lll leaks badly.

64038 Accumulator 22-03 Packing leak Replace (111) cartridge Cartridge replaced.

64039 Accumulator 18-07 Packing leak Replace (111) cartridge Cartridge replaced.

64040 Accumulator 10-11 Packing leak Replace (111) cartridge Cartridge replaced.

64041 Accumulator 14-11 Packing leak Replace (111) cartridge Cartridge replaced.

i 64042 Accumulator 30-15 Packing leak Replace (111) cartridge Cartridge replaced.

64043 Accumulator 22-15 Packing leak Replace (111) cartridge Cartridge replaced.

64044 Accumulator 18-15 Packing leak Replace (111) cartridge Cartridge replaced.

64045 Accumulator 10-15 Packing leak Replace (111) cartr idge Cartridge replaced.

64046 Accumulator 02-19 Packing leak Replace (111) cartridge Cartridge replaced.

I 64047 Accumulator 06-19 Packing leak Replace (111) cartridge Cartridge replaced.

64048 Accumulator 18--19 Packing leak Replace (111) cartridge Cartridge replaced.

64049 Accumulator 22 19 Packing leak Replace (111) cartridge Cartridge replaced.

64050 Accumulator 26-19 Packing leak Replace (111) cartridge Cartridge replaced.

64051 Accumulator 30-19 Packing leak Replace (111) cartridge Cartridge replaced.

64052 Accumulator 30- 23 Packing leak Replace (111) cartridge Cartridge replaced.

64053 Accumulator 26-23 Packing leak Replace (111) cartridge Cartridge replaced.

DOCUMENT ID 0036r/0005r

I TABLE 1 j

i CORRECTIVE MAINTENANCE OF l

SAFETY RELATED EQUIPMENT I

Unit #2 i

WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION l

ON SAFE PLANT OPERATION l

64054 Accumulator 10-23 Packing leak Replace (111) cartridge Cartridge replaced.

64056 Accumulator 06-31 Packing leak Replace (111) cartridge Cartridge replaced.

64057 Accumulator 02-31 Packing leak Replace (111) cartridge Cartridge replaced.

64058 Accumulator 02--35 Packing leak Replace (111) cartridge Cartridge replaced.

64059 Accumulator 14-35 Packing leak Replace (111) cartridge Cartridge replaced.

64060 Accumulator 18-35 Packing leak Replace (111) cartridge Cartridge replaced.

64061 Accumulator 02-39 Packing leak Replace (111) cartridge Cartridge replaced.

64062 Accumulator 06-43 Packing leak Replace (111) cartridge Cartridge replaced.

64063 Accumulator 10-43 Packing leak Replace (111) cartridge Cartridge replaced.

64064 Accumulator 26-47 Packing leak Replace (111) cartridge Cartridge replaced.

E4065 Accumulator 14-47 Packing leak Replace (111) cartridge Cartridge replaced.

64066 Accumulator 06-47 Packing leak Replace (111) cartridge Cartridge replaced.

64067 Accumulator 26-51 Packing leak Replace (111) cartridge Cartridge replaced.

64068 Accumulator 26-59 Packing leak Replace (111) cartridge Cartridge replaced.

64104 Accumulator 38-43 Packing leak Replace (111) cartridge Cartridge replaced.

64105 Accumulator 58-43 Packing leak Replace (111) cartridge Cartridge replaced.

64106 Accumulator 54-43 Packing leak Replace (111) cartr.dge Cartridge replaced.

DOCUMENT ID 0036r/0005r

TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 64116 Damper Actuators for To prevent seals from de-Remove / Replace Cylinders.

Two (2) cylinders replaced 2VR04YB (2FZ-VR015) grading, vendor recommends with new ones.

air cylinders be replaced each refueling outage.

264117 Damper actuators for To prevent seals from de--

Remove / Replace Cylinders.

Two (2) cylinders replaced 2VR04YA (2FZ-VR014) grading, vendor recommends with new ones.

air Cylinders be replaced each refueling outage.

264118 Damper actuators for To prevent seals from de-Remove / Replace Cylinders.

Two (2) cylinders replaced 2VR05YD (2FZ-VR002) grading, vendor recommends with new ones.

air cylindars be replaced each refueling outage.

64141 Accumulator 42-55 Packing leak Replace (111) Cartridge.

Cartridge replaced.

64142 Accumulator 42-51 Packing leak Replace (111) Cartridge.

Cartridge replaced.

64144 Accumulator 38-51 Packing leak Replace (111) Cartridge.

Cartridge replaced.

64145 Accumulator 34-47 Packing leak Replace (111) Cartridge.

Cartridge replaced.

64146 Accumulator 42-47 Packing leak Replace (111) Cartridge.

Cartridge replaced.

64147 Accumulator 46-47 Packing leak Replace (111) Cartridge.

Cartridge replaced.

64148 Accumulator 34-43 Packing leak Replace (111) Cartridge.

Cartridge replaced.

64202 Accumulator 34-35 Packing leak Replace (111) Cartridge.

Cartridge replaced.

64248 Accumulator 42"27 Packing leak Replace (111) Cartridge.

Cartridge replaced.

64249.

Accumulator 42-23 Packing leak Replace (111) Cartridge.

Cartridge replaced.

l l

DOCUMENT ID 0036r/0005r

TABLE 1 I

f CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT CORRECTIVE ACTION Unit #2 RESULTS AND EFFECTS CAUSE OF MALFUNCTION WORK REQUEST COMPONENT ON SAFE PLANT OPERATION Cartridge replaced.

Replace (111) Cartridge.

64250 Accumulator 38--27 Packing leak Cartridge replaced.

Replace (111) Cartridge.

UI251 Accumulator 34--27 Packing leak Cartridge replaced.

Replace (111) Cartridge.

64253 Accumulator 46-27 Packing leak Cartridge replaced.

Replace (111) Cartridge.

64055 Accumulator 18-27 Packing leak Transmitter recalibrated Pressure gage damaged Reading full scale.

and assured proper Ops.

64294 RCIC Pressure Gage Set limimts and cycled Troubleshoot 64441

  • B* RHR S/D Cooling Valve does not cycle.

valve satisfactorily.

Test. Check Valve 2R12-F0508 Snap ring replaced.

64490 Yaglve 2E32-F002E Handwheel rises when valve Repair is stroked, declutch lever does not work properly.

Solenoid valve found off.

Troubleshoot Reterminated and tested 64602 RHR Testable Check No indication of the Valve 2E12-F050A Control Room.

satisfactorily.

Dirty or intermittent contacts Replaced relay 74Fl.

64937 Relay 74F1 at SVGR Relay not functioning.

on relay.

243 ACB 2433 Cartridge replaced.

Replace (111) Cartridge.

65096 Accumulator 54--23 Packing Leak Cartridge replaced.

Replace (111) Cartridge.

65097 Accumulator 50 -23 Packing Leak Cartridge replaced.

Replace (111) Cartridge.

65098 Accumulator 50-19 Packing Leak Cartridge replaced.

Replace (111) Cartridge.

65099 Accumulator 34-15 Packing Leak DOCUMENT ID 0036r/0005r

TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT

~

Unit #2 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 65100 Accumulator 34-19 Packing Leak Replace (111) Cartridge.

Cartridge replaced.

65101 Accumulator 38--15 Packing Leak Replace (111) Cartridge.

Cartridge replaced.

65102 Accumulator 50--15 Packing Leak Replace (111) Cartridge, Cartridge replaced.

65103 Accumulator 46-11 Packing Leak Replace (111) Cartridge.

Cartridge replaced.

65104 Accumulator 38--07 Packing Leak Replace (111) Cartridge.

Cartridge replaced.

65105 Accumulator 42-07 Packing Leak Replace (111) Cartridge.

Cartridge replaced.

65106 Accumulator 34-03 Packing Leak Replace (111) Cartridge.

Cartridge replaced.

65107 Accumulator 42-03 Packing Leak Replace (111) Cartridge.

Cartridge replaced.

65319 Penetration E-26 Leak found at the input to Repair Repair leak and charged the flange.

to 30 lbs.

65368 FBCCW Otbd. Isol.

Snap ring missing from Replace Snap ring replaced.

Valve 2WR029 handwheel.

65371 RWCU Otbd. Isol.

Valve failed L.L.R.T.

Repair Torque switch adjusted.

Valve 2G33-F004 Proper Ops. observed.

65384 Valve 2E12-F041C Valve does not cycle Air cylinder leaks.

Replaced air cylinder and spring.

65553 MCC 235x--I Contactor sticks Repair Adjusted mechanical interlocks assured proper

Cps, i

DOCUMENT ID 0036r/0005r

TABLE 1 CORRECTIVE MAINTENANCE OF i

SAFETY RELATED EQUIPMENT 1

Unit #2 l

WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION I

ON SAFE PLANT OPERATION l

l l

l 67570 2H-IRM 2C51AZ009D 2H-IRM will not drive Investigate -- Drive Cable Reset the limits and l

out.

insulation was worn allowing repaired the insulation.

l water to drain through the Assured proper Ops.

drive cable, into the gear box.

65735 RHR Heat Exchanger Torque Switch contacts Internal mechanical problem.

Replaced worm and worm Shell Side Bypass make after torquing out.

gear. Verified proper 2E12-F048B Ops.

65957 RHR S/D Cooling Vlv Stem is leaking water.

Repack Valve repacked.

2E12-F006A 66050 HPCS p.p. Breaker Nylon bushings for Cam Replace Removed and replaced nylon 2E22-C001 shaft bearings are badly bushings.

frayed.

66109 RHR Pump Min Flow Stem end of viv operator.

Replaced Missing bolts have been bypass viv 2E12-F064C Missing bolts and lock--

replaced, washers.

66164 Flange Upstream of Flange leaking when Repair - Torque as needed.

Bolts not torqued as re--

2E12-F003B pressure testing.

quired. Cleaned faces of flange and torqued to 750 Ft. Lbs.

66211 valve 2B21-N020D Valve Leaks Repair Valve repaired and Q.C.

Inspected for no leaks.

66212 Mechanical Snubber Damaged Snubber Replace Damaged snubber replaced MSO4-2794-S with a new one.

66213 Mechaalcal Snubber Damaged Snubber Replace Damaged snubber replaced MS00 2013-S with a new one.

66214 Mechanical Snubber Damaged Snubber Replace Damaged snubber replaced MS06-2004-S with a new one.

DOCUMENT ID 0036r/0005r

~

TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION l

ON SAFE PLANT CPERATION 66215 Mechanical Snubber Damaged Snubber Replace Damaged snubber replaced M334-2810-S with a new one.

66216 Mechanical Snubber Damaged Snubber Replace Damaged snubber replaced MS04-2645-S with a new one.

i 66217 Mechanical Snubber Damaged Snubber Replace Damaged snubber replaced MSO4-2808-S with a new one.

66218 Mechanical Snubber Damaged Snubber Replace with new snubber.

Damaged snubber replaced.

LC01-2967-S 66409 2E31-F005B4 Broken Flex on 2LD184.

Determ Cable and repair.

Flex repaired and cable reterminated.

66420 2E12-F050B Broken Flex on Cable 2RH253 Determ cable and repair.

Flex repaired and cable reterminated.

66459 2E12-F041C Actuator Wiring to Solenald are Replace Replaced Solenoid Valve twisted and appear heat Coll, cable and sealtite.

damaged.

66587 Accumulator 50-23 Solenoid Blowing Air Repair Bonnet screws loose.

Retorqued to 120 inch-lbs.

66612 3/4" Flex conduit at Conduit damaged Replace Replaced damaged flex.

2E22-S001 66720 Mechanical Snubber Damaged Snubber.

' Replace snubber Damage snubber replaced M204-2711-S with a new one.

66755 Rx. Vessel Shroud Transmitter does not re-Replace New transmitter installed Level Transmitter spond to test inputs.

and calibrated.

2B21-N044B l

l DOCUMENT ID 0036r/0005r

TABLE 1 CORRECTIVE MAINTENANCE OF SAFETY RELATED EQUIPMENT Unit #2 WORK REQUEST COMPONENT CAUSE Ot7 MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 66774 Div I Battery Gnd.

Alarm sounds whenever viv Troubleshoot and repair.

Removed limitorque cover Alarm 2E12-F006A is open and found pinched wire between body and cover.

Repair and assured proper Ops.

66830 Valve 2E12-F026A No light indication in Bad Relay Replaced relay and assured Control Room.

proper Ops.

66848 Fuse Holder for 2E22-Side broken out of fuse Replace holder Replaced fuse holder C001 Block.

66885 Mechanical Snubber Snubber damaged Replace snubber Snubber replaced.

RH27-2003-S 66935 CRD HCU 34-39 Blowing Air from gaskets Check torque Tightened union above l

scram valve.

l 66968 HPCS Pump Disch.

Threads on body of trans-Replace transmitter.

Transmitter replaced and l

Pressure Indicator mitter are gone.

calibrated.

2E22-N004 I

67003 Directional Control Valve is leaking water Repair leak Leak repaired.

l Valve Solenoid 123 l

HCU 26-59 67016 Mechanical Snubber Snubber damaged Replace snubber Snubber replaced with new RIA2 2999-S one.

67076 HCU 58-35 Scram Pilot Solenoid has a Rebuild 118 Viv.

Rebuilt 118 Valve.

blown diaphragm.

67129 RHR B/C Water Leg Control relay contacts are Repair / replace Cleaned relay contact and Pump 2E12-C003 intermittent.

verified proper ops.

DOCUMENT ID 0036r/0005r

l l

l TABLE 1 l

l CORRECTIVE MAINTENANCE OF l

SAFETY RELATED EQUIPMENT 1

i l

Unit #2 l

WORK REQUEST COMPONENT CAUSE OF MALFUNCTION RESULTS AND EFFECTS CORRECTIVE ACTION ON SAFE PLANT OPERATION 67131 RHR Heat Exchanger A Overload Relay would not Repair / Replace Overload relay replaced.

Discharge 2E12--F068A trip when tested.

67188 RHR S/D Cooling Inj.

Breaker contacts show Replace Replaced breaker for a new valve 2E12-F053A evidence of pitting / mis-one.

alignment.

l l

67194 Supp. Pool Temp Reading Downscale Troubleshoot Replaced wiring harness.

Monitoring Recorder 2TR-CM037 67350 2E12-F020 Loose Limit Switch Arm on Repa?r Tightened limit switch the valve stem.

actuating arm. Verified proper ops.

67368 HCU 42-03 Packing Leak Replace (113) cartridge.

Cartridge replaced.

67496 HPCS Water Leg Pump Does not hold pressure.

Repair Lapped seat, reassembled Check Valve and seal welded bonnet.

l l

l I

I r

DOCUMENT ID 0036r/0005r i

TABLE 2 COMPLETED SAFETY RELATED MODIFICATIONS MODIFICATION NUMBER: A brief Synopsis of Incorporated Modification Objectives with final design resolution. Also, state reviewed or unreviewed safety questions.

UNIT TWO M-1-2-82-014 This Modification was to remove a G.E. pushbutton and control switches located in the Diesel Generator 2A engine gauge panel from the engine skid to meet NRC requirements.

There were no unreviewed safety questions.

M-1-2-83-012 This Modification was to implement the Electrical Maintenance Department M.I. 9644 lube oil system change on the '2B' diesel generator. This will improve the oil circulating subsystem which supplies ol' to the engine for emergency starts. There were no unreviewed safety questions.

M-1-2-84-110 This Modification was for the addition of new pressure switches and also new relays for the low RHR pump discharge pressure alarms and the engineered safety feature status.

There were no unreviewed safety features.

M-1-2-84-111 This modification was to install a Thermowell in the RHR Shutdown cooling line 2RH04C-20. There were no unreviewed safety questions.

M-1-2-84-129 This modification was to separate the High/ Low pressure alarms in the LPCS pump discharge pressure switches. There were no unreviewed safety questions.

M-1-2-85-049 This modification was for the replacement of the GE Model NA-200 Local Power Range Monitors (LPRM's) with the Westinghouse model WL-24286 LPRM. There were no unreviewed safety questions.

M-1-2-86-039 This modification was to add a high point vent to the existing piping of the RHR system on line 2RH41AA-3" and 2RH70A-3".

There were no unreviewed safety questions.

M-1-2-86-041 This modification was to add a high point vent to the existing piping of the RHR system in line 2RH038B-12".

There were no unreviewed safety questions.

M-1-2-86-042 This modification was to add a high point vent to the existingpiping of the RHR system on lines 2RH03BA-12" and 2RH34A-6".

There were no unreviewed safety questions.

DOCUMENT ID 0036r/0005r

TABLE 2 (cont'd)

COMPLETED SAFETY RELATED MODIFICATIONS MODIFICATION NUMBER: A brief Synopsis of Incorporated Modification Objectives with final design resolution. Also, state reviewed or unreviewed safety questions.

M-1-2-86-050 This mod was to add a redundant contact from a different relay in series with the existing contact. This will prevent a single short of a relay from operating the pilot valve. There were no unreviewed safety questions.

M-1-2-86-053 This modification was part of the snubber reduction program for subsystem 2SC02. There were no unreviewed safety questions.

M-1-2-86-054 This modification was part of the snubber reduction program for subsystem 2RIO3. There were no unreviewed safety questions.

M-1-2-86-058 This modification was part of the snubber reduction program for subsystem 2RRC2. There were no unreviewed safety questions.

M-1-2-86-060 This modification was part of the snubber reduction program for subsystem 2RRA9. There were no unreviewed safety questione.

M-1-2-86-061 This modification was part of the snubber reduction program for subsystem 2MS648. There were no unreviewed safety questions.

M-1-2-86-066 This modification was part of the snubber reduction program for subsystem 2MS64F. There were no unreviewed safety questions.

M-1-2-86-068 This mexlification was part of the snubber reduction program for subsystem 2RHBl. There were no unreviewed safety questions.

M-1-2-86-069 This modification was part of the snubber reduction program for subsystem 2RRC7A. There were no unreviewed safety features.

M-1-2-86-071 This modification was part of the snubber reduction program for subsystem 2HpA1. There were no unreviewed safety questions.

l M-1-2-86-078 This modification was part of the snubber reduction program for subsystem 2MS258. There were no unreviewed safety questions.

I DOCUMENT ID 0036r/0005r

r i

1 e *. s TABLE 2 (cont'd)

COMPLETED SAFETY RELATED MODIFICATIONS MODIFICATION NUMBER: A brief Synopsis of Incorporated Modification Objectives with final design resolution. Also, state reviewed or unreviewed safety questions.

M-1-2-86-085 This modification was to remove the existing Static-o-Ring level switch and replace it with a qualified Barton Level switch. There were no unreviewed safety questions.

l DOCUMENT ID 0036r/0005r

o.

o C.

LICENSEE EVENT REPORTS The following is a tabular summary of all licensee event reports for LaSalle Nuclear Power Station, Unit Two, logged during the reporting I

period, April 01, through April 30, 1987. This information is provided pursuant to the reportable occurrence reporting requirements as set forth in 10CPR 50.73.

Licensee Event Report Number Date I.itle of Occurrence 87-005-00 4/2/87 Auto start of 2B D/G during testing.

87-006-00 4/2/87 Group II pCIS Isolation during Mod Test.

87-007-00 4-12-87 Group II Isolation during 1

testing due to failed 2C71-K4Dl.

i 87-008-00 4-14-87 Scram Signal while moving mode l

switch due to blown fuses.

i 87-009-00 4-15-87 ESP Actuation during LLRT due to leakage past stop valve.

i 87-010-00 4-17-87 Scram Signal while defueled/ contractor bumped APRM Cable under RPV.

87-011-00 4-30-87 Static 'O' Ring differential i

pressure switch out.

i 1

i I

DOCU:1ENT ID 0036r/0005r

1 D.

DATA TABULATIONS The following data tabulations are presented in this report:

1. Operating Data Report
2. Average Daily Unit Power Level
3. Unit shutdowns and Power Reductions i

I DOCUMENT ID 0036r/0005r i

- ~ -

a.

1. OPERATING DATA REPORT DOCKET NO. 050-374 UNIT ],aSalle Two DATE May 10. 1987 COMPLETED BY Gregory Kirchner TELEPHONE (815)357-6761 MONTH APRIL 1987 OPERATING STATUS f

1.

REPORTING PERIOD:

April, 1987 GROSS IlOURS IN REPORTING PERIOD: 719 2.

CURRENTLY AUT140RIZED POWER LEVEL (MWt):3323 MAX DEPEND CAPACITY (MWe-Net): 1036 DESIGN ELECTRICAL RATING (MWe-Net): 1078, 3.

POWER LEVEL TO WiiICH RESTRICTt!D (IF PNY) (MWe-Net):

1050 4.

REASONS FOR RESTRICTION (IP ANY); Administrative TilIS MONTH YR TO DATE. CUMULATIVE 5

NUMBER OF llOURS REACTOR WAS CRITICAL 0.0 66.05

'l"069.5 6.

REACTOR RESERVE SHUTDOWN }{OURS 0.0 0.0 29.83 7.

HOURS GENERATOR ON LINE 0.0 59.92 11830.84

]

8.

UNIT RESERVE SHUTDOWN llOURS 0.0 0.0 0.0 9.

GROSS TIIERMAL ENERGY GENERATED (MWil) 0.0 120864 23635128 10.

GROSS ELEC. ENERGY GENERATED (MWH) 0.0 39232 11100804 11.

NET ELEC. ENERGY GENERATED (MWil)

-7324 4757 10544986 12.

REACTOR SERVICE FACTOR 0%

2.2%

53.3%

13.

REACTOR AVAILABILITY FACTOR 0%

2.2%

54.5%

14.

UNIT SERVICE FACTOR 0%

2.1.%

53%

15.

UNIT AVAILABILITY FACTOR Q1 2.1.%

53%

16.

UNIT CIPACITY FACTOR (USING MDC)

-0.9%

0.16%

__.45,81_

17.

UNIT CAPACITY FACTOR (USING DESIGN MWe)

-0.9%

0.15%

44%

18.

UNIT FORCED OUTAGE RATE 0%

0%

26.2%

19.

bHUTDOWNS SCllEDULED OVER NEXT 6 MONTilS (TYPE, DATE, AND DURATION OF EACH):

N/A Unit is in shutdown during this period.

20.

IF S!!UT DOVN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP 5/30/87 l

DOCUMENT ID 0036r/0005r l

1

r 1

~1

2. AVERAGE DAILY UNIT POWER LEVEL' DOCKET NO: 050-374 UNIT: ' LASALLE 'i'WO DATE: May 10. 1987 COMPLETED BY: Gregory Kirchner TELEPHONE: (815) 357-6761 MONTH: April 1987 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 4 l

1.

-8 17.

-10

2. -

-9 18.

-9 3

-10 19.

-9 4.

-10 20.

-9 5.

-9 21.

-9 6.

-9 22.

-9' 7.

-10 23.

-11 8.

-9 24.

-13 s

9.

-10 25.

12 10.

-10 26.

14 11.

-9 27.

r14 12.

-8 28.

14 13.

-8 29.

-14 14.

-7 30.

-14 15.

-8 31.

16.

-10 f

I I

DOCUMENT ID 0036r/000Sr

%,y.,--,

--,, - -w-_m_

.,...#,,,p,,

_,.-_..,.-,,,.~,%.,

y,,. _

,;-r-y--

y.,,._

3.

UNIT SHUTDOWNS AND POWER REDUC' CIONS

. DOCKET NO. 050-374-UNIT NAME LaSalle Tt_oo,

DATE May 10, 1987 REPORT MONTH April, 1987 COMPLETED BY G.J. Kircfaner TELEPHONE (815)357-6761 METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR OR CORRECTIVE NO.

DATE S: SCHEDULED (HOURS)

REASON REDUCING POWER ACTIONS / COP 9fENTS a

1 4/1/87 S

719 C

1 Refuel i

J l

1 i

?

+

1 i

t i

1 I

i l

I i

I 2

1 l

DOCUMENT ID 0036r/0005r i

~.

p l

i s.. s E.

UNIQUE REPORTING REQUIREMENTS 1.

Safety / Relief Valve Operations for Unit Two.

DATE VALVES NO & TYPE PLANT DESCRIPTION ACTUATED ACTUATIONS CONDITION OF EVENT There were no safety relief valves operated for Unit #2 during this reporting period.

DOCUMENT ID 0026r/0005r

e J.

ECCS Systcm3 Outcg:s The following outages were taken on ECCS Systems during the reporting period.

OUTAGE NO.

ROUIPMENT PURPOSE OF OUTAGE 2-1036-87 2E12-C300D Prevent use of motor which is torn apart.

2-1044-87 2HG-006A Rebuild 2HG006A.

2-1047-87 2E12-F092B Prevent inadvertantly filling the reactor.

2-1048-87 D/G 2B - Soak Back oil pump Replace damaged flex.

2-1051-87 2B D/G Calibrate relays.

2-1056-87 2E51-F064 Perform E.Q. Inspection.

2-1063-87 2A D/G Replace Air Start motors.

2-1069-87 RCIC Turbine Trip Throttle Replace Packing bushing.

2-1070-87 2E12-F050B Replace Flex.

2-1075-87 2E12-F024A and B Install temporary system change for full closure of valves.

2-1076-87 2E51-F059 Troubleshoot Limitorque.

2-1101-87 2A RHR Heat Exchanger Switch Replace overload relay.

Outlet.

2-1102-87 B and C RHR Water Leg Pump Replace control relay.

2-1104-87 2E12-F074B Replace nicked wire.

2-1107-87 2B RRR System Repair leaking flow orifice.

2-1111-87 2E12-F006A Repack Valve.

2-1118-87 2E12-F050B Repair sealtite.

2-1121-87 2E12-F041B Replace limit switch.

2-1122-87 2E12-F041C Replace sealtite and solenoid.

2-1127-87 2E12-F099A Replace reverse contactor.

2-1128-87 2E12-F053A Replace circuit breaker.

2-1150-87

".CIC Division 1 Power Ground Isolate.

2-1158-87 ZE12-F047B Repair / Replace Butt Splice.

2-1157-87 2E12-F048B Repair / Replace Butt Splice.

2-1159-87 2E12-F006B Repair / Replace Butt Splice.

2-1160-87 2E12-F009 Repair / Replace Butt Splice.

2-1161-87 2E12-F049B Repair / Replace Butt Splice.

2-1162-87 2E12-F042B Repair / Replace Butt Splice.

2-1163-87 2E12-F016B Repair / Replace Butt Splice.

2-1165-87 2E51-F019 Limitorque Work.

2-1170-87 2E51-F054 Replace cable 2RIO95.

2-1173-87 2E12-F027B Repair overload relay and wires.

2-1174-87 2E12-F050A Reconnect solenoid.

2-1191-87 2A RHR Pump Inspect motor.

2-1203-87 2E12-F332C Lock throttle at 4000 G.P.M.

while 2 'D' Service Water Pump is Out-of-Service.

DOCUMENT ID 0036r/0005r

e OUTAGE NO.

EOUIPMENT PUNPOSE OF OUTAGE 2-1215-87 HCU 22-23 Repair leaking 113 viv.

2-1224-87 2A RHR Pump Seal Cooler Clean and inspect.

2-1228-87 2A RHR Pump inspect Motor.

2-1241-87 2E12-F083B and -F084B Laak Repair.

2-1242-87 2E12-F087B Repair contactor.

2-1245-87 2E51-F064 Repair limitorque compartment cover.

2-1250-87 2E12-F049A Replace overload relay.

2-1251-87 2E12-F086 Replace 74-relay.

2-1253-87 HPCS D/G Air Start Solenoid Repair / Replace Air Start Solenoid Vlv.

2-1261-87 RI Hd Spray Remove blank flange and install HD Spray Line.

2-1262-87 2E12-C300D 2D RHR Service Repair Seized Pump.

Water Pump.

1

-l l

l DOCUMENT ID 0036r/0005r i

i

-. ~. -..,

w.c

,e.

--_..,y-

d *. 8.

Off-site Doso calculation Manual There were no changes to the ODCM diiring this reporting period.

4.

Radioactive Waste Treatment Systems.

There were no changes to the Radioactive Waste Treatment Systems during this reporting period.

5.

Indications of Failed Puel Elements.

There were no indications of failed fuel elements during this reporting period.

l J

DOCUMENT ID 0036r/0005r

I May 7, 1987 I

Director, Office of Managemc7t Information and Program Control j

United States Nuclear Regulatory Commission Washington, D.C.

20555 ATTN: Document Control Desk Gentlemen:

Enclosed for your information is the monthly performance report covering LaSalle County Nuclear Power Station for the period April 1, 1987 through April 30, 1987.

Very truly yours, fh-

+G.J. Diederich Station Manager LaSalle County Station GJD/GJK/sjc l

Enclosure xc:

J. G. Keppler, NRC, Region III NRC Resident Inspector LaSalle Gary Wright, Ill. Dept. of Nuclear Safety A. Bournia, NRR Project Manager D. P. Galle, CECO D. L. Farrar, CECO INPO Records Center L. J. Anastasia, PIP Coordinator SNED M. A. Ortin, GE Resident

/(f.

H. E. Bliss, Nuclear Fuel Services Manager

/

r C. F. Dillon, Senior Financial Coordinator, LaSalle J. C. Klika, Surveillance Group Leader I (

Dennis Carlson/ Tech Staff

(

Terry Novotney/ Training Central File DOCUMENT ID 0043r/0005r

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