ENS 55403: Difference between revisions

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| emergency class = Non Emergency
| emergency class = Non Emergency
| notification date = 08/11/2021 11:32
| notification date = 08/11/2021 11:32
| retracted = Yes
| notification by = Levi Smith
| notification by = Levi Smith
| NRC officer = Lloyd Desotell
| NRC officer = Lloyd Desotell
| event date = 08/11/2021 06:34 EDT
| event date = 08/11/2021 06:34 EDT
| last update date = 08/11/2021
| last update date = 10/06/2021
| title = HPCI Inoperability
| title = HPCI Inoperability
| event text = At 0634 EDT on August 11, 2021 [high pressure coolant injection] HPCI was declared inoperable due to a pump flow controller problem. The cause of the controller problem is unknown at this time and is under investigation.
| event text = At 0634 EDT on August 11, 2021 [high pressure coolant injection] HPCI was declared inoperable due to a pump flow controller problem. The cause of the controller problem is unknown at this time and is under investigation.
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There was no impact on the health and safety of the public or plant personnel.
There was no impact on the health and safety of the public or plant personnel.
The NRC Resident Inspector has been notified.
The NRC Resident Inspector has been notified.
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2021/20210813en.html#en55403
* * * RETRACTION FROM WHITNEY HEMMINGWAY TO KAREN COTTON ON 10/6/2021 AT 1036 EDT * * *
The purpose of this notification is to retract a previous report made on August 11, 2021 (EN 55403). At 0634 EDT on August 11, 2021, an unplanned inoperability of the High Pressure Coolant Injection system (HPCI) was reported pursuant to 10 CFR 50.72(b)(3)(v)(D) by EN 55403. HPCI was declared inoperable due to receipt of an alarm associated with the pump flow controller. The HPCI system operating procedure states that HPCI should be declared inoperable when this alarm is received. The cause of the alarm, a loose transmitter connection, was identified and corrected. Following clearance of the alarm, HPCI was declared operable at approximately 1930 EDT on August 11, 2021. 
This alarm indicated a fault in the signal from the transmitter to the HPCI flow controller; in this case,  the HPCI flow controller would have continuously called for maximum HPCI flow. The controller is configured with a high limiter to prevent an overspeed trip. An engineering evaluation of the event identified that HPCI was capable of performing its required safety functions while this alarm was present. The condition was that the HPCI flow controller would have continuously called for maximum HPCI flow upon HPCI initiation, however operators would be able to manually control HPCI flow upon HPCI initiation. Additionally HPCI would have run until Reactor Pressure Vessel (RPV) level reached Level 8 where it would trip until RPV level decreased to Level 2 then automatically restart.
The licensee notified the NRC Resident Inspector.
Notified R3DO (Peterson).
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2021/20211007en.html#en55403
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| Unit = 2
| Unit = 2

Latest revision as of 07:30, 7 October 2021

ENS 55403 +/- *RETRACTED*
Where
Fermi DTE Energy icon.png
Michigan (NRC Region 3)
Reporting
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
Time - Person (Reporting Time:+0.97 h0.0404 days <br />0.00577 weeks <br />0.00133 months <br />)
Opened: Levi Smith
11:32 Aug 11, 2021
NRC Officer: Lloyd Desotell
Last Updated: Oct 6, 2021
55403 - NRC Website
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