ML18152A304: Difference between revisions
StriderTol (talk | contribs) Created page by program invented by StriderTol |
StriderTol (talk | contribs) Created page by program invented by StriderTol |
||
| Line 33: | Line 33: | ||
e | e | ||
- - - _y_ _ _ _ -- - | - - - _y_ _ _ _ -- - | ||
e POW 34-04 | e POW 34-04 VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT 89-09 APPROVED: | ||
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT 89-09 APPROVED: | |||
l, | l, | ||
-----~----- | -----~----- | ||
| Line 51: | Line 48: | ||
: 7. Maximum Dependable Capacity (Net MWe): 781 | : 7. Maximum Dependable Capacity (Net MWe): 781 | ||
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: | : 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: | ||
: 9. Power Level To Which Restricted, If Any (Net MWe): | : 9. Power Level To Which Restricted, If Any (Net MWe): | ||
: 10. Reason For Restrictions, If Any: -------------- | : 10. Reason For Restrictions, If Any: -------------- | ||
THIS MONTH YTD CUMULATIVE | THIS MONTH YTD CUMULATIVE | ||
: 11. Hours In Reporting Period 720.0 6551. 0 147047.0 | : 11. Hours In Reporting Period 720.0 6551. 0 147047.0 | ||
| Line 73: | Line 68: | ||
: 26. Unit In Test Status (Prior to Commercial Operation): FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 1 | : 26. Unit In Test Status (Prior to Commercial Operation): FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 1 | ||
e | e OPERATING DATA REPORT DOCKET NO.: 50-281 DATE: 10/05/89 COMPLETED BY: Christle Arney TELEPHONE: (804)357-3184 x477 OPERATING STATUS NOTES | ||
OPERATING DATA REPORT DOCKET NO.: 50-281 DATE: 10/05/89 COMPLETED BY: Christle Arney TELEPHONE: (804)357-3184 x477 OPERATING STATUS NOTES | |||
: 1. Unit Name: Surry Unit 2 | : 1. Unit Name: Surry Unit 2 | ||
: 2. Reporting Period: Sept 1 - 30, 1989 | : 2. Reporting Period: Sept 1 - 30, 1989 | ||
| Line 84: | Line 77: | ||
: 7. Maximum Dependable Capacity (Net MWe): -781 --- | : 7. Maximum Dependable Capacity (Net MWe): -781 --- | ||
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: | : 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: | ||
: 9. Power Level To Which Restricted, If Any (Net MWe): | : 9. Power Level To Which Restricted, If Any (Net MWe): | ||
: 10. Reason For Restrictions, If Any: ------------- | : 10. Reason For Restrictions, If Any: ------------- | ||
THIS MONTH YTD CUMULATIVE | THIS MONTH YTD CUMULATIVE | ||
: 11. Hours In Reporting Period 720.0 6551.0 143927.0 | : 11. Hours In Reporting Period 720.0 6551.0 143927.0 | ||
| Line 112: | Line 103: | ||
COMPLETED BY: Christle Arney TELEPHONE: -,...,80""'4,---=3-=-5=-7_""'!!3"""1-=8"""4"""x..,4,. ,7""'7- \ | COMPLETED BY: Christle Arney TELEPHONE: -,...,80""'4,---=3-=-5=-7_""'!!3"""1-=8"""4"""x..,4,. ,7""'7- \ | ||
REPORT MONTH: | REPORT MONTH: | ||
SEPTEMBER 1989 | SEPTEMBER 1989 | ||
---------------------~ME=mo=~D:"'""!:O~F~---=L-=I~c=EN~s=E=E:-------------c=-A:-:U~S~E:"""'!'&--.::'CO=RRE=:-:c~T~I=VE~----- \ | ---------------------~ME=mo=~D:"'""!:O~F~---=L-=I~c=EN~s=E=E:-------------c=-A:-:U~S~E:"""'!'&--.::'CO=RRE=:-:c~T~I=VE~----- \ | ||
| Line 159: | Line 149: | ||
H - Other (Explain) Exhibit 1 - Same Source 4 | H - Other (Explain) Exhibit 1 - Same Source 4 | ||
e e AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.: 50-280* | |||
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.: 50-280* | |||
* UNIT NAME: Surry Unit 1 DATE: 10705789 COMPLETED BY: Christle Arney | * UNIT NAME: Surry Unit 1 DATE: 10705789 COMPLETED BY: Christle Arney | ||
* TELEPHONE:(8045357-3184 x477 MONTH: SEPTEMBER 1989 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 653 17 770 2 715 18 768 3 775 19 766 4 778 20 778 5 777 21 766 6 777 22 716 7 776 23 779 8 773 24 783 9 712 25 783 10 698 26 774 11 772 27 722 12 770 28 786 13 769 29 785 14 769 30 785 15 769 31 16 770 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt. | * TELEPHONE:(8045357-3184 x477 MONTH: SEPTEMBER 1989 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 653 17 770 2 715 18 768 3 775 19 766 4 778 20 778 5 777 21 766 6 777 22 716 7 776 23 779 8 773 24 783 9 712 25 783 10 698 26 774 11 772 27 722 12 770 28 786 13 769 29 785 14 769 30 785 15 769 31 16 770 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt. | ||
5 | 5 | ||
e e AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.: 50-281 UNIT NAME: _.Su_r_r_y__U_n-it__2_____ | |||
e e | |||
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.: 50-281 UNIT NAME: _.Su_r_r_y__U_n-it__2_____ | |||
DATE: 10/05/89 COMPLETED BY: -=ch~r~i~s~t~l-e-A~r-n_e_y____ | DATE: 10/05/89 COMPLETED BY: -=ch~r~i~s~t~l-e-A~r-n_e_y____ | ||
TELEPHONE: (804)357-3184 x477 MONTH: SEPTEMBER 1989 | TELEPHONE: (804)357-3184 x477 MONTH: SEPTEMBER 1989 | ||
| Line 179: | Line 163: | ||
==SUMMARY== | ==SUMMARY== | ||
OF OPERATING EXPERIENCE MONTH/YEAR: SEPTEMBER 1989 | OF OPERATING EXPERIENCE MONTH/YEAR: SEPTEMBER 1989 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents. | ||
Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents. | |||
UNIT ONE 09-01-89 0000 This reporting period begins with the Unit at 80% | UNIT ONE 09-01-89 0000 This reporting period begins with the Unit at 80% | ||
power. 650 MW. 'C' waterbox cleaning. | power. 650 MW. 'C' waterbox cleaning. | ||
| Line 207: | Line 189: | ||
MONTH/YEAR: | MONTH/YEAR: | ||
SEPTEMBER-1989 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents. | SEPTEMBER-1989 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents. | ||
UNIT ONE 09-22-89 0543 Start ramp up at 76% power. 1-PT-29.1 completed. 600 MW. | UNIT ONE 09-22-89 0543 Start ramp up at 76% power. 1-PT-29.1 completed. 600 MW. | ||
| Line 221: | Line 202: | ||
MONTH/YEAR: | MONTH/YEAR: | ||
SEPTEMBER 1989 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents. | SEPTEMBER 1989 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents. | ||
UNIT-TWO 09-01-89 0000 Unit started reporting period at Cold Shutdown. | UNIT-TWO 09-01-89 0000 Unit started reporting period at Cold Shutdown. | ||
| Line 244: | Line 224: | ||
9 | 9 | ||
8 | 8 | ||
| Line 296: | Line 275: | ||
UNIT TWO 09-28-89 1059 Commence ramp down from 40% power, 290 MW. | UNIT TWO 09-28-89 1059 Commence ramp down from 40% power, 290 MW. | ||
1135 Secure ramp at 200 MW for vibration data. | 1135 Secure ramp at 200 MW for vibration data. | ||
1154 Commence ramp down. | 1154 Commence ramp down. | ||
1235 Secure ramp at 110 MW for vibration data. | 1235 Secure ramp at 110 MW for vibration data. | ||
| Line 309: | Line 287: | ||
12 | 12 | ||
e e | e e FACILITY CHANGES REQUIRING NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 13 | ||
FACILITY CHANGES REQUIRING NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 13 | |||
MONTH/YEAR: | MONTH/YEAR: | ||
SEPTEMBER 1989 DC-84-70 PRESSURIZER SAFETY VALVE LOOP-SEAL INSULATION OVEN - UNIT 2 This design change installed metal reflective thermal insulation boxes which will enclose the safety valves loop seal piping. | SEPTEMBER 1989 DC-84-70 PRESSURIZER SAFETY VALVE LOOP-SEAL INSULATION OVEN - UNIT 2 This design change installed metal reflective thermal insulation boxes which will enclose the safety valves loop seal piping. | ||
This is to maintain the loop seal water temperature at approxi-mately 400°F. This temperature will allow part of the water to flash to steam after passing through the safety valves. The reduced density of the watersteam mixture will cause reduced fluid transient loads for the piping and supports. | This is to maintain the loop seal water temperature at approxi-mately 400°F. This temperature will allow part of the water to flash to steam after passing through the safety valves. The reduced density of the watersteam mixture will cause reduced fluid transient loads for the piping and supports. | ||
| Line 341: | Line 315: | ||
15 | 15 | ||
e | e FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 TM-Sl-89-165 TEMPORARY MODIFICATION 13-89 Temporary Modification to document that a hose from the Fire Pro-tection air compressor will be connected to the upstream side of the fill valve for Main Control Room air bottles located in the cable tunnel and a hose will be run through the fire door separating #1 and #2 Emergency Switchgear Rooms and the #3 Mechanical Equipment Room fire door. | ||
FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 TM-Sl-89-165 TEMPORARY MODIFICATION 13-89 Temporary Modification to document that a hose from the Fire Pro-tection air compressor will be connected to the upstream side of the fill valve for Main Control Room air bottles located in the cable tunnel and a hose will be run through the fire door separating #1 and #2 Emergency Switchgear Rooms and the #3 Mechanical Equipment Room fire door. | |||
The Main Control Room pressure boundary will not be breached, fire doors will be closed if required, and air bottle banks will remain operable while l-TOP-2128 is in effect. Therefore, no unreviewed safety question is created. | The Main Control Room pressure boundary will not be breached, fire doors will be closed if required, and air bottle banks will remain operable while l-TOP-2128 is in effect. Therefore, no unreviewed safety question is created. | ||
AC-S2-89-0917 ADMINISTRATIVE CONTROL 18-89 Administrative Control will be maintained to line-up service air to containment to support activities requiring service air usage. | AC-S2-89-0917 ADMINISTRATIVE CONTROL 18-89 Administrative Control will be maintained to line-up service air to containment to support activities requiring service air usage. | ||
| Line 373: | Line 345: | ||
'1 PROCEDURE OR METHOD OF OPERATION CHANGES REQUIRING NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 18 | '1 PROCEDURE OR METHOD OF OPERATION CHANGES REQUIRING NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 18 | ||
PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 2-PT-25.2 REQUEST TO CHANGE 01-89 This procedure change request requires the non-automatic contain-ment isolation vents to be opened and a safety-related MOV to be de-energized under administrative controls. | PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 2-PT-25.2 REQUEST TO CHANGE 01-89 This procedure change request requires the non-automatic contain-ment isolation vents to be opened and a safety-related MOV to be de-energized under administrative controls. | ||
An unreviewed safety question does not exist since administrative control of the vent valves and of the MOV will be required and utilized in accordance with Technical Specification 1.0.H, definition of containment integrity, and Surry Power Station's Administrative procedures. | An unreviewed safety question does not exist since administrative control of the vent valves and of the MOV will be required and utilized in accordance with Technical Specification 1.0.H, definition of containment integrity, and Surry Power Station's Administrative procedures. | ||
| Line 385: | Line 355: | ||
TESTS AND EXPERIMENTS REQUIRING NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 20 | TESTS AND EXPERIMENTS REQUIRING NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 20 | ||
. ] | . ] | ||
TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 21 | TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 21 | ||
~. \ | ~. \ | ||
*Z:....,....t, r VIRGINIA POWER SURRY POWER STATION CHEMISTRY REPORT MONTH/YEAR: SEPTEMBER 1989 PRIMARY COOLANT UNIT NO. 1 UNIT NO. 2 ANALYSIS MAX. MIN. AVG. MAX. MIN. AVG. | *Z:....,....t, r VIRGINIA POWER SURRY POWER STATION CHEMISTRY REPORT MONTH/YEAR: SEPTEMBER 1989 PRIMARY COOLANT UNIT NO. 1 UNIT NO. 2 ANALYSIS MAX. MIN. AVG. MAX. MIN. AVG. | ||
(1) | (1) | ||
Revision as of 22:39, 2 February 2020
| ML18152A304 | |
| Person / Time | |
|---|---|
| Site: | Surry |
| Issue date: | 09/30/1989 |
| From: | Arney C, Stewart W VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| 89-737, NUDOCS 8910230097 | |
| Download: ML18152A304 (27) | |
Text
'
\ '
v e e
- - VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 October 16, 1989 U.S. Nuclear Regulatory Commission Serial No.89-737 Attention: Document Control Desk NO/RPC:vlh Washington, D. C. 20555 Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 Gentlemen:
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of September 1989.
Very truly yours,
\\JL\~
W. L. Stewart Senior Vice President - Power Enclosure cc: U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N. W.
Suite 2900 Atlanta, Georgia 30323 Mr. W. E. Holland NRC Senior Resident Inspector Surry Power Station
/
I i
I I
\ '
I \ \,
e
- - - _y_ _ _ _ -- -
e POW 34-04 VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT 89-09 APPROVED:
l,
~-----
e e TABLE OF CONTENTS SECTION PAGE Operating Data Report - Unit No. 1 1 Operating Data Report - Unit No. 2 2 Unit Shutdowns and Power Reductions - Unit No. 1 3 Unit Shutdowns and Power Reductions - Unit No. 2 4 Average Daily Unit Power Level - Unit No. 1 5 Average Daily Unit Power Level - Unit No. 2 6 Summary of Operating Experience - Unit No. 1 7 Summary of Operating Experience - Unit No. 2 9 Facility Changes Requiring NRC Approval 13 Facility Changes That Did Not Require NRC Approval 14 Procedure or Method of Operation Changes Requiring NRC Approval 18 Procedure or Method of Operation Changes that Did Not Require NRC Approval 19 Tests and Experiments Requiring NRC Approval 20 Tests and Experiments That Did Not Require NRC Approval 21 Chemistry Report 22 Fuel Handling - Unit No. 1 23 Fuel Handling - Unit No. 2 23 Description of Periodic Test Which Were Not Completed Within the Time Limits Specified in Technical Specifications 24
e OPERATING DATA REPORT DOCKET NO.: 50-280 DATE: 10/05/89 COMPLETED BY: Christle Arney TELEPHONE: (804)357-3184 x477 OPERATING STATUS NOTES
- 1. Unit Name: Surry Unit 1
- 2. Reporting Period: Sept 1 - 30, 1989
- 3. Licensed Thermal Power (MWt):2441
- 4. Nameplate Rating (Gross MWe):847.5
- 5. Design Electrical Rating (Net MWe): 788
- 6. Maximum Dependable Capacity (Gross MWe): 820
- 7. Maximum Dependable Capacity (Net MWe): 781
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
- 9. Power Level To Which Restricted, If Any (Net MWe):
- 10. Reason For Restrictions, If Any: --------------
THIS MONTH YTD CUMULATIVE
- 11. Hours In Reporting Period 720.0 6551. 0 147047.0
- 12. Number of Hours Reactor Was Critical 720.0 2088.0 90566.6
- 13. Reactor Reserve Shutdown Hours 0 0 3774.5
- 14. Hours Generator On-Line 720.0 2036.7 88642.1
- 15. Unit Reserve Shutdown Hours 0 0 3736.2
- 16. Gross Thermal Energy Generated (MWH) 1724771.0 4685347.0 205856614.0
- 17. Gross Electrical Energy Generated (MWH) 578765.0 1554915.0 66758588.0
- 18. Net Electrical Energy Generated (MWH) 547473.0 1469275.0 63309678.0
- 19. Unit Service Factor 100% 31.1% 60.3%
- 20. Unit Available Factor 100% 31.1% 62.8%
- 21. Unit Capacity Factor (Using MDC Net) 97.4% 28.7% 55.6%
- 22. Unit Capacity Factor (Using DER Net) 96.5% 28.5% 54.6%
- 23. Unit Forced Rate 0% 68.9% 22.0%
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
- 25. If Shut Down at End of Report Period Estimated Date of Startup: _ _ _ _ _ __
- 26. Unit In Test Status (Prior to Commercial Operation): FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 1
e OPERATING DATA REPORT DOCKET NO.: 50-281 DATE: 10/05/89 COMPLETED BY: Christle Arney TELEPHONE: (804)357-3184 x477 OPERATING STATUS NOTES
- 1. Unit Name: Surry Unit 2
- 2. Reporting Period: Sept 1 - 30, 1989
- 3. Licensed Thermal Power (MWt): 2441
- 4. Nameplate Rating (Gross MWe): 847.5
- 5. Design Electrical Rating (Net MWe): 788
- 6. Maximum Dependable Capacity (Gross MWe): 820
- 7. Maximum Dependable Capacity (Net MWe): -781 ---
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
- 9. Power Level To Which Restricted, If Any (Net MWe):
- 10. Reason For Restrictions, If Any: -------------
THIS MONTH YTD CUMULATIVE
- 11. Hours In Reporting Period 720.0 6551.0 143927.0
- 12. Number of Hours Reactor Was Critical 327.9 327.9 90022.2
- 13. Reactor Reserve Shutdown Hours 0 0 328.1
- 14. Hours Generator On-Line 189 189 88482
- 15. Unit Reserve Shutdown Hours 0 0 0
- 16. Gross Thermal Energy Generated (MWH) 187755.9 187755. 9 206928192.0
- 17. Gross Electrical Energy Generated (MWH) 46725.0 46725.0 67182969.0
- 18. Net Electrical Energy Generated (MWH) 40831. 0 40831.0 63688209.0
- 19. Unit Service Factor 26.3% 2.9% 61.5%
- 20. Unit Available Factor 26.3% 2.9% 61.5%
- 21. Unit Capacity Factor (Using MDC Net) 7.3% .8% 56.8%
- 22. Unit Capacity Factor (Using DER Net) 7.2% .8% 56.2%
- 23. Unit Forced Rate 34.4% 34.4% 15.0%
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
- 25. If Shut Down at End of Report Period Estimated Date of Startup=----------==--
- 26. Unit In Test Status (Prior to Commercial Operation): FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 2
I I
UNIT SHUTDOWN AND POWER REDUCTION DOCKET NO.: 50-280 UNIT NAME: -s~u-rry-""':U:,:On~i~t'""""':11_____1 '
- 1
- DATE: 10/05/89 * ,\.,.
COMPLETED BY: Christle Arney TELEPHONE: -,...,80""'4,---=3-=-5=-7_""'!!3"""1-=8"""4"""x..,4,. ,7""'7- \
REPORT MONTH:
SEPTEMBER 1989
~ME=mo=~D:"'""!:O~F~---=L-=I~c=EN~s=E=E:-------------c=-A:-:U~S~E:"""'!'&--.::'CO=RRE=:-:c~T~I=VE~----- \
I DURATION SHU'ITIN'G EVENT SYSTEM COMPONENT ACTION TO PREVENT i NO. DATE TYPE(l) (HOURS) REASON(2) DOWN REACTOR(3) REPORT# CODE(4) CODE(5) RECURRENT \
1I 09-01-89 S 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> B 1 N/A KE COND Cleaned Waterbox 'C' \
40 min.
09-01-89 F 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> 54 min.
A 1 N/A SL lPBU 'A I Bus Duct cooling fan motor grounded - placed e \\ I
\
alternate motor in service. ,
Cleaned 'A', 'D' water- \\
boxes. !
09-09-89 s 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> B 1 N/A KE COND Clean waterboxes 'A' and 36 min. 'CI.
09-10-89 s 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> B 1 N/A KE COND Clean waterboxes 'B' and 10 min. 'C' 09-21-89 s 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> B 1 'N/A SB TRB Tested Main Turbine Valves 14 min. in accordance with l-PT-29.1 09-26-89 s 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> B 1 N/A. KE COND Cleaned waterboxes 'B' and 55 min. 'C' e
(1) (2) (3) (4)
F: Forced REASON: METHOD:
S: Scheduled A - Equipment Failure (Explain) 1 - Manual Exhibit G - Instructions for B - Maintenance or Test 2 - Manual Scram. Preparation of Data Entry Sheets C - Refueling 3 - Automatic Scram. for Licensee Event Report (LER)
D - Regulatory Restriction 4 - Other (Explain) File (NUREG 0161)
E - Operator Training & License Examination F - Administrative (5)
G - Operational Error (Explain)
H - Other (Explain) Exhibit 1 - Same Source 3
' \.
DOCKET NO.: 50-281 \
- UNIT SHUTDOWN AND POWER REDUCTION UNIT NAME: """""s-u-rry-""'Un.....,i,..t-.:2,----
DATE: 10/05/89 r \-
COMPLETED BY: Christle Arney \
REPORT MONTH: SEPTEMBER 1989 TELEPHONE:
- 804-357-3184 x477\
METHOD OF LICENSEE CAUSE & CORRECTIVE DURATION SHUTTING EVENT SYSTEM COMPONENT ACTIOOO TO PREVENT NO. DATE TYPE(l) (HOURS) REASON(2) DOWN REACTOR(3) REPORT# CODE(4) CODE(5) RECURRENT
\
C-10-1 09-18-89 F 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> A 3 2-89-009 EL GEOO Main Generator Lockout trip\
4 min. when exciter field breaker\
closed. Repaired Genera~
Leads Differential Relay~
C-10-2 09-19-89 F 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> G 3 2-89-010 JB SG 'B' Steam Generator Lo-Lo \
50 min. Level while attempting to place Main Feed Regulator Valves inservice.
09-22-89 F 19 hours2.199074e-4 days <br />0.00528 hours <br />3.141534e-5 weeks <br />7.2295e-6 months <br /> B 1 N/A TA TRB Unit taken off line for 49 min. Turbine Overspeed Test and Balancing of Main Turbine. Reactor remained Critical.
09-28-89 F 57 hours6.597222e-4 days <br />0.0158 hours <br />9.424603e-5 weeks <br />2.16885e-5 months <br /> B 1 N/A TA TRB Unit taken off line for 55 min. Turbine Balancing. Reactor remained critical.
e (1) (2) (3) (4)
F: Forced REASON: METHOD:
S: Scheduled A - Equipment Failure (Explain) 1 - Manual Exhibit G - Instructions for B - Maintenance or Test 2 - Manual Scram. Preparation of Data Entry Sheets C - Refueling 3 - Automatic Scram. for Licensee Event Report (LER)
D - Regulatory Restriction 4 - Other (Explain) File (NUREG 0161)
E - Operator Training & License Examination F - Administrative (5)
G - Operational Error (Explain)
H - Other (Explain) Exhibit 1 - Same Source 4
e e AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.: 50-280*
- UNIT NAME: Surry Unit 1 DATE: 10705789 COMPLETED BY: Christle Arney
- TELEPHONE:(8045357-3184 x477 MONTH: SEPTEMBER 1989 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 653 17 770 2 715 18 768 3 775 19 766 4 778 20 778 5 777 21 766 6 777 22 716 7 776 23 779 8 773 24 783 9 712 25 783 10 698 26 774 11 772 27 722 12 770 28 786 13 769 29 785 14 769 30 785 15 769 31 16 770 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
5
e e AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.: 50-281 UNIT NAME: _.Su_r_r_y__U_n-it__2_____
DATE: 10/05/89 COMPLETED BY: -=ch~r~i~s~t~l-e-A~r-n_e_y____
TELEPHONE: (804)357-3184 x477 MONTH: SEPTEMBER 1989
- DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 0 17 0 2 0 18 0 3 0 19 134 4 O* 20 165 5 0 21 165 6 0 22 173 7 0 23 251 8 0 24 240 9 0 25 240 10 0 26 244 11 0 27 247 12 0 28 216 13 0 29 0 14 0 30 0 15 0 31 16 0 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
6
\,
SUMMARY
OF OPERATING EXPERIENCE MONTH/YEAR: SEPTEMBER 1989 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT ONE 09-01-89 0000 This reporting period begins with the Unit at 80%
power. 650 MW. 'C' waterbox cleaning.
0700 Start ramp up from 80% power.
0940 100% power. 820 MW.
1726 Start ramp down at 100% power. 'A' Bus duct fan tripped.
1844 Stop ramp at 67.5%. 540 MW.
09-02-89 0020 Start ramp up at 70% power. 530 MW. 'A' phase Bus duct fan returned to service; 'A' waterbox cleaned.
0118 Stop ramp at 80% power. 625 MW. 'D' waterbox out of service.
0350 Start ramp up at 80%. 625 MW. 'D' waterbox returned to service.
0903 Stop ramp at 100% power. 825 MW.
09-09-89 0038 Start ramp down for waterbox cleaning at 100% power.
810 MW.
0214 Stop ramp at 80% power. 650 MW.
1002 Start ramp up at 82% power. 'C', 'A' waterbox cleaned.
660 MW.
1214 Stop ramp at 100% power. 820 MW.
09-10-89 0041 Start ramp down at 100% power. Clean waterbox. 820 MW.
0209 Stop ramp at 80% power. 650 MW.
1141 Start ramp up at 81% power. 665 MW. 'BI' 'D' waterboxes cleaned.
1351 Stop ramp at 100% power. 820 MW.
09-21-89 2205 Start ramp down from 100% power for l-PT-29.1. 815 MW.
2345 Stop ramp at 75% power. 610 MW.
7
MONTH/YEAR:
SEPTEMBER-1989 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT ONE 09-22-89 0543 Start ramp up at 76% power. 1-PT-29.1 completed. 600 MW.
0719 Stop ramp up at 100% power. 800 MW.
09-26-89 2205 Start ramp down from 100% power for waterbox cleaning.
820 MW.
2325 Stop ramp at 80%. 658 MW.
09-27-89 0839 Start ramp up from 82%. 'B', 'C' waterbox cleaned.
650 MW.
1000 Stop ramp at 100% power. 820 MW.
09-30-89 2400 Unit ended reporting period at 100% power.
8
MONTH/YEAR:
SEPTEMBER 1989 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT-TWO 09-01-89 0000 Unit started reporting period at Cold Shutdown.
09-10-89 2310 Reactor Coolant System> 200°.
09-13-89 2003 Reactor Coolant System> 350°.
09-14-89 1048 Unit at Hot Shutdown.
09-16-89 1016 'A' and 'B' Shutdown Banks withdrew in preparation for dilution.
1200 Commence pull to Criticality.
1228 Experienced problems with bank overlap, 'A' Control Bank was at 13 steps and 'B' Bank was at 15 steps.
Bank overlap unit was at 143 steps. Manually tripped reactor.
1458 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> report for Manual Reactor Trip.
1744 Commenced Reactor Start-up.
1950 Reactor Critical. 'D' Bank at 147 steps.
-8 2000 Reactor stable at 10 amps. 'D' Bank at 140 steps.
TAV=544.5. CB - 1531; Letdown 1533 Pressure.
09-18-89 1030 Increased Reactor power> 10% in preparation for going on line.
1042 Reactor Trip. First Outs EA8 (Reactor Trip by Turbine Trip) and F-E-1 (Generator Backup Lockout Relay Trip).
Enter EP occurred while attempting to raise generator voltage, 1045 Closed Main Steam Trip Valves to stop cooldown.
1115 Unit stable at Hot Shutdown.
1546 Reactor Critical.
-8 1555 Reactor at 10 amps 'D' Bank 152 steps; Tave-544.5; Reactor Coolant System Boron 1526 ppm.
9
8
SUMMARY
OF OPERATING EXPERIENCE MONTH/YEAR: SEPTEMBER 1989 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT TWO 09-19-89 0032 Output breakers closed.
0050 Reactor trip on 'B' Steam Generator Low Level.
0801 Reactor Critical; 'D' 125 steps.
8 0812 Reactor at 10- amps; Tave-547; 'D' Bank - 112 steps; Reactor Coolant System Boron 1500 ppm.
2105 Unit on line.
09-20-89 0200 Turbine load at 200 MW, Reactor Power at 34%.
09-21-89 2134 Commence ramp up at 3%/hr, Reactor power 34%, 195 MW.
2227 Reactor power at 37%, 220 MW, Turbine Vibrations - 7.26 mils.
2354 Secured ramp at 41.5%, 255 MW, due to turbine vibration.
09-22-89 0626 Start ramp down at 150/hr to 30% power. 39% power, 240 MW.
0700 Stop ramp at 30% power, 190 MW.
0930 Received report of seal leak on 2-FW-P-lB. Inboard seal failed.
0934 Start 2-FW-P-lA.
0935 Secured 2-FW-P-lB.
1013 Commenced unit ramp down for Turbine Overspeed Test and Balance.
1130 Generator off line.
1207 Turbine Overspeed Test Tripped at 1954 RPM OP-2.2.6.
10
- -----~
SUMMARY
OF OPERATING EXPERIENCE MONTH/YEAR: SEPTEMBER 1989 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT TWO 09-23-89 0719 Unit on line.
0803 Holding ramp at 120 MW.
1024 Commence ramp up at 3%/hr.
2006 Reactor Power 59%, 410 MW.
2045 Holding ramp at 59.5%, 410 MW.
2258 Commence ramp down for turbine vibrations. Reactor power 59%, 410 MW.
2330 Secured ramp at 50% power, 360 MW.
2333 Commence ramp down.
09-24-89 0010 Secured ramp down at 40% power, 290 MW.
09-26-89 1300 Commence ramp up to monitor turbine vibrations.
Reactor power 40%, 270 MW.
1312 Secured ramp at 40.5% power while Instrument Technicians replace Individual Rod Position Indicator F-8 (2-PT-5 .1).
1400 Instrument Technicians complete replacement of F-8.
Commence ramp up at 30%/hr.
1539 Holding ramp at 46%, 330 MW. Turbine vibrations increasing.
1654 Commence ramp down. Reactor power 46%, 330 MW, due to High Vibration on Main Turbine.
1735 Secured ramp at 40% power, 285 MW. #5 Bearing - 5.5 mils, #6 Bearing - 5.8 mils.
09-27-89 0931 Start ramp up at 40% power, 290 MW.
0932 Secured ramp at 40% power, 290 MW.
11
Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT TWO 09-28-89 1059 Commence ramp down from 40% power, 290 MW.
1135 Secure ramp at 200 MW for vibration data.
1154 Commence ramp down.
1235 Secure ramp at 110 MW for vibration data.
1250 Commence ramp down.
1405 Unit off line in order to balance main turbine jackshaft.
1421 Manually tripped turbine.
09-29-89 0234 2-CH-RV-2203 lifted when letdown line flashed when charging flow was reduced in "AUTO".
09-30-89 0645 Start up Reactor power to 2% to bring in steam.
1913 2-CH-RV-2203 repair complete.
2400 Ended the reporting period with the reactor at 2%
power. Turbine Balance was complete and preparations were under way to place unit back on line.
12
e e FACILITY CHANGES REQUIRING NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 13
MONTH/YEAR:
SEPTEMBER 1989 DC-84-70 PRESSURIZER SAFETY VALVE LOOP-SEAL INSULATION OVEN - UNIT 2 This design change installed metal reflective thermal insulation boxes which will enclose the safety valves loop seal piping.
This is to maintain the loop seal water temperature at approxi-mately 400°F. This temperature will allow part of the water to flash to steam after passing through the safety valves. The reduced density of the watersteam mixture will cause reduced fluid transient loads for the piping and supports.
SUMMARY
OF SAFETY ANALYSIS The installation of the boxes will not affect the operation of the pressurizer or the safety valves. The boxes will reduce fluid transient loads to ensure the piping and supports are qualified for the design basis transients once the supports have been modified. The boxes do not affect any safety related system or component and does not impact any Technical Specification.
DC-88-36 CONTROL ROOM ENVELOPE HEATING, VENTILATING, AIR CONDITIONING (HVAC) INTERIM MODIFICATIONS - UNITS 1 & 2 This design change involved several modifications to the present equipment on an interim basis until larger capacity replacement equipment can be procured (approximately 24 months). The redun-dancy of certain equipment had been lost due to increased heat loads exceeding the rated capacity of the equipment.
Each of the air handling units had a redundant drive motor installed which was powered from a different power source. This will ensure operability of the air handling unit from a loss of the drive motor or it power source. In addition, the belt drive was modified to increase the fan speed and therefore increase the air flow and cooling capacity. The increased air flow through the ventilation ducting created the requirement to modify the ducting to keep the air velocity below 2,000 feet per minute (FPM).
One of the chillers and support equipment, i.e. chilled water and service water pumps and chilled water outlet MOV, was provided with a redundant source of power.
SUMMARY
OF SAFETY ANALYSIS This design change .restores the control room and emergency switchgear room Technical Specification design basis by ensuring that equipment and operational capability exists to compensate for normal and accident heat loads therein. The installation of the new motors will not affect other safety-related equipment or the qualification of the air handling units. The redundancy of the HVAC system is restored to provide single failure protection.
The added equipment is seismically qualified and seismically installed and supported.
14
. FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 SCAFFOLDING REQUEST 01-89 This request is to document the erection of temporary scaffolding located in the Emergency Service Water Pump House to support painting and associated preparatory work.
Installation of this temporary scaffolding was reviewed for effect on accident analyses and equipment operability/function.
Conclusion is that assumptions, bases and probabilities of accident analyses and equipment malfunctions are not affected.
TM-SZ-89-114 TEMPORARY MODIFICATION 01-89 Temporary Modification to document that "B" Reactor Coolant Pump Containment Isolation Valve for Component Cooling (TV-CC-205B) will be blocked open using a split schedule 80 pipe with clamps attached to the valve stem. This modification will be installed to maintain component cooling flow during certain testing performed at cold shutdown.
Technical Specification 3.8.A.l requires that containment integrity is maintained when in refueling mode or above cold shutdown. The isolation valve will only be blocked for the duration of the test. The valve will be returned to service prior to exceeding cold shutdown. Therefore, no unreviewed safety question is created.
TM-SZ-89-118 TEMPORARY MODIFICATION 04-89 This modification was to document that 2-DA-TV-200B was removed to allow repair. A spool piece was installed in its place to allow continued operation of the containment sump pump.
This Temporary Modification does not present an unreviewed safety question since the unit will be at cold shutdown throughout the Temporary Modification installation. 2-DA-TV-200A will remain operational allowing closure for isolation of the flow path from containment, if required.
AC-SZ-89-0909 ADMINISTRATIVE CONTROL 09-89 Administrative control will be maintained to ensure that TV-CV-250D will remain closed until it is operable. The solenoid leads will be lifted, the air to the solenoid will be tagged closed and the valve will be under Administrative Control.
Failing TV-CV-250D closed has been evaluated and it is determined that since the valve will be in its closed (accident) position the consequences or probability of any accident will not be increased. This change will not create an unreviewed safety question.
15
e FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 TM-Sl-89-165 TEMPORARY MODIFICATION 13-89 Temporary Modification to document that a hose from the Fire Pro-tection air compressor will be connected to the upstream side of the fill valve for Main Control Room air bottles located in the cable tunnel and a hose will be run through the fire door separating #1 and #2 Emergency Switchgear Rooms and the #3 Mechanical Equipment Room fire door.
The Main Control Room pressure boundary will not be breached, fire doors will be closed if required, and air bottle banks will remain operable while l-TOP-2128 is in effect. Therefore, no unreviewed safety question is created.
AC-S2-89-0917 ADMINISTRATIVE CONTROL 18-89 Administrative Control will be maintained to line-up service air to containment to support activities requiring service air usage.
Administrative Control of the valves will maintain containment integrity and the valves provide redundant isolation capability.
Therefore, no unreviewed safety question is created.
SCAFFOLDING REQUEST 21-89 This request is to document the erection of temporary scaffolding located in Unit 2 cable vault to work cable tray covers.
Installation of this temporary scaffolding was reviewed for effect on accident analyses and equipment operability/function.
Conclusion is that assumptions, bases and probabilities of accident analyses and equipment malfunctions are not affected.
SCAFFOLDING REQUEST 21-89 This request is to document the erection of temporary scaffolding located in #3 Mechanical Equipment Room to work l-VS-PCV-531.
Installation of this temporary scaffolding was reviewed for effect on accident analyses and equipment operability/function.
Conclusion is that assumptions, bases and probabilities of accident analyses and equipment malfunctions are not affected.
SCAFFOLDING REQUEST 21-89 This request is to document the erection of temporary scaffolding located in the Fire Pump House, in the diesel driven fire pump area for painting.
Installation of this temporary scaffolding was reviewed for effect on accident analyses and equipment operability/function.
Conclusion is that assumptions, bases and probabilities of accident analyses and equipment malfunctions are not affected.
16
- e FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 JC0-89-311 JUSTIFICATION FOR CONTINUED OPERATION 26-89 This JCO provides compensatory actions to ensure the Emergency Service Water pump diesel drivers will reliably start when the outside ambient temperature is below 50°F.
The JCO provides actions to be taken to ensure that the Emergency Service Water pump house temperature remains above the manufac-turer's recommended minimum temperature for reliable diesel starting. Therefore, no unreviewed safety question is created via this JCO.
SCAFFOLDING REQUEST 27-89 This request is to document erection of temporary scaffolding located in Unit 2 Safeguards Basement (Steam side) for cable tray cover installation.
Installation of this temporary scaffolding was reviewed for effect on accident analyses and equipment operability/function.
Conclusion is that assumptions, bases and probabilities of accident analyses and equipment malfunctions are not affected.
SCAFFOLDING REQUEST 27-89 This request is to document erection of temporary scaffolding located in Unit 1 valve pit at the 12' level for cable tray cover installation.
Installation of this temporary scaffolding was reviewed for effect on accident analyses and equipment operability/function.
Conclusion is that assumptions, bases, and probabilities of accident analyses and equipment malfunctions are not affected.
UFSAR CHANGE REQUEST FOR SECTION 9.1.2.6.21 27-89 UFSAR Change Request to clarify the operating sequence between the duplicate heat trace circuits and enhance the coordination of the primary circuit under-temperature setpoint with the backup circuit control setpoint.
The 10CFR50.59 Review concluded that an unreviewed safety question was not created. Malfunction of Heat Trace Circuit will not contribute to an over dilution. If Boric Acid precipitation occurred, alternate Chemical Volume and Control System flow paths exist.
17
'1 PROCEDURE OR METHOD OF OPERATION CHANGES REQUIRING NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 18
PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 2-PT-25.2 REQUEST TO CHANGE 01-89 This procedure change request requires the non-automatic contain-ment isolation vents to be opened and a safety-related MOV to be de-energized under administrative controls.
An unreviewed safety question does not exist since administrative control of the vent valves and of the MOV will be required and utilized in accordance with Technical Specification 1.0.H, definition of containment integrity, and Surry Power Station's Administrative procedures.
l-TOP-2128 PROCEDURE CHANGE REQUEST 13-89 Procedure to document that a hose from Fire Protection air compressor will be connected to upstream side of fill valve for Main Control Room air bottles located in cable tunnel and a hose will be run through the fire door separating 1 and 2 Emergency Switchgear Rooms and the #3 Mechanical Equipment Room fire door.
The Main Control Room pressure boundary will not be breached, fire doors will be closed if required, and air bottle banks will remain operable while this Temporary Operating Procedure is in effect. No unreviewed safety question created.
19
4,.
._,_, (
TESTS AND EXPERIMENTS REQUIRING NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 20
. ]
TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 21
~. \
- Z:....,....t, r VIRGINIA POWER SURRY POWER STATION CHEMISTRY REPORT MONTH/YEAR: SEPTEMBER 1989 PRIMARY COOLANT UNIT NO. 1 UNIT NO. 2 ANALYSIS MAX. MIN. AVG. MAX. MIN. AVG.
(1)
Gross Radioact., µCi/ml 8. 44 (E-1) 4.15(E-1) 6.52(E-1) I. 23 (E-1) 7.lO(E-4) 2.79(E-2)
Suspended Solids, ppm 0.0 o.o o.o o.o 0.0 0.0 Gross Tritium, µCi/ml 3.15 (E-1) 2. 91 (E-1) 2.99(E-1) I. 72 (E-2) 1.10 (E-2) 1. 41 (E-2)
Iodine-131, µCi/ml 7.14(E-3) 2.14(E-3) 3,36(E-3) 2.60(E-4) 1.51(E-5) 9.73(E-5)
Iodine-131/Iodine-133 0.18 0.08 0.12 0.07 0.07 0.07 Hydrogen, cc/kg 28.6 25.5 27.7 34.0 23,0 27.6 Lithium, ppm 2.33 2.06 2.24 2.86 1.33 2.02 Boron - 10, ppm* 158 143 150 434 240 314 Oxygen, (DO)* ppm 0.005 0.005 0.005 0.005 0.005 0.005 Chloride, ppm 0.012 0.007 0.009 0.014 0.008 0.011 pH@ 25 degree Celsius 6.76 6.61 6.67 6.34 5.63 5.93
Unit one started September at 100% power with BMB in service. On September 1, 140 grams of lithium were added. Later on September 1, the unit ramped back to 70% to clean water boxes. On September 9, the unit ramped to 77% to clean water boxes. On September 24, the unit ramped back to 74% to conduct turbine valve freedom tests. On September 26, the unit ramped back to 80% to clean water boxes, and ended the month at 100% full power.
UNIT TWO:
Unit two started the month at cold shutdown with BMB and RHR in service. On September 7 the "A" RCP was placed in service and "B" taken out. On September 10 the unit exceeded 200°F just prior to midnight while heating up towards startup. On September 11 the "C" RCP was taken out of service because of high temperature buildup within the pump. On September 16, 2167 grams of lithium were added to the RCS. The reactor startup commenced on September 16 at 1205 hours0.0139 days <br />0.335 hours <br />0.00199 weeks <br />4.585025e-4 months <br /> and went critical at 1950 hours0.0226 days <br />0.542 hours <br />0.00322 weeks <br />7.41975e-4 months <br />. The RCS dissolved hydrogen was out-of-specification after criticality until 0310 hours0.00359 days <br />0.0861 hours <br />5.125661e-4 weeks <br />1.17955e-4 months <br /> on September 17. On September 18, 162 grams and then another 243 grams of lithium were added to the RCS. On September 19, 162 grams of lithium were added to the RCS. On September 29, letdown was isolated due to a leaking relief valve on the letdown system. The unit ended the month at 2% power.
22
... e FUEL HANDLING DATE: SEPTEMBER 1989
~, '
NEW OR DATE NUMBER OF NEW OR SPENT SPENT FUEL SHIPPED ASSEMBLIES ASSEMBLY ANSI INITIAL FUEL SHIPPING SHIPMENT II OR RECEIVED PER SHIPMENT NUMBER NUMBER ENRICHMENT CASK ACTIVITY LEVEL NONE DURING THIS PERIOD 23
~, r DESCRIPTION OF PERIODIC TEST WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR: SEPTEMBER 1989 NONE DURING THIS PERIOD 24