PNO-III-15-001, A: Update: Shutdown of Prairie Island Unit 1 Due to Increasing Trend in Reactor Coolant System Leakage: Difference between revisions

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{{#Wiki_filter:PRELIMINARY NOTIFICATION February 17, 2015 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE-PNO-III-15-001A This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. Some of the information may not yet be fully verified or evaluated by the Region III staff.
{{#Wiki_filter:PRELIMINARY NOTIFICATION February 17, 2015 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE-PNO-III-15-001A This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. Some of the information may not yet be fully verified or evaluated by the Region III staff.
Facility Prairie Island Nuclear Plant Northern States Power Co.  
Facility                                           Licensee Emergency Classification Prairie Island Nuclear Plant                           Notification of Unusual Event Northern States Power Co.                             Alert Welch, MN                                             Site Area Emergency Docket: 50-282                                         General Emergency License: DPR-42                                     X Not Applicable
 
Welch, MN Docket: 50-282 License: DPR-42 Licensee Emergency Classification Notification of Unusual Event Alert      Site Area Emergency General Emergency  X   Not Applicable


==SUBJECT:==
==SUBJECT:==
UPDATE: SHUTDOWN OF PRAIRIE ISLAND UNIT 1 DUE TO INCREASING TREND IN REACTOR COOLANT SYSTEM LEAKAGE Prairie Island Unit 1 was restarted on February 11, 2015. Prairie Island Unit 1 was shut down on January 26, 2015, to repair a leak from one of two reactor coolant pumps. The leak was identified after plant operators observed an increasing trend in the reactor coolant system leakage rate following repairs made to the reactor coolant pump seal in December. The plant shut down prior to the seal leakage reaching the licensee's administrative limit, which was lower than the 1 gallon per minute (gpm) limit specified in the Technical Specifications. The peak leakage measured was 0.596 gpm. The reactor coolant pumps ensure adequate cooling of the reactor when the plant is operating. There was no release to the environment from this event.  
UPDATE: SHUTDOWN OF PRAIRIE ISLAND UNIT 1 DUE TO INCREASING TREND IN REACTOR COOLANT SYSTEM LEAKAGE Prairie Island Unit 1 was restarted on February 11, 2015. Prairie Island Unit 1 was shut down on January 26, 2015, to repair a leak from one of two reactor coolant pumps. The leak was identified after plant operators observed an increasing trend in the reactor coolant system leakage rate following repairs made to the reactor coolant pump seal in December. The plant shut down prior to the seal leakage reaching the licensees administrative limit, which was lower than the 1 gallon per minute (gpm) limit specified in the Technical Specifications. The peak leakage measured was 0.596 gpm. The reactor coolant pumps ensure adequate cooling of the reactor when the plant is operating. There was no release to the environment from this event.
 
After the pump was repaired, plant operators commenced a startup and the reactor was made critical on February 11, 2015. The unit was synchronized to the electrical grid on February 12, 2015, and full power was reached on February 13, 2015. The Resident Inspectors were on site and monitored portions of the startup activities.
After the pump was repaired, plant operators commenced a startup and the reactor was made critical on February 11, 2015. The unit was synchronized to the electrical grid on February 12, 2015, and full power was reached on February 13, 2015. The Resident Inspectors were on site and monitored portions of the startup activities.  
 
This preliminary notification is issued for information only and no further action by the staff is anticipated. State officials have been informed.
This preliminary notification is issued for information only and no further action by the staff is anticipated. State officials have been informed.
The information presented herein has been discussed with the licensee, and is current as of  
The information presented herein has been discussed with the licensee, and is current as of 08:30 am CDT, on February 17, 2015.
 
ADAMS Accession Number: ML15048A179 CONTACT: Kenneth Riemer 630-829-9628 Kenneth.Riemer@nrc.gov}}
08:30 am CDT, on February 17, 2015.  
 
ADAMS Accession Number: ML15048A179 CONTACT: Kenneth Riemer 630-829-9628 Kenneth.Riemer@nrc.gov}}


{{PNO-Nav|region=III}}
{{PNO-Nav|region=III}}

Latest revision as of 16:32, 31 October 2019

PNO-III-15-001A: Update: Shutdown of Prairie Island Unit 1 Due to Increasing Trend in Reactor Coolant System Leakage
ML15048A179
Person / Time
Site: Prairie Island Xcel Energy icon.png
Issue date: 02/17/2015
From: Kenneth Riemer
NRC/RGN-III
To:
References
PNO-III-15-001A
Download: ML15048A179 (1)


PRELIMINARY NOTIFICATION February 17, 2015 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE-PNO-III-15-001A This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. Some of the information may not yet be fully verified or evaluated by the Region III staff.

Facility Licensee Emergency Classification Prairie Island Nuclear Plant Notification of Unusual Event Northern States Power Co. Alert Welch, MN Site Area Emergency Docket: 50-282 General Emergency License: DPR-42 X Not Applicable

SUBJECT:

UPDATE: SHUTDOWN OF PRAIRIE ISLAND UNIT 1 DUE TO INCREASING TREND IN REACTOR COOLANT SYSTEM LEAKAGE Prairie Island Unit 1 was restarted on February 11, 2015. Prairie Island Unit 1 was shut down on January 26, 2015, to repair a leak from one of two reactor coolant pumps. The leak was identified after plant operators observed an increasing trend in the reactor coolant system leakage rate following repairs made to the reactor coolant pump seal in December. The plant shut down prior to the seal leakage reaching the licensees administrative limit, which was lower than the 1 gallon per minute (gpm) limit specified in the Technical Specifications. The peak leakage measured was 0.596 gpm. The reactor coolant pumps ensure adequate cooling of the reactor when the plant is operating. There was no release to the environment from this event.

After the pump was repaired, plant operators commenced a startup and the reactor was made critical on February 11, 2015. The unit was synchronized to the electrical grid on February 12, 2015, and full power was reached on February 13, 2015. The Resident Inspectors were on site and monitored portions of the startup activities.

This preliminary notification is issued for information only and no further action by the staff is anticipated. State officials have been informed.

The information presented herein has been discussed with the licensee, and is current as of 08:30 am CDT, on February 17, 2015.

ADAMS Accession Number: ML15048A179 CONTACT: Kenneth Riemer 630-829-9628 Kenneth.Riemer@nrc.gov